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37-129-26288

Well Details

Well ID: 37-129-26288
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Country: United States
State: Pennsylvania
County: Westmoreland
Municipality: Derry Township
Operator Name: DIVERSIFIED OIL & GAS LLC
Well Pad ID:
Farm/Lease Name: RAMALEY 6
License Status: ACTIVE
Spud Date:
Permit Date: 2006-04-19
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.353631
Longitude: -79.393607

For data sources see[1][2][3]

Well History

Date Event
2006-04-19 New Permit Application
2006-05-23 Performed Spud Operation
2006-05-30 Drilling Completion
2006-06-12 Perforation
2006-09-14 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2006 DOUGLAS OIL & GAS LP 11347.00 210 0.00 0 0.00 0
2007 DOUGLAS OIL & GAS LP 15843.00 365 0.00 0 0.00 0
2008 REX ENERGY OPERATING CORP 13126.00 366 0.00 0 0.00 0
2009 REX ENERGY OPERATING CORP 10662.00 365 0.00 0 0.00 0
2010 REX ENERGY OPERATING CORP 7,899.00 365 0.00 0 0.00 0
2011 REX ENERGY OPERATING CORP 6,268.00 365 0.00 0 0.00 0
2012 RE GAS DEV LLC 5,068.00 366 0.00 0 0.00 0
2013 RE GAS DEV LLC 4,679.00 365 0.00 0 0.00 0
2014 RE GAS DEV LLC 4,917.00 365 0.00 0 0.00 0
2015 RE GAS DEV LLC 6,037.00 365 0.00 0 0.00 0
2016 RE GAS DEV LLC 6,386.00 298 0.00 0 0.00 0
2017 DIVERSIFIED OIL & GAS LLC 724.00 252 0.00 0 0.00 0
2018 DIVERSIFIED OIL & GAS LLC 2,375.00 365 0.00 0 0.00 0
2019 DIVERSIFIED OIL & GAS LLC 1,610.00 61 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2009 REX ENERGY OPERATING CORP Brine 75.00 Bbl Brine or Industrial Waste Treatment Plt PA0091472
2010 REX ENERGY OPERATING CORP Produced Fluid 75.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0091472

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2475244 Primary Facility 2016-04-12 Administrative/File Review No Violations Noted On 4/11/2016 @ 14:10pm, Operator (Jim Noon) called to notify Department of a spill of production fluid at the above well pad. Operator to provide additional details of quantity and cause of spill upon investigation.

UPDATE 4/12/2016 At 9:00am, Operator (Jim Noon) called to update Department on the above spill. Operator states that spill was due to a pinhead leak on the brine tank discharge valve. Operator estimates less than 2-gallons of production fluid were released. Affected area has been cleaned-up in accordance with the spill policy. Department will conduct site inspection.

2475247 Primary Facility 2016-04-12 Incident- Response to Accident or Event In Compliance with Policy Inspection performed in response to Operator’s report of a spill of production fluid caused by a leaking valve (Inspection ID 2475244). Access road gated and locked. At the time of inspection well appears equipped for production. Well tag present and affixed in a permanent manner. Brine tank located on site and appears to be structurally sound. Leaking discharge valve has been replaced and impacted area cleaned-up.

For data sources see[7]

References