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34-111-24109

Well Details

Well ID: 34-111-24109
County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date:
Unconventional:
Horizontal:
Producing:
Violations:
Latitude:
Longitude:

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
1179788941 2007-05-21 On site to witness testing of BOP,operator closed BOP and pressured up to 500 psi and attempted to test first test failed due to faulty flange gasket,second attempt passed after operator changed seal ring and renippled up BOP no leaks detected after new seal ring installed.
1288703869 2010-11-02 On day of inspection well is supplied with a rabbet and 7cas,4.5cas,1.5tubing.There is a 100bbl tank with dike, id and all carbon filters inplace.Preliminary restoration passed.
17587135 2011-10-31 On day of inspection well was complete with plunger lift system. Tank battery contents included one 110 barrel oil storage tank and a mechanical separator. Site met requirements of the ORC and preliminary restoration is now passed.
2147433744 2012-07-16 Inspection of the well head found the following equipment present, 4.5production casing, 1.5 tubing with the commercial production valves closed and the domestic valves open, the well being produced by the means of a plunger lift system . A single 100 barrel tank along with a separator and gas meter are present in an established containment dike with proper well identification present.