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Well ID: 37-051-24328 | Loading map...
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County: Fayette | |
Municipality: Dunbar Township | |
Operator Name: XTO ENERGY INC | |
Well Pad ID: 148509 | |
Farm/Lease Name: HELEN K BUKOVAC 4H | |
First Permit Date: 2010-03-12 | |
Last Permit Date: 2010-03-12 | |
Spud Date: 2010-05-26 | |
Unconventional: Yes | |
Horizontal: Yes | |
Well Status: ACTIVE | |
Violations: 1 | |
Latitude: 40.010133 | |
Longitude: -79.672622 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2010-3 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2010-2 | 143357.0 | 52.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2010-2 | 143357.0 | 52.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-1 | 475503.0 | 181.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-2 | 296529.0 | 184.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2012-1 | 231036.0 | 182.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2012-2 | 196772.0 | 184.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2013-1 | 168164.0 | 181.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2013-2 | 154823.0 | 184.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2014-1 | 75532.0 | 179.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2014-2 | 146944.0 | 184.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2015-02 | 10051.0 | 15.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2015-01 | 16332.0 | 19.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2015-03 | 21460.0 | 23.0 | 0.0 | 0.0 | 0.0 | 0.0 |
For data sources see[1]
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|---|---|---|---|---|---|---|---|
2010-2 | PRODUCED FLUID | 1.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PAR000519462 | ADVANCED WASTE SERVICES OF PA LLC | NEW CASTLE | PA |
2011-1 | PRODUCED FLUID | 2.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PAR000519462 | ADVANCED WASTE SERVICES OF PA LLC | NEW CASTLE | PA |
2011-1 | PRODUCED FLUID | 80.0 | Bbl | INJECTION DISPOSAL WELL | 34-059-24067 | DEVCO UNIT #1 (SWIW #11) | CAMBRIDGE | OH |
2011-1 | PRODUCED FLUID | 219.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PBR | RESERVED ENVIRONMENTAL SERVICES, LLC | PITTSBURGH | PA |
2011-2 | PRODUCED FLUID | 200.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PAR000519462 | ADVANCED WASTE SERVICES OF PA LLC | NEW CASTLE | PA |
2011-2 | PRODUCED FLUID | 810.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0254185 | RESERVED ENV SVC WASTE WATER TREATMENT FACILITY | MOUNT PLEASANT | PA |
2011-2 | PRODUCED FLUID | 45.0 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE OF BRINE TO FRAC A WELL | |||
2012-1 | PRODUCED FLUID | 92.0 | Bbl | INJECTION DISPOSAL WELL | 34-133-24189 | MEYERS #2 (SWIW #33) | ATWATER | OH |
2012-1 | PRODUCED FLUID | 442.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0254185 | RESERVED ENV SVC WASTE WATER TREATMENT FACILITY | MOUNT PLEASANT | PA |
2012-2 | PRODUCED FLUID | 852.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0254185 | RESERVED ENV SVC WASTE WATER TREATMENT FACILITY | MOUNT PLEASANT | PA |
2012-2 | PRODUCED FLUID | 92.0 | Bbl | INJECTION DISPOSAL WELL | 34-133-21076 | SALTYS DISPOSAL - MYERS INECTION WELL #1 | PARIS | OH |
2013-1 | PRODUCED FLUID | 398.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0254185 | RESERVED ENV SVC WASTE WATER TREATMENT FACILITY | MOUNT PLEASANT | PA |
2013-2 | PRODUCED FLUID | 294.0 | Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0254185 | RESERVED ENV SVC WASTE WATER TREATMENT FACILITY | MOUNT PLEASANT | PA |
2014-1 | PRODUCED FLUID | 110.0 | Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NW009 | RES WATER BUTLER | PA | |
2014-1 | PRODUCED FLUID | 663.0 | Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0254185 | RESERVED ENV SVC WASTE WATER TREATMENT FACILITY | MOUNT PLEASANT | PA |
2014-2 | PRODUCED FLUID | 100.0 | Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NW009 | RES WATER BUTLER | PA | |
2014-2 | PRODUCED FLUID | 177.0 | Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123SW005 | RESERVED ENV SVC HEMPFIELD TWP RESIDUAL WASTE OPER | PA |
For data sources see[2]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
---|---|---|---|---|---|---|
1889802 | 2010-06-03 | No Violations Noted | ||||
1893303 | 2010-06-16 | No Violations Noted | ||||
1910105 | 2010-08-20 | No Violations Noted | HORIZONTAL MARCELLUS, SAXON RIG -124 LANDING CURVE, TD ESTIMATED AT 11350', PITS AND E&S ARE GOOD. | |||
2131364 | 2013-01-15 | No Violations Noted | Notice of termination inspection. All areas reclaimed and had at least 70% growth. Well labeled, tanks in containment, ID sign up.Site stable. | |||
2239093 | 2014-01-13 | Violation(s) Noted | On Monday, January 13, 2014, the Department received a report about a spill that had occurred the previous day on XTOï¾’s Helen Bukovac #4H site; I investigated on January 14, 2014.
The site was a Marcellus well, some production equipment and two 210 bbl production tanks floating together for a total capacity of 420 bbl (17,640 gallon); these tanks contained primarily weak brine. Sometime during the night of January 11th and 12th the brine froze a valve causing #1 tank (the north tank) to fail. The produce water went to containment, but, since the containment was earthen it seeped through to the outside. XTO discovered the problem during the morning of the 12th, called the Department and initiated a response. They closed in the wells, called in a vacuum truck that recovered 29 bbl of material and contracted an excavating company. They were planning on excavating until tests indicated soil to background. XTO also has plans to permanently remove the damaged tank.
|
687336 | 91.34A - Failure to take all necessary measures to prevent spill. Inadequate diking, potential pollution | |
2242810 | 2014-01-23 | Outstanding Violations - No Viols Req'd | On 1/24/2014, the Department conducted a follow -up inspection at the XTO Energy Incï¾’s Helen Bukovac 4H OG WELL in Dunbar Twp., Fayette County.
The purpose of the inspection was a follow - up to the spill that occurred on January 12, 2014. There are 42 dumpsters full of material removed as the result of the spill. 10 dumpsters were at the well site and 32 were located up on a hill along the access road to the well. The material removed so far was from inside the dike. The tanks that leaked have been removed from the dike. |
For data sources see[3]