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34-133-21961

Well Details

Well ID: 34-133-21961
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County: Portage
Municipality:
Operator Name: PETROX, INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1989-06-12
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 41.21677621
Longitude: -81.21905939

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 3135.0 300.0
1985-0 2501.0 239.0
1986-0 304.0 0.0
1987-0 2614.0 330.0
1988-0 3686.0 147.0
1989-0 9638.0 238.0
1991-0 3744.0 569.0
1992-0 8137.0 149.0
1993-0 585.0 306.0
1994-0 450.0 369.0
1995-0 354.0 398.0
1996-0 326.0 345.0
1997-0 304.0 210.0
1998-0 358.0 281.0
2000-0 293.0 149.0
2001-0 481.0 266.0
2002-0 320.0 130.0
2003-0 0.0 242.0
2004-0 162.0 63.0
2005-0 492.0 121.0
2006-0 571.0 89.0
2007-0 517.0 218.0
2008-0 729.0 172.0
2009-0 529.0 126.0
2010-0 377.0 138.0
2011-0 597.0 52.0
2012-0 620.0 120.0
2013-0 443.0 145.0
2014-0 384.0 365.0 62.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1293578670 2002-06-18 FOLLOW UP TO NOV # 2154i213 6-15-02 Received a report of a flowline leak from Mike Loper, Cell # 330-495-3939, Home # 330-866-5292. Approx. 4 bbls. of crude oil were released. D&M Contracting was on their way to contain and clean up the release. 6-16-02 Received an update from Mi
2047762563 2003-03-27 Status check inspection - this pump jack well has no identification at the wellhead. The last reported production was 2001.
2154i213 2002-06-18 6-15-02 Received a report of a flowline leak from Mike Loper, Cell # 330-495-3939, Home # 330-866-5292. Approx. 4 bbls. of crude oil were released. D&M Contracting was on their way to contain and clean up the release. 6-16-02 Received an update from Mike Loper that the release was contained and the clean up was in progress. 6-18-02 Met with Dave Miller (D&M) and inspected the site. The site is 90% cleaned up, a new flowline will be installed, and contaminated soils will be taken to Countywide Landfill. An N.O.V. was issued.
2154i262 2002-07-02 Flowline leak has been repaired and site has been seeded. Booms and pads are still in place.
23578869 2005-03-07 Status check inspection - no violations at this time.
28878992 2002-07-17 Inspected site. VIOLATION RESOLVED. No further action.
PL6390 Preliminary Restoration done information from Data Point

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.