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Well ID: 37-063-21315 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Indiana | |
Municipality: Rayne Township | |
Operator Name: ALLIANCE PETROLEUM CO LLC | |
Well Pad ID: | |
Farm/Lease Name: FLOSSIE WHITACRE 4608 | |
License Status: Active | |
Spud Date: 10/30/1969 | |
Permit Date: 9/22/1969 | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Latitude: 40.727370 | |
Longitude: -79.141513 |
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1991 | DOMINION PEOPLES | 1,602.00 | 335 | 0.00 | 0.00 | ||
1996 | DOMINION PEOPLES | 1,919.00 | 365 | 0.00 | 0.00 | ||
1999 | DOMINION EXPLORATION & PROD INC | 2,882.00 | 365 | 0.00 | 0.00 | ||
2000 | DOMINION EXPLORATION & PROD INC | 2,414.00 | 365 | 0.00 | 0.00 | ||
2001 | DOMINION EXPLORATION & PROD INC | 2,380.00 | 365 | 0.00 | 0.00 | ||
2002 | DOMINION EXPLORATION & PROD INC | 2,421.00 | 365 | 0.00 | 0.00 | ||
2003 | DOMINION EXPLORATION & PROD INC | 2,245.00 | 365 | 0.00 | 0.00 | ||
2005 | DOMINION EXPLORATION & PROD INC | 2,240.00 | 365 | 0.00 | 0.00 | ||
2006 | DOMINION EXPLORATION & PROD INC | 2,200.00 | 365 | 0.00 | 0.00 | ||
2007 | DOMINION EXPLORATION & PROD INC | 2,048.00 | 365 | 0.00 | 0.00 | ||
2008 | DOMINION EXPLORATION & PROD INC | 2,013.00 | 365 | 0.00 | 0.00 | ||
2009 | DOMINION EXPLORATION & PROD INC | 1,841.00 | 365 | 0.00 | 0.00 | ||
2010 | CONSOL GAS CO | 1,556.00 | 365 | 0.00 | 0.00 | ||
2011 | 0.00 | 0.00 | 0.00 | ||||
2012 | CNX GAS CO LLC | 1,581.00 | 366 | 0.00 | 0.00 | ||
2013 | CNX GAS CO LLC | 1,491.00 | 365 | 0.00 | 0.00 | ||
2014 | CNX GAS CO LLC | 1,157.00 | 365 | 0.00 | 0.00 | ||
2015 | CNX GAS CO LLC | 1,243.00 | 365 | 0.00 | 0.00 | ||
2016 | CNX GAS CO LLC | 1,068.00 | 366 | 0.00 | 0.00 | ||
2017 | CNX GAS CO LLC | 880.00 | 365 | 0.00 | 0.00 | ||
2018 | CNX GAS CO LLC | 728.00 | 365 | 0.00 | 0.00 |
For data sources see[4]
Period | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|
2003-0 | Brine | 29.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0091472 |
2005-0 | Brine | 44.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0095273 |
2008-0 | Brine | 2.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0026034 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2293661 | Primary Facility | 07/31/2014 | Administrative/File Review | In Compliance with Policy | SPILL. |
2293678 | Primary Facility | 07/31/2014 | Administrative/File Review | In Compliance with Policy | Admin inspt as follow-up to record 2293661 for the reported release of 25 gal brine water.Upon receipt of spill report, Dept contacted Opr rep Ryan Scrips via phone.Mr. Scrips stated the release resulted from a small crack in the lip of the brine tank. The impacted area is approximately 23' by 4'. No waterways reported to be affected.Mr. Scrips discovered the release on 7/31 at 0945 and reported it to the SWRO at 1125.The BT has been removed and one roll-off box and excavator are currently on-site to remove all visibly impacted soils.Sampling will be conducted to ensure all contaminants have been adequately removed.Excavated soils will then be replaced and then the site will be seeded/mulched.Dept requested e-mail documenting events surrounding release.It appears Opr is handling the situation according to policy and a follow-up inspection will be conducted to assess any environmental impacts and/or issued any associated viols as necessary. |
For data sources see[6]