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Difference between revisions of "34-115-22667"

m
 
m
Line 3: Line 3:
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-115-22667
 
| Well ID: 34-115-22667
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.5876863823, -81.8675623899 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.58786863, -81.86764108 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Morgan County, Ohio|Morgan]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[STONEBRIDGE OPERATING CO]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 1982-04-14
 
| Spud Date: 1982-04-14
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Producing
 
|-
 
|-
| Violations: 4
+
| Violations: 0
 
|-
 
|-
| Latitude: 39.5876863823
+
| Latitude: 39.58786863
 
|-
 
|-
| Longitude: -81.8675623899
+
| Longitude: -81.86764108
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 1984-0
 +
| style="text-align:right;" | 9.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1985-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1986-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1987-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1990-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1991-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1995-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1996-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1997-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1998-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2000-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2001-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2002-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2003-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2004-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2005-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2006-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2007-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2008-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2009-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2010-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2011-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2012-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2013-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 274:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 +
|-
 +
| -1016719121
 +
| 2013-12-02
 +
|
 +
| Compliance Action Follow-up 1173472080: There has been no resolution to any of the previous inspector's issues. The well is disconnected from the pumpjack. The well is equipped with a reducer swedge. It is connected to a closed 1 line.
 +
|
 +
|
 +
| Compliance Notice
 +
|-
 +
|-
 +
| -1016719121
 +
| 2013-12-02
 +
|
 +
| Compliance Action Follow-up 1173472080: There has been no resolution to any of the previous inspector's issues. The well is disconnected from the pumpjack. The well is equipped with a reducer swedge. It is connected to a closed 1 line.
 +
|
 +
|
 +
| Compliance Notice
 +
|-
 +
|-
 +
| -1016719121
 +
| 2013-12-02
 +
|
 +
| Compliance Action Follow-up 1173472080: There has been no resolution to any of the previous inspector's issues. The well is disconnected from the pumpjack. The well is equipped with a reducer swedge. It is connected to a closed 1 line.
 +
|
 +
|
 +
| Compliance Notice
 +
|-
 +
|-
 +
| -1016719121
 +
| 2013-12-02
 +
|
 +
| Compliance Action Follow-up 1173472080: There has been no resolution to any of the previous inspector's issues. The well is disconnected from the pumpjack. The well is equipped with a reducer swedge. It is connected to a closed 1 line.
 +
|
 +
|
 +
| Compliance Notice
 +
|-
 +
|-
 +
| -1016719121
 +
| 2013-12-02
 +
|
 +
| Compliance Action Follow-up 1173472080: There has been no resolution to any of the previous inspector's issues. The well is disconnected from the pumpjack. The well is equipped with a reducer swedge. It is connected to a closed 1 line.
 +
|
 +
|
 +
| Compliance Notice
 +
|-
 
|-
 
|-
 
| -1016719121
 
| -1016719121
 
| 2013-12-02
 
| 2013-12-02
|
+
|  
| Compliance Action Follow-up 1173472080: There has been no resolution to any of the previous inspector's issues. The well is disconnected from the pumpjack. The well is equipped with a reducer swedge. It is connected to a closed 1" line.
+
| Compliance Action Follow-up 1173472080: There has been no resolution to any of the previous inspector's issues. The well is disconnected from the pumpjack. The well is equipped with a reducer swedge. It is connected to a closed 1 line.
|
+
|  
|
+
|  
|
+
| Compliance Notice
 
|-
 
|-
 
|-
 
|-
| -1690436418
+
| -1016719121
| 2007-03-09
+
| 2013-12-02
|
+
|  
| FOLLOW UP TO NOV #  1173472080 Upon inspecting site again found well still idle tubing&rods have been removed from well operator stated that casing had a hole in it landowner wants well placed back into production or plugged.
+
| Compliance Action Follow-up 1173472080: There has been no resolution to any of the previous inspector's issues. The well is disconnected from the pumpjack. The well is equipped with a reducer swedge. It is connected to a closed 1 line.
|
+
|  
|
+
|  
|
+
| Compliance Notice
 
|-
 
|-
 
|-
 
|-
| -1761821430
+
| -1016719121
| 2007-03-09
+
| 2013-12-02
|
+
|  
| FOLLOW UP TO NOV #  1173472080 Upon inspecting site again found well still idle tubing&rods have been removed from well operator stated that casing had a hole in it landowner wants well placed back into production or plugged.
+
| Compliance Action Follow-up 1173472080: There has been no resolution to any of the previous inspector's issues. The well is disconnected from the pumpjack. The well is equipped with a reducer swedge. It is connected to a closed 1 line.
|
+
|  
|
+
|  
|
+
| Compliance Notice
 
|-
 
|-
 
|-
 
|-
| -580598964
+
| 1021763819
| 2007-03-09
+
| 2014-09-15
|
+
|  
| FOLLOW UP TO NOV #  1173472080 Upon inspecting site again found well still idle tubing&rods have been removed from well operator stated that casing had a hole in it landowner wants well placed back into production or plugged.
+
| Compliance Action Follow-up 1173472080: There has been no resolution to any of the previous inspector's issues. The well is still idle and disconnected from pumpjack. There was a 1 line attached to the wellhead but it has been cut in half. The wellhead is no longer attached to anything.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1173472080
 
| 1173472080
 
| 2007-03-09
 
| 2007-03-09
|
+
|  
 
| Upon inspecting site again found well still idle tubing&rods have been removed from well operator stated that casing had a hole in it landowner wants well placed back into production or plugged.
 
| Upon inspecting site again found well still idle tubing&rods have been removed from well operator stated that casing had a hole in it landowner wants well placed back into production or plugged.
|
+
|  
| NONE
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1183408571
 
| 1183408571
 
| 2007-07-02
 
| 2007-07-02
|
+
|  
 
| Follow up inspection revealed no change in status of well it is still idle in conversation with local pumper stating  that well has hole in casing,recommend Chief's Order to plug said well.
 
| Follow up inspection revealed no change in status of well it is still idle in conversation with local pumper stating  that well has hole in casing,recommend Chief's Order to plug said well.
|
+
|  
| NONE
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1239017495
 
| 1239017495
 
| 2009-04-06
 
| 2009-04-06
|
+
|  
 
| Inspection revealed that well still remains incapable of producing,pump jack has been removed from site and rods&tubing also in conversation with well owner stating that casing has a hole in it making well infeasable of producing Chief's Order has been requested on said well still awaiting order to be issued.
 
| Inspection revealed that well still remains incapable of producing,pump jack has been removed from site and rods&tubing also in conversation with well owner stating that casing has a hole in it making well infeasable of producing Chief's Order has been requested on said well still awaiting order to be issued.
|
+
|  
| NONE
+
|  
|
+
|
 +
|-
 +
|-
 +
| -1690436418
 +
| 2007-03-09
 +
|
 +
| FOLLOW UP TO NOV #  1173472080 Upon inspecting site again found well still idle tubing&rods have been removed from well operator stated that casing had a hole in it landowner wants well placed back into production or plugged.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -1761821430
 +
| 2007-03-09
 +
|
 +
| FOLLOW UP TO NOV #  1173472080  Upon inspecting site again found well still idle tubing&rods have been removed from well operator stated that casing had a hole in it landowner wants well placed back into production or plugged.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 1965573672
 +
| 2007-03-09
 +
|
 +
| FOLLOW UP TO NOV #  1173472080 Upon inspecting site again found well still idle tubing&rods have been removed from well operator stated that casing had a hole in it landowner wants well placed back into production or plugged.
 +
|
 +
|
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 285033413
 
| 285033413
 
| 2007-12-04
 
| 2007-12-04
|
+
|  
 
| Non-compliance to NOV,well is still idle and incapable of producing in it's present state of repair.
 
| Non-compliance to NOV,well is still idle and incapable of producing in it's present state of repair.
 
Recommend Chief's Order to plug said well.
 
Recommend Chief's Order to plug said well.
|
+
|  
| NONE
+
|  
|
+
|
 +
|-
 +
|-
 +
| -580598964
 +
| 2007-03-09
 +
|
 +
| FOLLOW UP TO NOV #  1173472080  Upon inspecting site again found well still idle tubing&rods have been removed from well operator stated that casing had a hole in it landowner wants well placed back into production or plugged.
 +
|
 +
|
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 625240495
 
| 625240495
 
| 2006-07-31
 
| 2006-07-31
|
+
|  
 
| Stopped by well site to check status of well,owner recently worked on well placed tubing and rods in well and attempted too produce said well on this day tubing and rods have been removed from site apparently there is possible down hole problems will need to monitor site,if owner does not produce well  then Notice of Violation will be in order.
 
| Stopped by well site to check status of well,owner recently worked on well placed tubing and rods in well and attempted too produce said well on this day tubing and rods have been removed from site apparently there is possible down hole problems will need to monitor site,if owner does not produce well  then Notice of Violation will be in order.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| 694890554
 +
| 2007-03-09
 +
|
 +
| FOLLOW UP TO NOV #  -580598964 FOLLOW UP TO NOV #  1173472080  Upon inspecting site again found well still idle tubing&rods have been removed from well operator stated that casing had a hole in it landowner wants well placed back into production or plugged.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -823776680
 +
| 2007-03-09
 +
|
 +
| FOLLOW UP TO NOV #  -1690436418 FOLLOW UP TO NOV #  1173472080 Upon inspecting site again found well still idle tubing&rods have been removed from well operator stated that casing had a hole in it landowner wants well placed back into production or plugged.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 866308939
 +
| 2007-03-09
 +
|
 +
| FOLLOW UP TO NOV #  -1761821430 FOLLOW UP TO NOV #  1173472080  Upon inspecting site again found well still idle tubing&rods have been removed from well operator stated that casing had a hole in it landowner wants well placed back into production or plugged.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 969133132
 
| 969133132
 
| 2014-04-01
 
| 2014-04-01
|
+
|  
| Compliance Action Follow-up 1173472080: There has been no resolution to any of the previous inspector's issues. The well is still idle and disconnected from pumpjack. There is a 1" line with a shut valve attached to the swage. I will refer this well to my supervisor for legal review.
+
| Compliance Action Follow-up 1173472080: There has been no resolution to any of the previous inspector's issues. The well is still idle and disconnected from pumpjack. There is a 1 line with a shut valve attached to the swage. I will refer this well to my supervisor for legal review.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 05:26, 16 July 2015

Well Details

Well ID: 34-115-22667
Loading map...
County: Morgan
Municipality:
Operator Name: STONEBRIDGE OPERATING CO
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1982-04-14
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 39.58786863
Longitude: -81.86764108

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 9.0 0.0
1985-0 0.0 0.0
1986-0 0.0 0.0
1987-0 0.0 0.0
1990-0 0.0 0.0
1991-0 0.0 0.0
1995-0 0.0 0.0
1996-0 0.0 0.0
1997-0 0.0 0.0
1998-0 0.0 0.0
2000-0 0.0 0.0
2001-0 0.0 0.0
2002-0 0.0 0.0
2003-0 0.0 0.0
2004-0 0.0 0.0
2005-0 0.0 0.0
2006-0 0.0 0.0
2007-0 0.0 0.0
2008-0 0.0 0.0
2009-0 0.0 0.0
2010-0 0.0 0.0
2011-0 0.0 0.0
2012-0 0.0 0.0
2013-0 0.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1016719121 2013-12-02 Compliance Action Follow-up 1173472080: There has been no resolution to any of the previous inspector's issues. The well is disconnected from the pumpjack. The well is equipped with a reducer swedge. It is connected to a closed 1 line. Compliance Notice
-1016719121 2013-12-02 Compliance Action Follow-up 1173472080: There has been no resolution to any of the previous inspector's issues. The well is disconnected from the pumpjack. The well is equipped with a reducer swedge. It is connected to a closed 1 line. Compliance Notice
-1016719121 2013-12-02 Compliance Action Follow-up 1173472080: There has been no resolution to any of the previous inspector's issues. The well is disconnected from the pumpjack. The well is equipped with a reducer swedge. It is connected to a closed 1 line. Compliance Notice
-1016719121 2013-12-02 Compliance Action Follow-up 1173472080: There has been no resolution to any of the previous inspector's issues. The well is disconnected from the pumpjack. The well is equipped with a reducer swedge. It is connected to a closed 1 line. Compliance Notice
-1016719121 2013-12-02 Compliance Action Follow-up 1173472080: There has been no resolution to any of the previous inspector's issues. The well is disconnected from the pumpjack. The well is equipped with a reducer swedge. It is connected to a closed 1 line. Compliance Notice
-1016719121 2013-12-02 Compliance Action Follow-up 1173472080: There has been no resolution to any of the previous inspector's issues. The well is disconnected from the pumpjack. The well is equipped with a reducer swedge. It is connected to a closed 1 line. Compliance Notice
-1016719121 2013-12-02 Compliance Action Follow-up 1173472080: There has been no resolution to any of the previous inspector's issues. The well is disconnected from the pumpjack. The well is equipped with a reducer swedge. It is connected to a closed 1 line. Compliance Notice
-1016719121 2013-12-02 Compliance Action Follow-up 1173472080: There has been no resolution to any of the previous inspector's issues. The well is disconnected from the pumpjack. The well is equipped with a reducer swedge. It is connected to a closed 1 line. Compliance Notice
1021763819 2014-09-15 Compliance Action Follow-up 1173472080: There has been no resolution to any of the previous inspector's issues. The well is still idle and disconnected from pumpjack. There was a 1 line attached to the wellhead but it has been cut in half. The wellhead is no longer attached to anything.
1173472080 2007-03-09 Upon inspecting site again found well still idle tubing&rods have been removed from well operator stated that casing had a hole in it landowner wants well placed back into production or plugged.
1183408571 2007-07-02 Follow up inspection revealed no change in status of well it is still idle in conversation with local pumper stating that well has hole in casing,recommend Chief's Order to plug said well.
1239017495 2009-04-06 Inspection revealed that well still remains incapable of producing,pump jack has been removed from site and rods&tubing also in conversation with well owner stating that casing has a hole in it making well infeasable of producing Chief's Order has been requested on said well still awaiting order to be issued.
-1690436418 2007-03-09 FOLLOW UP TO NOV # 1173472080 Upon inspecting site again found well still idle tubing&rods have been removed from well operator stated that casing had a hole in it landowner wants well placed back into production or plugged.
-1761821430 2007-03-09 FOLLOW UP TO NOV # 1173472080 Upon inspecting site again found well still idle tubing&rods have been removed from well operator stated that casing had a hole in it landowner wants well placed back into production or plugged.
1965573672 2007-03-09 FOLLOW UP TO NOV # 1173472080 Upon inspecting site again found well still idle tubing&rods have been removed from well operator stated that casing had a hole in it landowner wants well placed back into production or plugged.
285033413 2007-12-04 Non-compliance to NOV,well is still idle and incapable of producing in it's present state of repair.

Recommend Chief's Order to plug said well.

-580598964 2007-03-09 FOLLOW UP TO NOV # 1173472080 Upon inspecting site again found well still idle tubing&rods have been removed from well operator stated that casing had a hole in it landowner wants well placed back into production or plugged.
625240495 2006-07-31 Stopped by well site to check status of well,owner recently worked on well placed tubing and rods in well and attempted too produce said well on this day tubing and rods have been removed from site apparently there is possible down hole problems will need to monitor site,if owner does not produce well then Notice of Violation will be in order.
694890554 2007-03-09 FOLLOW UP TO NOV # -580598964 FOLLOW UP TO NOV # 1173472080 Upon inspecting site again found well still idle tubing&rods have been removed from well operator stated that casing had a hole in it landowner wants well placed back into production or plugged.
-823776680 2007-03-09 FOLLOW UP TO NOV # -1690436418 FOLLOW UP TO NOV # 1173472080 Upon inspecting site again found well still idle tubing&rods have been removed from well operator stated that casing had a hole in it landowner wants well placed back into production or plugged.
866308939 2007-03-09 FOLLOW UP TO NOV # -1761821430 FOLLOW UP TO NOV # 1173472080 Upon inspecting site again found well still idle tubing&rods have been removed from well operator stated that casing had a hole in it landowner wants well placed back into production or plugged.
969133132 2014-04-01 Compliance Action Follow-up 1173472080: There has been no resolution to any of the previous inspector's issues. The well is still idle and disconnected from pumpjack. There is a 1 line with a shut valve attached to the swage. I will refer this well to my supervisor for legal review.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.