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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-119-28095 | | Well ID: 34-119-28095 | ||
− | | style="height=100%; align=center" rowspan="15" | {{#display_map: 40. | + | | style="height=100%; align=center" rowspan="15" | {{#display_map: 40.11437083, -81.98714242 | width=100% | height=100% }} |
|- | |- | ||
− | | County: | + | | County: [[Muskingum County, Ohio|Muskingum]] |
|- | |- | ||
− | | Municipality: | + | | Municipality: |
|- | |- | ||
− | | Operator Name: | + | | Operator Name: [[ENERVEST OPERATING L]] |
|- | |- | ||
− | | Well Pad ID: | + | | Well Pad ID: |
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: |
|- | |- | ||
− | | First Permit Date: | + | | First Permit Date: |
|- | |- | ||
− | | Last Permit Date: | + | | Last Permit Date: |
|- | |- | ||
| Spud Date: 1997-06-10 | | Spud Date: 1997-06-10 | ||
|- | |- | ||
− | | Unconventional: | + | | Unconventional: No |
|- | |- | ||
− | | | + | | Configuration: Vertical |
|- | |- | ||
− | | | + | | Well Status: Final Restoration |
|- | |- | ||
− | | Violations: | + | | Violations: 0 |
|- | |- | ||
− | | Latitude: 40. | + | | Latitude: 40.11437083 |
|- | |- | ||
− | | Longitude: -81. | + | | Longitude: -81.98714242 |
|- | |- | ||
|} | |} | ||
Line 43: | Line 43: | ||
!scope="col" | OIL QUANTITY | !scope="col" | OIL QUANTITY | ||
!scope="col" | OIL PRODUCTION DAYS | !scope="col" | OIL PRODUCTION DAYS | ||
+ | |- | ||
+ | | 1997-0 | ||
+ | | style="text-align:right;" | 1282.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1998-0 | ||
+ | | style="text-align:right;" | 10627.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 3290.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1999-0 | ||
+ | | style="text-align:right;" | 14155.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 1977.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2000-0 | ||
+ | | style="text-align:right;" | 23508.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 1512.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2001-0 | ||
+ | | style="text-align:right;" | 27698.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 911.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2002-0 | ||
+ | | style="text-align:right;" | 12369.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 394.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2003-0 | ||
+ | | style="text-align:right;" | 14919.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 348.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2004-0 | ||
+ | | style="text-align:right;" | 9865.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 295.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2005-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 22.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2006-0 | ||
+ | | style="text-align:right;" | 1363.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2007-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2008-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2009-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2010-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 3.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2011-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2012-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2013-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2014-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | |- | ||
|} | |} | ||
− | + | For data sources see<ref>{{cite web | |
− | + | | title = Ohio Department of Natural Resources RBDMS | |
− | + | | publisher = [http://oilandgas.ohiodnr.gov/] | |
− | + | | date = 2015-06-19 | |
− | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production | |
− | + | | accessdate = 2015-06-20 }}</ref> | |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
== Inspection Data == | == Inspection Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 64: | Line 220: | ||
!scope="col" | VIOLATION ID | !scope="col" | VIOLATION ID | ||
!scope="col" | VIOLATION CODE | !scope="col" | VIOLATION CODE | ||
− | !scope="col" | | + | !scope="col" | VIOLATION COMMENT |
|- | |- | ||
− | | | + | | 1110816583 |
− | | | + | | 2005-03-14 |
− | | | + | | |
− | | | + | | Not selling gas at present time |
− | | | + | | |
− | | | + | | |
− | | | + | | Field Visit or Inspection |
|- | |- | ||
|- | |- | ||
− | | | + | | 1110816583 |
− | | | + | | 2005-03-14 |
− | | | + | | |
− | | | + | | Not selling gas at present time |
− | | | + | | |
− | | | + | | |
− | | | + | | Compliance Notice |
|- | |- | ||
|- | |- | ||
− | | | + | | 1110816583 |
− | | | + | | 2005-03-14 |
− | | | + | | |
− | | | + | | Not selling gas at present time |
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
− | | | + | | 1110816583 |
− | | | + | | 2005-03-14 |
− | | | + | | |
− | | | + | | Not selling gas at present time |
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 1110816583 | | 1110816583 | ||
| 2005-03-14 | | 2005-03-14 | ||
− | | | + | | |
| Not selling gas at present time | | Not selling gas at present time | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | -1116706422 | ||
+ | | 2012-11-01 | ||
+ | | | ||
+ | | Well is still idle with no tubing present in well. There are two flanges that are bolted together with 2 bolts. The flow line has been un hooked and is laying on site. I called Tim McConahae and he will check on this well. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| 1177157089 | | 1177157089 | ||
| 2003-04-08 | | 2003-04-08 | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
− | | | + | | |
− | + | | | |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | | | ||
|- | |- | ||
|- | |- | ||
| 1357245521 | | 1357245521 | ||
| 2013-01-03 | | 2013-01-03 | ||
− | | | + | | |
| Idle well with two flanges bolted together. The flow line is disconnected from the well head. There are 2-100barrel tanks and no production has been reported since 2010 of only 3 barrels of oil. There is a large gap of time from 2006-2010 that there was n | | Idle well with two flanges bolted together. The flow line is disconnected from the well head. There are 2-100barrel tanks and no production has been reported since 2010 of only 3 barrels of oil. There is a large gap of time from 2006-2010 that there was n | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 1406027748 | | 1406027748 | ||
| 2014-07-22 | | 2014-07-22 | ||
− | | | + | | |
| Chipco is plugging for Enervest and is spotting bottom plug thru 1.5''tubing. The tubing depth is at 5800-5400'. Chipco is running 50 sacks of regular class A cement in 5.5 ''casing. Good circulation. | | Chipco is plugging for Enervest and is spotting bottom plug thru 1.5''tubing. The tubing depth is at 5800-5400'. Chipco is running 50 sacks of regular class A cement in 5.5 ''casing. Good circulation. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 1406293247 | | 1406293247 | ||
| 2014-07-24 | | 2014-07-24 | ||
− | | | + | | |
| Chipco had ripped 5.5''casing off and ran 1.5'' tubing in to 4368'. The pump truck could not pump on the tubing because the tubing was plugged off. They would pull the tubing out and round trip back in. | | Chipco had ripped 5.5''casing off and ran 1.5'' tubing in to 4368'. The pump truck could not pump on the tubing because the tubing was plugged off. They would pull the tubing out and round trip back in. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | 1418228073 | ||
+ | | 2014-12-09 | ||
+ | | | ||
+ | | Final restoration passed on 12-9-14 by Patrick Shreve. Vegetation has been established to prevent erosion. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| 1469193576 | | 1469193576 | ||
| 2010-01-05 | | 2010-01-05 | ||
− | | | + | | |
| Well is shut in and has been for some time. | | Well is shut in and has been for some time. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 1617206024 | | 1617206024 | ||
| 2007-11-05 | | 2007-11-05 | ||
− | | | + | | |
| Well is shut in. Well is on plug list recently sent to WVA. (per Jeff Murrey) | | Well is shut in. Well is on plug list recently sent to WVA. (per Jeff Murrey) | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | -1809256060 | ||
+ | | 2014-07-25 | ||
+ | | | ||
+ | | Chipco has ran 1.5''tubing in to depth of 3952-3536 and set the clinton/ Rip plug of 120 sacks of regular class A cement. The lime plug was set at 2657-2457'. They ran 60 sacks of regular Class A cement. The Bottom of the surface plug was at 1170-970'. They ran 60 sacks of regular class A cement . The surface plug was at 200-0. They ran 60 sacks of regular class A cement. All plugs circulated. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2132821366 | ||
+ | | 2014-07-25 | ||
+ | | | ||
+ | | Well has been plugged in compliance with OAC 1501:9-11. This has resolved the Compliance Notices # 985074867,1357245521 and -1116706422. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| 262691999 | | 262691999 | ||
| 2013-04-10 | | 2013-04-10 | ||
− | | | + | | |
| Per Request of Enervest on the status of the well. Well is not in compliance with 1509. Waiting on Enervest to Plug well. Plug permit in hand. | | Per Request of Enervest on the status of the well. Well is not in compliance with 1509. Waiting on Enervest to Plug well. Plug permit in hand. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 485255462 | | 485255462 | ||
| 2004-02-18 | | 2004-02-18 | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 536526114 | | 536526114 | ||
| 2014-07-24 | | 2014-07-24 | ||
− | | | + | | |
| I stopped back at site to find out what had plugged the tubing off. It was a red sand and a gray shale. Could be the Red Medina and the Queenston. Chipco is running 1.5''tubing in and circulating on every 30 joints. | | I stopped back at site to find out what had plugged the tubing off. It was a red sand and a gray shale. Could be the Red Medina and the Queenston. Chipco is running 1.5''tubing in and circulating on every 30 joints. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | -844873200 | ||
+ | | 2010-09-09 | ||
+ | | | ||
+ | | FOLLOW UP TO NOV # 985074867 Pulled tubing to use to plug another well. This well is not producing. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | -917044231 | ||
+ | | 2014-07-23 | ||
+ | | | ||
+ | | On the date of inspection I accompanied ODNR Inspector Patrick Shreve to check the status of the well plugging. The production casing had been ripped and the service rig was pulling casing at the time of my inspection. Refer to Patrick Shreve's report for further details. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| 985074867 | | 985074867 | ||
| 2010-09-09 | | 2010-09-09 | ||
− | | | + | | |
| Pulled tubing to use to plug another well. This well is not producing. | | Pulled tubing to use to plug another well. This well is not producing. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Ohio Department of Natural Resources RBDMS | ||
+ | | publisher = [http://oilandgas.ohiodnr.gov/] | ||
+ | | date = 2015-06-19 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection | ||
+ | | accessdate = 2015-06-20 }}</ref> | ||
+ | == References == | ||
+ | {{reflist}} | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Wells]] | [[Category:Wells]] |
Well ID: 34-119-28095 | Loading map...
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County: Muskingum | |
Municipality: | |
Operator Name: ENERVEST OPERATING L | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1997-06-10 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Final Restoration | |
Violations: 0 | |
Latitude: 40.11437083 | |
Longitude: -81.98714242 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1997-0 | 1282.0 | 0.0 | ||||
1998-0 | 10627.0 | 3290.0 | ||||
1999-0 | 14155.0 | 1977.0 | ||||
2000-0 | 23508.0 | 1512.0 | ||||
2001-0 | 27698.0 | 911.0 | ||||
2002-0 | 12369.0 | 394.0 | ||||
2003-0 | 14919.0 | 348.0 | ||||
2004-0 | 9865.0 | 295.0 | ||||
2005-0 | 0.0 | 22.0 | ||||
2006-0 | 1363.0 | 0.0 | ||||
2007-0 | 0.0 | 0.0 | ||||
2008-0 | 0.0 | 0.0 | ||||
2009-0 | 0.0 | 0.0 | ||||
2010-0 | 0.0 | 3.0 | ||||
2011-0 | 0.0 | 0.0 | ||||
2012-0 | 0.0 | 0.0 | ||||
2013-0 | 0.0 | 0.0 | ||||
2014-0 | 0.0 | 0.0 | 0.0 | 0.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1110816583 | 2005-03-14 | Not selling gas at present time | Field Visit or Inspection | |||
1110816583 | 2005-03-14 | Not selling gas at present time | Compliance Notice | |||
1110816583 | 2005-03-14 | Not selling gas at present time | ||||
1110816583 | 2005-03-14 | Not selling gas at present time | ||||
1110816583 | 2005-03-14 | Not selling gas at present time | ||||
-1116706422 | 2012-11-01 | Well is still idle with no tubing present in well. There are two flanges that are bolted together with 2 bolts. The flow line has been un hooked and is laying on site. I called Tim McConahae and he will check on this well. | ||||
1177157089 | 2003-04-08 | |||||
1357245521 | 2013-01-03 | Idle well with two flanges bolted together. The flow line is disconnected from the well head. There are 2-100barrel tanks and no production has been reported since 2010 of only 3 barrels of oil. There is a large gap of time from 2006-2010 that there was n | ||||
1406027748 | 2014-07-22 | Chipco is plugging for Enervest and is spotting bottom plug thru 1.5tubing. The tubing depth is at 5800-5400'. Chipco is running 50 sacks of regular class A cement in 5.5 casing. Good circulation. | ||||
1406293247 | 2014-07-24 | Chipco had ripped 5.5casing off and ran 1.5 tubing in to 4368'. The pump truck could not pump on the tubing because the tubing was plugged off. They would pull the tubing out and round trip back in. | ||||
1418228073 | 2014-12-09 | Final restoration passed on 12-9-14 by Patrick Shreve. Vegetation has been established to prevent erosion. | ||||
1469193576 | 2010-01-05 | Well is shut in and has been for some time. | ||||
1617206024 | 2007-11-05 | Well is shut in. Well is on plug list recently sent to WVA. (per Jeff Murrey) | ||||
-1809256060 | 2014-07-25 | Chipco has ran 1.5tubing in to depth of 3952-3536 and set the clinton/ Rip plug of 120 sacks of regular class A cement. The lime plug was set at 2657-2457'. They ran 60 sacks of regular Class A cement. The Bottom of the surface plug was at 1170-970'. They ran 60 sacks of regular class A cement . The surface plug was at 200-0. They ran 60 sacks of regular class A cement. All plugs circulated. | ||||
2132821366 | 2014-07-25 | Well has been plugged in compliance with OAC 1501:9-11. This has resolved the Compliance Notices # 985074867,1357245521 and -1116706422. | ||||
262691999 | 2013-04-10 | Per Request of Enervest on the status of the well. Well is not in compliance with 1509. Waiting on Enervest to Plug well. Plug permit in hand. | ||||
485255462 | 2004-02-18 | |||||
536526114 | 2014-07-24 | I stopped back at site to find out what had plugged the tubing off. It was a red sand and a gray shale. Could be the Red Medina and the Queenston. Chipco is running 1.5tubing in and circulating on every 30 joints. | ||||
-844873200 | 2010-09-09 | FOLLOW UP TO NOV # 985074867 Pulled tubing to use to plug another well. This well is not producing. | ||||
-917044231 | 2014-07-23 | On the date of inspection I accompanied ODNR Inspector Patrick Shreve to check the status of the well plugging. The production casing had been ripped and the service rig was pulling casing at the time of my inspection. Refer to Patrick Shreve's report for further details. | ||||
985074867 | 2010-09-09 | Pulled tubing to use to plug another well. This well is not producing. |
For data sources see[2]