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Difference between revisions of "34-133-21961"

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Line 3: Line 3:
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-133-21961
 
| Well ID: 34-133-21961
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.2167762118, -81.2190593944 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.21677621, -81.21905939 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Portage County, Ohio|Portage]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[PETROX, INC]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 1989-06-12
 
| Spud Date: 1989-06-12
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Producing
 
|-
 
|-
| Violations: 4
+
| Violations: 0
 
|-
 
|-
| Latitude: 41.2167762118
+
| Latitude: 41.21677621
 
|-
 
|-
| Longitude: -81.2190593944
+
| Longitude: -81.21905939
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 1984-0
 +
| style="text-align:right;" | 3135.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 300.0
 +
|
 +
|-
 +
|-
 +
| 1985-0
 +
| style="text-align:right;" | 2501.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 239.0
 +
|
 +
|-
 +
|-
 +
| 1986-0
 +
| style="text-align:right;" | 304.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1987-0
 +
| style="text-align:right;" | 2614.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 330.0
 +
|
 +
|-
 +
|-
 +
| 1988-0
 +
| style="text-align:right;" | 3686.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 147.0
 +
|
 +
|-
 +
|-
 +
| 1989-0
 +
| style="text-align:right;" | 9638.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 238.0
 +
|
 +
|-
 +
|-
 +
| 1991-0
 +
| style="text-align:right;" | 3744.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 569.0
 +
|
 +
|-
 +
|-
 +
| 1992-0
 +
| style="text-align:right;" | 8137.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 149.0
 +
|
 +
|-
 +
|-
 +
| 1993-0
 +
| style="text-align:right;" | 585.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 306.0
 +
|
 +
|-
 +
|-
 +
| 1994-0
 +
| style="text-align:right;" | 450.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 369.0
 +
|
 +
|-
 +
|-
 +
| 1995-0
 +
| style="text-align:right;" | 354.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 398.0
 +
|
 +
|-
 +
|-
 +
| 1996-0
 +
| style="text-align:right;" | 326.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 345.0
 +
|
 +
|-
 +
|-
 +
| 1997-0
 +
| style="text-align:right;" | 304.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 210.0
 +
|
 +
|-
 +
|-
 +
| 1998-0
 +
| style="text-align:right;" | 358.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 281.0
 +
|
 +
|-
 +
|-
 +
| 2000-0
 +
| style="text-align:right;" | 293.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 149.0
 +
|
 +
|-
 +
|-
 +
| 2001-0
 +
| style="text-align:right;" | 481.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 266.0
 +
|
 +
|-
 +
|-
 +
| 2002-0
 +
| style="text-align:right;" | 320.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 130.0
 +
|
 +
|-
 +
|-
 +
| 2003-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 242.0
 +
|
 +
|-
 +
|-
 +
| 2004-0
 +
| style="text-align:right;" | 162.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 63.0
 +
|
 +
|-
 +
|-
 +
| 2005-0
 +
| style="text-align:right;" | 492.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 121.0
 +
|
 +
|-
 +
|-
 +
| 2006-0
 +
| style="text-align:right;" | 571.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 89.0
 +
|
 +
|-
 +
|-
 +
| 2007-0
 +
| style="text-align:right;" | 517.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 218.0
 +
|
 +
|-
 +
|-
 +
| 2008-0
 +
| style="text-align:right;" | 729.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 172.0
 +
|
 +
|-
 +
|-
 +
| 2009-0
 +
| style="text-align:right;" | 529.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 126.0
 +
|
 +
|-
 +
|-
 +
| 2010-0
 +
| style="text-align:right;" | 377.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 138.0
 +
|
 +
|-
 +
|-
 +
| 2011-0
 +
| style="text-align:right;" | 597.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 52.0
 +
|
 +
|-
 +
|-
 +
| 2012-0
 +
| style="text-align:right;" | 620.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 120.0
 +
|
 +
|-
 +
|-
 +
| 2013-0
 +
| style="text-align:right;" | 443.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 145.0
 +
|
 +
|-
 +
|-
 +
| 2014-0
 +
| style="text-align:right;" | 384.0
 +
| style="text-align:right;" | 365.0
 +
|
 +
|
 +
| style="text-align:right;" | 62.0
 +
| style="text-align:right;" | 365.0
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 319:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
|-
 
| 1293578670
 
| 2002-06-18
 
|
 
| FOLLOW UP TO NOV #  2154i213  6-15-02  Received a report of a flowline leak from Mike Loper, Cell # 330-495-3939, Home # 330-866-5292. Approx. 4 bbls. of crude oil were released. D&M Contracting was on their way to contain and clean up the release. 6-16-02  Received an update from Mi
 
|
 
| 9-1-07
 
|
 
|-
 
 
|-
 
|-
 
| 1293578670
 
| 1293578670
 
| 2002-06-18
 
| 2002-06-18
|
+
|  
 
| FOLLOW UP TO NOV #  2154i213  6-15-02  Received a report of a flowline leak from Mike Loper, Cell # 330-495-3939, Home # 330-866-5292. Approx. 4 bbls. of crude oil were released. D&M Contracting was on their way to contain and clean up the release. 6-16-02  Received an update from Mi
 
| FOLLOW UP TO NOV #  2154i213  6-15-02  Received a report of a flowline leak from Mike Loper, Cell # 330-495-3939, Home # 330-866-5292. Approx. 4 bbls. of crude oil were released. D&M Contracting was on their way to contain and clean up the release. 6-16-02  Received an update from Mi
|
+
|  
| 9-9-05(A)10
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 2047762563
 
| 2047762563
 
| 2003-03-27
 
| 2003-03-27
|
+
|  
 
| Status check inspection - this pump jack well has no identification at the wellhead. The last reported production was 2001.
 
| Status check inspection - this pump jack well has no identification at the wellhead. The last reported production was 2001.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 2154i213
 
| 2154i213
 
| 2002-06-18
 
| 2002-06-18
|
+
|  
 
| 6-15-02  Received a report of a flowline leak from Mike Loper, Cell # 330-495-3939, Home # 330-866-5292. Approx. 4 bbls. of crude oil were released. D&M Contracting was on their way to contain and clean up the release. 6-16-02  Received an update from Mike Loper that the release was contained and the clean up was in progress. 6-18-02  Met with Dave Miller (D&M) and inspected the site. The site is 90% cleaned up, a new flowline will be installed, and contaminated soils will be taken to Countywide Landfill. An N.O.V. was issued.
 
| 6-15-02  Received a report of a flowline leak from Mike Loper, Cell # 330-495-3939, Home # 330-866-5292. Approx. 4 bbls. of crude oil were released. D&M Contracting was on their way to contain and clean up the release. 6-16-02  Received an update from Mike Loper that the release was contained and the clean up was in progress. 6-18-02  Met with Dave Miller (D&M) and inspected the site. The site is 90% cleaned up, a new flowline will be installed, and contaminated soils will be taken to Countywide Landfill. An N.O.V. was issued.
|
+
|  
| 9-1-07
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 2154i262
 
| 2154i262
 
| 2002-07-02
 
| 2002-07-02
|
+
|  
 
| Flowline leak has been repaired and site has been seeded. Booms and pads are still in place.
 
| Flowline leak has been repaired and site has been seeded. Booms and pads are still in place.
|
+
|  
| 9-1-07
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 23578869
 
| 23578869
 
| 2005-03-07
 
| 2005-03-07
|
+
|  
 
| Status check inspection - no violations at this time.
 
| Status check inspection - no violations at this time.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 28878992
 
| 28878992
 
| 2002-07-17
 
| 2002-07-17
|
+
|  
 
| Inspected site. VIOLATION RESOLVED. No further action.
 
| Inspected site. VIOLATION RESOLVED. No further action.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| PL6390
 
| PL6390
|
+
|  
|
+
|  
 
| Preliminary Restoration  done information from Data Point
 
| Preliminary Restoration  done information from Data Point
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 19:48, 15 July 2015

Well Details

Well ID: 34-133-21961
Loading map...
County: Portage
Municipality:
Operator Name: PETROX, INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1989-06-12
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 41.21677621
Longitude: -81.21905939

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 3135.0 300.0
1985-0 2501.0 239.0
1986-0 304.0 0.0
1987-0 2614.0 330.0
1988-0 3686.0 147.0
1989-0 9638.0 238.0
1991-0 3744.0 569.0
1992-0 8137.0 149.0
1993-0 585.0 306.0
1994-0 450.0 369.0
1995-0 354.0 398.0
1996-0 326.0 345.0
1997-0 304.0 210.0
1998-0 358.0 281.0
2000-0 293.0 149.0
2001-0 481.0 266.0
2002-0 320.0 130.0
2003-0 0.0 242.0
2004-0 162.0 63.0
2005-0 492.0 121.0
2006-0 571.0 89.0
2007-0 517.0 218.0
2008-0 729.0 172.0
2009-0 529.0 126.0
2010-0 377.0 138.0
2011-0 597.0 52.0
2012-0 620.0 120.0
2013-0 443.0 145.0
2014-0 384.0 365.0 62.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1293578670 2002-06-18 FOLLOW UP TO NOV # 2154i213 6-15-02 Received a report of a flowline leak from Mike Loper, Cell # 330-495-3939, Home # 330-866-5292. Approx. 4 bbls. of crude oil were released. D&M Contracting was on their way to contain and clean up the release. 6-16-02 Received an update from Mi
2047762563 2003-03-27 Status check inspection - this pump jack well has no identification at the wellhead. The last reported production was 2001.
2154i213 2002-06-18 6-15-02 Received a report of a flowline leak from Mike Loper, Cell # 330-495-3939, Home # 330-866-5292. Approx. 4 bbls. of crude oil were released. D&M Contracting was on their way to contain and clean up the release. 6-16-02 Received an update from Mike Loper that the release was contained and the clean up was in progress. 6-18-02 Met with Dave Miller (D&M) and inspected the site. The site is 90% cleaned up, a new flowline will be installed, and contaminated soils will be taken to Countywide Landfill. An N.O.V. was issued.
2154i262 2002-07-02 Flowline leak has been repaired and site has been seeded. Booms and pads are still in place.
23578869 2005-03-07 Status check inspection - no violations at this time.
28878992 2002-07-17 Inspected site. VIOLATION RESOLVED. No further action.
PL6390 Preliminary Restoration done information from Data Point

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.