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34-133-22378

Well Details

Well ID: 34-133-22378
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1980-11-08
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 41.1218434718
Longitude: -81.0933036919

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-315880063 2014-02-20 I conducted a status check inspection of this tank battery. My inspection found the tank battery was fenced, diked, and contained 1-210 barrel stock tank, a 50 barrel poly tank, and a horizontal separator. There was a domestic hook up with 11psi on the gauge inside the battery. The ID was posted on the tank and indicated that the Reagan #1 (#22377) produced to this tank battery as well. A bull plug on the bottom of the separator had a minor leak and there were several absorbent pads on the ground to catch the drip. Valves on both sides of the production unit were closed and nothing was being produced at this time. I will talk to Enervest about repairing or replacing the separator in this tank battery. No violations.