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34-169-22054

Well Details

Well ID: 34-169-22054
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County: Wayne
Municipality:
Operator Name: BERNHARDT JAMES R INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1978-07-25
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 40.8971159
Longitude: -81.74745939

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 5389.0 0.0
1985-0 4537.0 70.0
1986-0 3732.0 0.0
1987-0 1074.0 0.0
1988-0 0.0 0.0
1989-0 0.0 0.0
1990-0 0.0 0.0
1991-0 0.0 0.0
1992-0 0.0 0.0
1993-0 0.0 0.0
1994-0 0.0 0.0
1995-0 0.0 0.0
1996-0 0.0 0.0
1997-0 0.0 0.0
1999-0 0.0 0.0
2000-0 0.0 0.0
2001-0 0.0 0.0
2002-0 0.0 0.0
2003-0 0.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1070307762 2003-11-21 Check on rig status for plugging of well with bad casing and tubing. Today they are fishing for chunks of shreded casing and tubing. Still pulling junk out at 124 ft.
1071586956 2003-12-02 Check on rig status to see if they are ready to plug well and found that they have caught fish and are going back in with 1 1/2 tubing. Should be ready to plug soon.
-1236019352 2003-12-11 Check on rig to see if they are ready to plug since catching the fish. John wants to plug from 2100ft. With shot holes and not pulling the 2 7/8 . I called Rick and spoke with him about casing string and the need for multiples of shots needed to finish plug. Rick agreed that there should be several shots to insure that the cement has a place to seek hydrostatic equilibrium
1423392870 2003-12-17 Set plug at the deepest point that could be accessed which is 2110 ft. The 4 1/2 casing which remains in well has been shot with 10 shots and the Clinton formaiton does not have a plug . The plug was then pumped thru 1 1/2 tubing . Next pulled up to 710 ft. and shot again with 10 shots and set plug to surface.Let plug set over night and plan to tag plug and grout to surface.
-1788874677 2003-11-28 Rig still fishing for casing and junk left in the hole because casing had deteriorated into pudding. They are pulling chunks out about the size of a coffee can. Should be ready to pull good casing soon.
2066517510 2003-11-06 Still fishing for tools in hole at 124ft/.
54208147 2004-09-02 Meets requirements for restoration final.
-702249199 2003-12-24 My inspection showed that the cement at the top of this well had settled and additional cement is needed to fill to surface.
-908656274 2003-11-04 Check on progress of well plugging . The operator has service rig over the hole fishing for tubing. They are at 124ft.
-996622150 2003-12-15 Try and set plug at 2300 ft. and could not get shot line down hole. Pick up tools and go back in and try and clear pipe / could not and went out to plug front well on this lease while Glen Davis works on well.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.