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Difference between revisions of "37-125-23398"

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__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 37-125-23398
 
| Well ID: 37-125-23398
| style="height=100%; align=center" rowspan="14" | {{#display_map: 40.149333, -79.969302 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.149333, -79.969303 | width=100% | height=100% }}
 +
|-
 +
| Country: United States
 +
|-
 +
| State: Pennsylvania
 +
|-
 +
| County: [[Washington_County,_Pennsylvania|Washington]]
 
|-
 
|-
| Operator Name: [[CNX GAS CO LLC]]
+
| Municipality: [[Fallowfield Township,_Washington_County,_Pennsylvania|Fallowfield Township]]
 
|-
 
|-
| First Permit Date: 2008-11-10
+
| Operator Name: [[ALLIANCE PETRO CO LLC]]
 
|-
 
|-
| Last Permit Date: 2008-11-10
+
| Well Pad ID:  
 
|-
 
|-
| Spud Date: 2009-01-18
+
| Farm/Lease Name: PALUSO FF84CV
 
|-
 
|-
| Unconventional: No
+
| License Status:  
 
|-
 
|-
| Horizontal: No
+
| Spud Date:  
 
|-
 
|-
| Violations: 2
+
| Permit Date: 2008-11-10
 +
|-
 +
| Well Type: GAS
 +
|-
 +
| Unconventional Well: N
 +
|-
 +
| Configuration: Vertical Well
 +
|-
 +
| Conservation: No
 
|-
 
|-
 
| Latitude: 40.149333
 
| Latitude: 40.149333
 
|-
 
|-
| Longitude: -79.969302
+
| Longitude: -79.969303
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Permits Issued Detail Report
 +
|publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2019-05-20
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref><ref>{{cite web
 +
| title = Spud Data Report
 +
|publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2019-04-30
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-16 }}</ref><ref>{{cite web
 +
| title = Oil and Gas Well Pad Report
 +
|publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2019-05-20
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Date
 +
!scope="col" | Event
 +
|-
 +
| 2008-11-10
 +
| New Permit Application
 +
|-
 +
| 2009-01-13
 +
| Drilling Completion
 +
|-
 +
| 2009-01-18
 +
| Performed Spud Operation
 +
|-
 +
| 2009-02-04
 +
| Perforation
 +
|-
 +
| 2009-02-05
 +
| Performed Stimulation 
 +
|-
 +
| 2012-03-28
 +
| NEWLY DRILLED
 
|-
 
|-
 
|}
 
|}
__TOC__
+
For data sources see<ref>{{cite web
== Production Data ==
+
| title = Compiled from multiple data sources - see Pennsylvania Oil and Gas Data Sources
 +
| date = 2020-02-27
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-02-27 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" | Job Number
!scope="col" | GAS QUANTITY
+
!scope="col" | Job Start Date
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" | Job End Date
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" | True Vertical Depth (ft)
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" | Total Water Volume (gal)
!scope="col" | OIL QUANTITY
+
!scope="col" | Total Non-Water Volume (gal)
!scope="col" | OIL PRODUCTION DAYS
 
 
|-
 
|-
| 2013-0
+
|}-->
| style="text-align:right;" | 2083.13
+
<!--==== Fluid Composition Data ====
| style="text-align:right;" | 365.0
+
{| class="wikitable sortable" width="95%"
| style="text-align:right;" | 0.0
+
!scope="col" | Job Number
| style="text-align:right;" | 0.0
+
!scope="col" | Trade Name
| style="text-align:right;" | 0.0
+
!scope="col" | Supplier
| style="text-align:right;" | 0.0
+
!scope="col" | Purpose
 +
!scope="col" | Ingredient Name
 +
!scope="col" | CAS Number
 +
!scope="col" | Additive Percentage by Mass
 +
!scope="col" | Job Percentage by Mass
 +
!scope="col" | Mass Used (lb)
 
|-
 
|-
 +
|}-->
 +
 +
== Stimulation Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Stimulation Date
 +
!scope="col" | Phase Number
 +
!scope="col" | Chemical Agent
 +
!scope="col" | Volume (gal)
 +
!scope="col" | Treating Pressure (psi)
 +
!scope="col" | Breakdown Pressure (psi)
 
|-
 
|-
| 2012-0
+
| 2009-02-05
| style="text-align:right;" | 1125.43
+
| style="text-align: right;" |  
| style="text-align:right;" | 366.0
+
 
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Completion Reports - Stimulations
 +
| publisher = Pennsylvania Department of Conservation and Natural Resources
 +
| date = 2020-03-02
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-03-02 }}</ref>
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Period
 +
!scope="col" | Operator Name
 +
!scope="col" | Gas Quantity (mcf)
 +
!scope="col" | Gas Production Days
 +
!scope="col" | Oil Quantity (bbl)
 +
!scope="col" | Oil Production Days
 +
!scope="col" | Water Quantity (bbl)
 +
!scope="col" | Water Production Days
 
|-
 
|-
| 2011-0
+
| 2008
| style="text-align:right;" | 2386.69
+
| [[CNX GAS CO LLC]]
| style="text-align:right;" | 365.0
+
| style="text-align: right;" | 0.00
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
| 2009
 +
| [[CNX GAS CO LLC]]
 +
| style="text-align: right;" | 4,367.00
 +
| style="text-align: right;" | 318
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2010-0
+
| 2010
| style="text-align:right;" | 2859.87
+
| [[CNX GAS CO LLC]]
| style="text-align:right;" | 365.0
+
| style="text-align: right;" | 2,859.87
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
| 2011
 +
| [[CNX GAS CO LLC]]
 +
| style="text-align: right;" | 2,386.69
 +
| style="text-align: right;" | 365
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2009-0
+
| 2012
| style="text-align:right;" | 4367.0
+
| [[CNX GAS CO LLC]]
| style="text-align:right;" | 318.0
+
| style="text-align: right;" | 1,125.43
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 366
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
| 2013
 +
| [[CNX GAS CO LLC]]
 +
| style="text-align: right;" | 2,083.13
 +
| style="text-align: right;" | 365
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2008-0
+
| 2014
| style="text-align:right;" | 0.0
+
| [[CNX GAS CO LLC]]
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 1,371.00
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
|}
+
| 2015
== Waste Data ==
+
| [[CNX GAS CO LLC]]
{| class="wikitable sortable" width="95%"
+
| style="text-align: right;" | 1,198.68
!scope="col" | PERIOD
+
| style="text-align: right;" | 365
!scope="col" | TYPE
+
| style="text-align: right;" | 0.00
!scope="col" | QUANTITY
+
| style="text-align: right;" | 0
!scope="col" | UNITS
+
| style="text-align: right;" | 0.00
!scope="col" | DISPOSAL METHOD
+
| style="text-align: right;" | 0
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
 
|-
 
|-
| 2009-0
+
| 2016
| BRINE
+
| [[CNX GAS CO LLC]]
| style="text-align:right;" | 6521.0
+
| style="text-align: right;" | 703.4
| Bbl
+
| style="text-align: right;" | 366
| BRINE OR INDUSTRIAL WASTE TREATMENT PLT
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 0
| BAILEY MINE SLURRY POND
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 0
|  
 
 
|-
 
|-
 +
| 2017
 +
| [[CNX GAS CO LLC]]
 +
| style="text-align: right;" | 497.94
 +
| style="text-align: right;" | 242
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2009-0
+
| 2018
| BRINE
+
| [[CNX GAS CO LLC]]
| style="text-align:right;" | 6521.0
+
| style="text-align: right;" | 0.00
| Bbl
+
| style="text-align: right;" | 0
| BRINE OR INDUSTRIAL WASTE TREATMENT PLT
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 0
| CARPER WELL SERVICES, BELLE VALLEY
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 0
|  
 
 
|-
 
|-
 +
| 2019
 +
| [[ALLIANCE PETRO CO LLC]]
 +
| style="text-align: right;" | 214.00
 +
| style="text-align: right;" | 214
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2009-0
+
|}
| BRINE
+
For data sources see<ref>{{cite web
| style="text-align:right;" | 6521.0
+
| title =Oil and Gas Production Reports
| Bbl
+
|publisher = [[Pennsylvania Department of Environmental Protection]]
| BRINE OR INDUSTRIAL WASTE TREATMENT PLT
+
| date = 2019-03-31
|  
+
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
| CLAIRTON
+
| accessdate = 2019-05-21 }}</ref>
|  
+
== Waste Data ==
|  
+
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Period
 +
!scope="col" | Operator
 +
!scope="col" | Waste Type
 +
!scope="col" | Quantity
 +
!scope="col" | Disposal Method
 +
!scope="col" | Waste Facility ID
 
|-
 
|-
 +
| 2009
 +
| [[CNX GAS CO LLC]]
 +
| Brine
 +
| style="text-align: right;" | 2.00 Bbl
 +
| Brine or Industrial Waste Treatment Plt
 +
| 34-167-2-9395
 
|-
 
|-
| 2009-0
+
| 2009
| BRINE
+
| [[CNX GAS CO LLC]]
| style="text-align:right;" | 6521.0
+
| Brine
| Bbl
+
| style="text-align: right;" | 474.00 Bbl
| BRINE OR INDUSTRIAL WASTE TREATMENT PLT
+
| Municipal Sewage Treatment Plant
|
+
| PA0026913
| DAVID R. HILL
 
|
 
|  
 
 
|-
 
|-
 +
| 2009
 +
| [[CNX GAS CO LLC]]
 +
| Brine
 +
| style="text-align: right;" | 1,140.00 Bbl
 +
| Brine or Industrial Waste Treatment Plt
 +
| PA0026824
 
|-
 
|-
| 2009-0
+
| 2009
| BRINE
+
| [[CNX GAS CO LLC]]
| style="text-align:right;" | 6521.0
+
| Brine
| Bbl
+
| style="text-align: right;" | 13.00 Bbl
| MUNICIPAL SEWAGE TREATMENT PLANT
+
| Brine or Industrial Waste Treatment Plt
|
+
| 30810703
| MCKEESPORT MUN WWTP
 
|
 
|  
 
 
|-
 
|-
 +
| 2009
 +
| [[CNX GAS CO LLC]]
 +
| Brine
 +
| style="text-align: right;" | 4,888.00 Bbl
 +
| Brine or Industrial Waste Treatment Plt
 +
| PAS2D210BGRE
 
|-
 
|-
| 2009-0
+
| 2009
| BRINE
+
| [[CNX GAS CO LLC]]
| style="text-align:right;" | 6521.0
+
| Brine
| Bbl
+
| style="text-align: right;" | 4.00 Bbl
| BRINE OR INDUSTRIAL WASTE TREATMENT PLT
+
| Brine or Industrial Waste Treatment Plt
|
+
| 34-121-23390
| MORRIS RUN
 
|
 
|  
 
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title =Oil and Gas Waste Reports
 +
|publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2019-03-31
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" | Inspection ID
!scope="col" | DATE
+
!scope="col" | Inspection Category
!scope="col" | DESCRIPTION
+
!scope="col" | Inspection Date
!scope="col" | COMMENT
+
!scope="col" | Inspection Type
!scope="col" | VIOLATION ID
+
!scope="col" | Inspection Result
 +
!scope="col" | Inspection Comments
 
|-
 
|-
 
| 1756017
 
| 1756017
 +
| Primary Facility
 
| 2008-12-11
 
| 2008-12-11
 +
| Complaint Inspection
 
| Violation(s) Noted
 
| Violation(s) Noted
 
| Complainants spring has been affected by silt discharge.  E/S viols also.
 
| Complainants spring has been affected by silt discharge.  E/S viols also.
| 552674
 
 
|-
 
|-
 +
| 1758371
 +
| Primary Facility
 +
| 2008-12-23
 +
| Compliance Evaluation
 +
| No Violations Noted
 +
| BMPs have been installed to divert runoff away from neighboring spring.
 +
|-
 +
|}
 +
==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Inspection ID
 +
!scope="col" | Violation ID
 +
!scope="col" | Violation Date
 +
!scope="col" | Date Resolved
 +
!scope="col" | Violation Code
 +
!scope="col" | Violation Type
 +
!scope="col" | Violation Comments
 
|-
 
|-
 
| 1756017
 
| 1756017
 +
| 552674
 +
| 12/11/2008
 
| 2008-12-11
 
| 2008-12-11
| Violation(s) Noted
+
| 102.4 - Failure to minimize accelerated erosion, implement E&S plan, maintain E&S controls. Failure to stabilize site until total site restoration under OGA Sec 206(c)(d)
| Complainants spring has been affected by silt discharge. E/S viols also.
+
| Environmental Health & Safety
| 552674
+
|  
|-
 
 
|-
 
|-
 
| 1756017
 
| 1756017
 +
| 552675
 +
| 12/11/2008
 
| 2008-12-11
 
| 2008-12-11
| Violation(s) Noted
+
| 301CSL - Stream discharge of IW, includes drill cuttings, oil, brine and/or silt
| Complainants spring has been affected by silt discharge.  E/S viols also.
+
| Environmental Health & Safety
| 552675
+
|  
 
|-
 
|-
 +
|}
 +
==== Penalties Applied ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Violation ID
 +
!scope="col" | Penalty ID
 +
!scope="col" | Penalty Code
 +
!scope="col" | Penalty Status
 +
!scope="col" | Penalty Date
 +
!scope="col" | Enforcement Date
 +
!scope="col" | Penalty Amount
 +
!scope="col" | Amount Collected
 
|-
 
|-
| 1756017
+
| 552674
| 2008-12-11
+
| 241092
| Violation(s) Noted
+
| NOV - Notice of Violation
| Complainants spring has been affected by silt discharge.  E/S viols also.
+
| Comply/Closed
| 552675
+
|
 +
| 2008-12-23
 +
| style="text-align: right;" |
 +
| style="text-align: right;" |  
 
|-
 
|-
 +
| 552674
 +
| 249374
 +
| CACP - Consent Assessment of Civil Penalty
 +
| Comply/Closed
 +
| 2009-08-24
 +
| 2009-08-24
 +
| style="text-align: right;" | $93,600.00
 +
| style="text-align: right;" | $93,600.00
 
|-
 
|-
| 1758371
+
| 552675
 +
| 241092
 +
| NOV - Notice of Violation
 +
| Comply/Closed
 +
|
 
| 2008-12-23
 
| 2008-12-23
| No Violations Noted
+
| style="text-align: right;" |
| BMPs have been installed to divert runoff away from neighboring spring.
+
| style="text-align: right;" |
|  
+
|-
 +
| 552675
 +
| 249374
 +
| CACP - Consent Assessment of Civil Penalty
 +
| Comply/Closed
 +
| 2009-08-24
 +
| 2009-08-24
 +
| style="text-align: right;" | $93,600.00
 +
| style="text-align: right;" | $93,600.00
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title =Oil and Gas Compliance Report
 +
|publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2019-05-20
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 
==References==
 
==References==
{{Reflist}}
+
<references/>
 
 
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Pennsylvania Wells]]

Latest revision as of 09:37, 15 May 2020

Well Details

Well ID: 37-125-23398
Loading map...
Country: United States
State: Pennsylvania
County: Washington
Municipality: Fallowfield Township
Operator Name: ALLIANCE PETRO CO LLC
Well Pad ID:
Farm/Lease Name: PALUSO FF84CV
License Status:
Spud Date:
Permit Date: 2008-11-10
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.149333
Longitude: -79.969303

For data sources see[1][2][3]

Well History

Date Event
2008-11-10 New Permit Application
2009-01-13 Drilling Completion
2009-01-18 Performed Spud Operation
2009-02-04 Perforation
2009-02-05 Performed Stimulation
2012-03-28 NEWLY DRILLED

For data sources see[4]

Stimulation Data

Stimulation Date Phase Number Chemical Agent Volume (gal) Treating Pressure (psi) Breakdown Pressure (psi)
2009-02-05 0 0 0

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2008 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2009 CNX GAS CO LLC 4,367.00 318 0.00 0 0.00 0
2010 CNX GAS CO LLC 2,859.87 365 0.00 0 0.00 0
2011 CNX GAS CO LLC 2,386.69 365 0.00 0 0.00 0
2012 CNX GAS CO LLC 1,125.43 366 0.00 0 0.00 0
2013 CNX GAS CO LLC 2,083.13 365 0.00 0 0.00 0
2014 CNX GAS CO LLC 1,371.00 365 0.00 0 0.00 0
2015 CNX GAS CO LLC 1,198.68 365 0.00 0 0.00 0
2016 CNX GAS CO LLC 703.4 366 0.00 0 0.00 0
2017 CNX GAS CO LLC 497.94 242 0.00 0 0.00 0
2018 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2019 ALLIANCE PETRO CO LLC 214.00 214 0.00 0 0.00 0

For data sources see[6]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2009 CNX GAS CO LLC Brine 2.00 Bbl Brine or Industrial Waste Treatment Plt 34-167-2-9395
2009 CNX GAS CO LLC Brine 474.00 Bbl Municipal Sewage Treatment Plant PA0026913
2009 CNX GAS CO LLC Brine 1,140.00 Bbl Brine or Industrial Waste Treatment Plt PA0026824
2009 CNX GAS CO LLC Brine 13.00 Bbl Brine or Industrial Waste Treatment Plt 30810703
2009 CNX GAS CO LLC Brine 4,888.00 Bbl Brine or Industrial Waste Treatment Plt PAS2D210BGRE
2009 CNX GAS CO LLC Brine 4.00 Bbl Brine or Industrial Waste Treatment Plt 34-121-23390

For data sources see[7]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1756017 Primary Facility 2008-12-11 Complaint Inspection Violation(s) Noted Complainants spring has been affected by silt discharge. E/S viols also.
1758371 Primary Facility 2008-12-23 Compliance Evaluation No Violations Noted BMPs have been installed to divert runoff away from neighboring spring.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
1756017 552674 12/11/2008 2008-12-11 102.4 - Failure to minimize accelerated erosion, implement E&S plan, maintain E&S controls. Failure to stabilize site until total site restoration under OGA Sec 206(c)(d) Environmental Health & Safety
1756017 552675 12/11/2008 2008-12-11 301CSL - Stream discharge of IW, includes drill cuttings, oil, brine and/or silt Environmental Health & Safety

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
552674 241092 NOV - Notice of Violation Comply/Closed 2008-12-23
552674 249374 CACP - Consent Assessment of Civil Penalty Comply/Closed 2009-08-24 2009-08-24 $93,600.00 $93,600.00
552675 241092 NOV - Notice of Violation Comply/Closed 2008-12-23
552675 249374 CACP - Consent Assessment of Civil Penalty Comply/Closed 2009-08-24 2009-08-24 $93,600.00 $93,600.00

For data sources see[8]

References