X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

Difference between revisions of "37-115-20212"

m
m
Line 1: Line 1:
 
__TOC__
 
__TOC__
 
== Well Details ==
 
== Well Details ==
{| class="wikitable" width="95%"
+
{| class="wikitable welldetails" width="95%"
 
| Well ID: 37-115-20212
 
| Well ID: 37-115-20212
| style="width: 50%; height=100%; align=center" rowspan="14" | {{#display_map: 41.697738, -75.840136 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="14" | {{#display_map: 41.697738, -75.840136 | width=100% | height=100% }}  
 
|-
 
|-
 
| County: [[Susquehanna County, Pennsylvania|Susquehanna]]
 
| County: [[Susquehanna County, Pennsylvania|Susquehanna]]

Revision as of 04:24, 29 June 2014

Well Details

Well ID: 37-115-20212
Loading map...
County: Susquehanna
Municipality: Lathrop Township
Operator Name: CHIEF OIL & GAS LLC
Well Pad ID: 148675
Farm/Lease Name: KERR UNIT 1H
First Permit Date: 2009-09-02
Last Permit Date: 2009-09-02
Spud Date: 2010-07-17
Unconventional: Yes
Horizontal: Yes
Producing: Yes
Violations: 2
Latitude: 41.697738
Longitude: -75.840136

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID
1897668 2010-07-09 No Violations Noted
1919700 2010-10-12 Violation(s) Noted Inspected well head. Cellar has 1' water in bottom. Observed gas coming to surface on outside of 13 3/8" casing. Well is shut in and has not been fracced yet. Operator was notified of condition on 10/8/10 after DEP inspector McShea visited the site. 597191
1919700 2010-10-12 Violation(s) Noted Inspected well head. Cellar has 1' water in bottom. Observed gas coming to surface on outside of 13 3/8" casing. Well is shut in and has not been fracced yet. Operator was notified of condition on 10/8/10 after DEP inspector McShea visited the site. 597192
1938962 2010-12-21 No Violations Noted Met John Hafer of Cummings Riter on site. PErforming 24 hr pressure test on 9 5/8" and 13 3/8" annulus's. Shut in started at 11:00.
2009105 2011-09-12 No Violations Noted

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2012-2 1148642.0 182.0 0.0 0.0 0.0 0.0
2012-1 1088630.77 182.0 0.0 0.0 0.0 0.0
2011-2 139500.0 34.0 0.0 0.0 0.0 0.0
2011-1 0.0 0.0 0.0 0.0 0.0 0.0
2010-2 0.0 0.0 0.0 0.0 0.0 0.0
2010-3 0.0 0.0 0.0 0.0 0.0 0.0
2009-0 0.0 0.0 0.0 0.0 0.0 0.0

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2012-2 PRODUCED FLUID 223.1 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING
2010-3 FRACING FLUID WASTE 101.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0027057 WILLIAMSPORT SAN AUTH - CENTRAL STP WILLIAMSPORT PA
2010-2 DRILLING FLUID WASTE 8767.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR119 EUREKA RESOURCES (WILLIAMSPORT WATER TREATMENT) WILLIAMSPORT PA
2010-2 DRILLING FLUID WASTE 1517.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0008451 SUNBURY GENERATION WASTE WATER TRMT FAC SHAMOKIN DAM PA
2012-1 PRODUCED FLUID 818.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING

References