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Well ID: 37-063-21793 | Loading map...
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County: Indiana | |
Municipality: Grant Township | |
Operator Name: XTO ENERGY INC | |
Well Pad ID: | |
Farm/Lease Name: LULU M STEWART FMLY A L BRAUGHLER 4 | |
First Permit Date: 1972-05-30 | |
Last Permit Date: 1972-05-30 | |
Spud Date: 1972-06-06 | |
Unconventional: No | |
Horizontal: No | |
Well Status: ACTIVE | |
Violations: 0 | |
Latitude: 40.819484 | |
Longitude: -78.978476 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1992-0 | 4299.0 | 119.0 | 0.0 | 0.0 | 0.0 | 0.0 |
1993-0 | 4359.0 | 158.0 | 0.0 | 0.0 | 0.0 | 0.0 |
1996-0 | 7308.0 | 365.0 | 0.0 | 0.0 | 0.0 | 0.0 |
1997-0 | 6635.0 | 170.0 | 0.0 | 0.0 | 0.0 | 0.0 |
1998-0 | 1760.0 | 84.0 | 0.0 | 0.0 | 0.0 | 0.0 |
1999-0 | 1972.0 | 31.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2000-0 | 3884.0 | 97.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2001-0 | 607.0 | 36.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2002-0 | 637.0 | 8.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2003-0 | 1049.0 | 9.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2004-0 | 3812.0 | 365.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2005-0 | 3589.0 | 318.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2006-0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2007-0 | 2867.0 | 365.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2008-0 | 4125.0 | 236.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2010-0 | 3589.0 | 219.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-0 | 3367.0 | 269.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2012-0 | 3101.0 | 366.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2013-0 | 2817.0 | 365.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2014-0 | 2361.0 | 365.0 | 0.0 | 0.0 | 0.0 | 0.0 |
For data sources see[1]
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|---|---|---|---|---|---|---|---|
1997-0 | BRINE | 62.0 | Bbl | BRINE OR INDUSTRIAL WASTE TREATMENT PLT | PA0095443 | CREEKSIDE TREATMENT FACILITY | CREEKSIDE | PA |
1999-0 | BRINE | 83.0 | Bbl | BRINE OR INDUSTRIAL WASTE TREATMENT PLT | PA0095443 | CREEKSIDE TREATMENT FACILITY | CREEKSIDE | PA |
2004-0 | BRINE | 64.0 | Bbl | BRINE OR INDUSTRIAL WASTE TREATMENT PLT | PA0095443 | CREEKSIDE TREATMENT FACILITY | CREEKSIDE | PA |
2005-0 | BRINE | 62.0 | Bbl | BRINE OR INDUSTRIAL WASTE TREATMENT PLT | PA0095273 | FLUID RECOVERY SERVICE JOSEPHINE FACILITY | JOSEPHINE | PA |
2008-0 | BRINE | 30.0 | Bbl | BRINE OR INDUSTRIAL WASTE TREATMENT PLT | ||||
2012-0 | PRODUCED FLUID | 27.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 | FLUID RECOVERY SERVICE JOSEPHINE FACILITY | JOSEPHINE | PA |
2013-0 | PRODUCED FLUID | 120.0 | Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 | FLUID RECOVERY SERVICE JOSEPHINE FACILITY | JOSEPHINE | PA |
2014-0 | PRODUCED FLUID | 139.0 | Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 | FLUID RECOVERY SERVICE JOSEPHINE FACILITY | JOSEPHINE | PA |
For data sources see[2]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
---|---|---|---|---|---|---|
537596 | 1989-04-10 | No Violations Noted | E&S OK; NO TANK | |||
2070225 | 2012-05-11 | In Compliance with Policy | At approximately 1305 today, May 11, 2012. Department received a call from Stephen Smith of XTO reporting an approximate 10gal brine relelase. According to prelimary reports, at 1215 Well tender found plug removed from brine tank (blieve to be vandalism) and brine actively flowing from tank. Well tender immediately replaced plug. Absorbant pads were placed on ground and a vac truck call to remove fluids. By 1300hrs well tender reported that incident had be cleaned up. Operator plans to visual removed any impacted soil and repair accordingly. As per operator this well is visited daily and the 10gal lose was based on previous days tank reading.
As per current spill policy it appears operator is compliance with policy and appropriately notified and began clean up mesures in a timely manner as outined by the said policy. A follow up site inspection will be conducted in the near future. Well drilled/completed 6/12/1972. Well listed as in production. |
For data sources see[3]