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Difference between revisions of "34-099-22131"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-099-22131
 
| Well ID: 34-099-22131
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.0003510923, -80.6289756596 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.00041068, -80.62927426 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Mahoning County, Ohio|Mahoning]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[OHIO VALLEY ENERGY SYSTEM CORP]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 1987-10-30
 
| Spud Date: 1987-10-30
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Producing
 
|-
 
|-
 
| Violations: 0
 
| Violations: 0
 
|-
 
|-
| Latitude: 41.0003510923
+
| Latitude: 41.00041068
 
|-
 
|-
| Longitude: -80.6289756596
+
| Longitude: -80.62927426
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 1988-0
 +
| style="text-align:right;" | 15401.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1990-0
 +
| style="text-align:right;" | 9984.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1992-0
 +
| style="text-align:right;" | 1703.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1993-0
 +
| style="text-align:right;" | 5076.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1994-0
 +
| style="text-align:right;" | 5212.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1995-0
 +
| style="text-align:right;" | 4535.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1996-0
 +
| style="text-align:right;" | 3456.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1997-0
 +
| style="text-align:right;" | 4644.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1998-0
 +
| style="text-align:right;" | 5243.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1999-0
 +
| style="text-align:right;" | 4227.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2000-0
 +
| style="text-align:right;" | 3252.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2001-0
 +
| style="text-align:right;" | 2098.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2002-0
 +
| style="text-align:right;" | 2505.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2003-0
 +
| style="text-align:right;" | 2821.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2004-0
 +
| style="text-align:right;" | 2421.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2005-0
 +
| style="text-align:right;" | 2465.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2006-0
 +
| style="text-align:right;" | 1815.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2007-0
 +
| style="text-align:right;" | 1629.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2008-0
 +
| style="text-align:right;" | 1691.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2009-0
 +
| style="text-align:right;" | 2068.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2010-0
 +
| style="text-align:right;" | 1841.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2011-0
 +
| style="text-align:right;" | 1714.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2012-0
 +
| style="text-align:right;" | 1666.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2013-0
 +
| style="text-align:right;" | 1470.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2014-0
 +
| style="text-align:right;" | 3744.0
 +
| style="text-align:right;" | 365.0
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 365.0
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 283:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
 
| 1216i617
 
| 1216i617
 
| 2002-05-31
 
| 2002-05-31
|
+
|  
 
| Obtained GPS coordinates.
 
| Obtained GPS coordinates.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1285785742
 
| 1285785742
 
| 2010-09-29
 
| 2010-09-29
|
+
|  
 
| I performed a random field inspection.  I GPS'd both the tank battery and the wellhead.  I continued to walk around both the wellhead and the tank battery.  This inspection satisfies 1501:9-9-05.  There were no violations at this time.
 
| I performed a random field inspection.  I GPS'd both the tank battery and the wellhead.  I continued to walk around both the wellhead and the tank battery.  This inspection satisfies 1501:9-9-05.  There were no violations at this time.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1322929132
 
| 1322929132
 
| 2004-02-19
 
| 2004-02-19
|
+
|  
 
| The tank battery consists of 1-100 bbl storage tank, 1-50 bbl salt water tank and a dike.
 
| The tank battery consists of 1-100 bbl storage tank, 1-50 bbl salt water tank and a dike.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1359649420
 
| 1359649420
 
| 2013-01-29
 
| 2013-01-29
|
+
|  
 
| I stopped on this location to check on a collapsed 50 barrel production tank for inspector John Fleming. The tank is severely damaged and can no longer hold any fluid beyond the 12 inches that is currently in the tank. A 100 barrel production tank with a semi corroded flow line is currently used for production. The operator has been contacted and the issue is going to be taken care of. There is no oil or brine leaks in the tank battery and everything is contained by a SPCC dike.
 
| I stopped on this location to check on a collapsed 50 barrel production tank for inspector John Fleming. The tank is severely damaged and can no longer hold any fluid beyond the 12 inches that is currently in the tank. A 100 barrel production tank with a semi corroded flow line is currently used for production. The operator has been contacted and the issue is going to be taken care of. There is no oil or brine leaks in the tank battery and everything is contained by a SPCC dike.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| PL12669
 
| PL12669
|
+
|  
|
+
|  
 
| Preliminary Restoration  done information from Data Point
 
| Preliminary Restoration  done information from Data Point
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 07:57, 15 July 2015

Well Details

Well ID: 34-099-22131
Loading map...
County: Mahoning
Municipality:
Operator Name: OHIO VALLEY ENERGY SYSTEM CORP
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1987-10-30
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 41.00041068
Longitude: -80.62927426

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1988-0 15401.0 0.0
1990-0 9984.0 0.0
1992-0 1703.0 0.0
1993-0 5076.0 0.0
1994-0 5212.0 0.0
1995-0 4535.0 0.0
1996-0 3456.0 0.0
1997-0 4644.0 0.0
1998-0 5243.0 0.0
1999-0 4227.0 0.0
2000-0 3252.0 0.0
2001-0 2098.0 0.0
2002-0 2505.0 0.0
2003-0 2821.0 0.0
2004-0 2421.0 0.0
2005-0 2465.0 0.0
2006-0 1815.0 0.0
2007-0 1629.0 0.0
2008-0 1691.0 0.0
2009-0 2068.0 0.0
2010-0 1841.0 0.0
2011-0 1714.0 0.0
2012-0 1666.0 0.0
2013-0 1470.0 0.0
2014-0 3744.0 365.0 0.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1216i617 2002-05-31 Obtained GPS coordinates.
1285785742 2010-09-29 I performed a random field inspection. I GPS'd both the tank battery and the wellhead. I continued to walk around both the wellhead and the tank battery. This inspection satisfies 1501:9-9-05. There were no violations at this time.
1322929132 2004-02-19 The tank battery consists of 1-100 bbl storage tank, 1-50 bbl salt water tank and a dike.
1359649420 2013-01-29 I stopped on this location to check on a collapsed 50 barrel production tank for inspector John Fleming. The tank is severely damaged and can no longer hold any fluid beyond the 12 inches that is currently in the tank. A 100 barrel production tank with a semi corroded flow line is currently used for production. The operator has been contacted and the issue is going to be taken care of. There is no oil or brine leaks in the tank battery and everything is contained by a SPCC dike.
PL12669 Preliminary Restoration done information from Data Point

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.