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34-111-24433

Well Details

Well ID: 34-111-24433
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County: Monroe
Municipality:
Operator Name: HG ENERGY LLC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2014-02-11
Unconventional: No
Configuration: Vertical
Well Status: Well Drilled
Violations: 0
Latitude: 39.67951802
Longitude: -81.17192345

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1015453037 2014-09-25 Milling on old packer and the hope to be ready to run new packer later this week if all goes well.
-1057808470 2014-02-12 On site to witness running and cementing of 9.625 casing Decker Drilling drilled to a depth of 190' and ran 160' of casing equipped with 1-guide shoe and 1 centralize and 1 cement basket and Baker Hughes cemented it in place with 85 sacks of Class A cement and they had 7 bbl of good returns.
1128492295 2014-03-17 On site to witness Baker Hughes set composite plug in bottom of casing and once they set plug we will pressure test entire string for integrity.

Note: Pressure test failed again after setting composite bridge plug above float collar in bottom of casing, company rep stated they were looking for multi-set inflatable packer to try and find leaking casing.

117499401 2014-05-20 On site performing site evaluation for conversion of well to injection well status.
1392141147 2014-02-11 The said well was spudded by Decker Well Service rig # 9 with a 28' X 13.375 54# casing working string set for the rig to attach their drilling air body to, 50 sacks of class A -3% calcium -1/4# flake cement was mixed and the casing cemented to surface, the company has also set a tin horn and will be solidifying all cutting on this location.
1392256329 2014-02-12 On 02/12/14 the conductor was set and cemented to surface with 170' of 9.625 36# casing used and Bake Hughes cement services using 85 sacks of class A 1/4# flake 3% calcium cement with 6 barrels of good cement returns to surface.
1392397066 2014-02-14 On 02/13/14 1308' of 7 surface casing was set and cemented to surface using 275 sacks of class A 3% calcium-1/4# flake cement with 50% excess ran and 20 barrels of cement returns to surface, the well will now be turned over to the region UIC inspector Dave Ball for the production borehole and casing completion.
1392407349 2014-02-13 On site to witness running of 7 surface casing Decker Drilling drilled too a depth of 1310' and they ran 1308' of limited service casing equipped with 1-guide shoe and 15 centralizes and Baker Hughes cemented with 275 sacks cement with 20 bbl of good returns.
1392414591 2014-02-14 On site to witness testing of annular BLOWOUT PREVENT OR the first attempt failed due to faulty bladder in the annular, once it was replaced they attempted to test it again and it held 500# for fifth teen minutes with no decline in pressure(test passed).
1392764556 2014-02-18 Stopped by drilling rig for update they were broke down at the time of my inspection and there depth was 1760' and the well bore was still dry at this point.
1393689885 2014-03-01 On site to witness cementing of second stage of cementing process.

Note: Total depth of well was noted at 8005' and they ran a total of 7938' of 4.5 casing and Baker Hughes cemented it in place with 826 sacks total. Note stage tool@4112' and they had good returns on both stages of cementing process.

1394378958 2014-03-09 On site to witness Baker Hughes try and perform squeeze job on stage tool, bridge plug was set at 4165' and retainer was set at 4105' and stage tool was@4112' GL. They pumped water ahead and then stung into retainer and hole pressured up to 3500# and after several attempts they decided too drill out retainer and pressure test casing again.
1394485568 2014-03-10 On site to witness Baker Hughes try and perform squeeze job on stage tool, bridge plug was set at 4165' and retainer was set at 4105' and stage tool was@4112' GL. Baker Hughes on site again too squeeze cement on faulty stage tool.

Note: Baker Hughes used 100 sacks of cement to perform squeeze job.

1394655675 2014-03-12 Squeeze job on stage tool failed again and decision was made to acquire a casing patch and place it over the faulty stage tool.
1395706621 2014-03-24 Status check inspection on the 4.5 11.6# production casing repair process, the company has a work over rig on the hole and has set a Weathorford casing patch over the 2 stage DV tool at 4011' after the initial casing pressure test did not pass and indicated the DV tool was leaking, the initial 20' casing patch did not pressure test after being set and was milled out and the company has run several casing logs and is preparing to set a second patch to be 40' long, the casing patch burst pressure is rated at 9,000 psi.
1396197200 2014-03-28 On site to witness Archer Wireline Company perforate casing at 7545'-7551' 24 shots and once perforation procedure was complete it was noted that wellbore went on slight vacuum and fluid levels in hole were down 1000' when they brought out wireline tools.
1396385989 2014-03-30 On site to attempt to perform injection testing owner was unable too test at this time due to pressure issues.
1396812591 2014-04-04 On site to witness injectivity testing of said well,Weatherford pump man started injecting at a rate of 1.1 bpm@1910 psi and 45 minutes into testing they injected 100 bbl of water,4/5/14 7a.m. 2.3 bpm@1910 psi and 12:30 p.m. they were at 1.7 bpm at 1950 psi and 4/6/14 @7a.m. they were injecting@2.7 bpm@1980 psi operator will call at conclusion of testing to inform me of total bbls put away and final injection pressures.
1405289599 2014-07-10 Inspection revealed that owner is waiting on SWIW permit to be issued and once issued they will begin construction of surface facility.
1410305578 2014-09-09 Inspection revealed that there has been no change in status of well it still needs to be completed and tubing and packer ran into well and surface facility constructed.
1411080818 2014-09-17 On site to witness tubing and packer run into well and witness pressure testing.

Weatherford inflatable packer was run to a depth of 7477' and packer deployed and they tried to pressure test after pumping 106 barrel of fresh water and inhibitor and testing failed they will try and set dart inside of tubing to pressure test it and if it checks out they will pull entire string from well bore.

1412026448 2014-09-28 On site to witness tubing and packer run into well bore this is the third Weatherford Inflatable packer that has been run into this well and setting depth is 7457' and we tested annulus at 400 psi with no decline in pressure.

Note: Two pen recorder required to monitor pressures when owner get authorization to place well into injection well status.

1441068900 2014-10-27 On site to witness injection test on said well I monitored injection pressures to make sure they did not exceed maximum injection pressure of 1935 psi and also monitored annulus pressure to make sure injection string or packer showed any signs of loss integrity.

Note: Testing was cancelled after six hours of fighting pressure issues.

-1463099593 2015-02-26 Inspection revealed that there is no activity at the site at this time.

Note: Well has been sold to AEU Energy and they are waiting on well to be transferred to there bond.

-151954226 2014-02-20 Rig crew tripping bit@4340' should be back to drilling this afternoon.
1532934666 2014-03-06 Stopped by service rig for update they were drilling on stage tool and once drilled they will run to bottom and tag float collar.
-1571475981 2014-03-26 On site to pressure test integrity of production casing after setting casing patch they applied 1950 psi and we monitored pressure for 15 minutes with a 18lb pressure loss which is 1% loss in pressure which is acceptable.
-1575080932 2014-09-22 Stone Service Rig milling on top of packer in hopes of trying to possibly retrieve tomorrow.
1764348099 2014-02-20 Status check inspection of the drilling process found the current drilling depth to be 4340' using a 6.5 hammer drill bit and misting on air with a good oil show at 1680' while drilling- The Keener sand.
1816274858 2014-06-17 Inspection revealed that well is waiting on company to submit conversion plan for SWIW facility.
1933450876 2014-03-21 On site to witness testing of inflatable packer ,owner trying to determine where possible leakage in tubing may be Weatherford Services ran packer down below casing patch and set packer and we pressured up.
-2025994037 2014-02-25 Status check inspection on the drilling progress found the current drilling depth to be 7500' using a 6.5 drill bit and the company currently running in the hole with the drill string after a bit change.
386263641 2014-12-21 Inspection revealed that restoration work at site is satisfactory there is vegetation established and there were no pits to be closed they drilled well with a closed loop system.
466701100 2014-03-24 Stone Energy's Service rig ran 40' HOMCO casing patch in well today and they plan on letting resign set up for 36 hours before pressure testing casing and if pressure test passes then they will continue to complete well.
521142384 2014-03-05 Stone Energy service rig moving in on well to drill out stage tool@4112' and clean out hole to total depth.
-676941115 2014-02-26 Inspection revealed that rig crew was tripping bit at 7646' and hope to be back to drilling later tonight.
-677659995 2014-03-15 On site to witness setting of Weatherford HOMCO 10,000 PSI patch which was set at 4125'-4105' which was centered over center of faulty cement stage tool and while setting it rig crew blew a bad high pressure line and after line was repaired they proceeded to set patch and once set they started out of hole standing back tubing string.

Note: Operator will pressure test casing after they let resin cure for 24 hours.

836714233 2014-09-26 On site to witness Stone Energy Service rig start Weatherford packer in hole and they ran it to a depth of 7498' and we attempted to circulate fresh water and inhibitor into annulus of tubing with no luck due to inflatable packer setting before they could circulate inhibitor so decision was made to release packer and pull it again from well bore and once they determine what their next move will be they were instructed to contact inspector.
846199601 2014-09-18 Went by site to consult with company rep discussing the next step in trying to get another packer on site and ready to run in well and possibly be ready to perform additional testing.

For data sources see[1]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20.