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34-067-20777

Well Details

Well ID: 34-067-20777
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County: Harrison
Municipality:
Operator Name: RHDK OIL & GAS LLC/DBA RED HIL
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1986-10-07
Unconventional: No
Configuration: Vertical
Well Status: Plugged and Abandoned
Violations: 0
Latitude: 40.26197611
Longitude: -81.16777837

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1986-0 0.0 0.0
1987-0 4626.0 0.0
1988-0 4767.0 0.0
1989-0 3337.0 0.0
1990-0 2508.0 0.0
1991-0 2520.0 0.0
1992-0 2137.0 103.0
1993-0 2197.0 0.0
1994-0 2399.0 0.0
1995-0 3.0 0.0
1996-0 2319.0 0.0
1997-0 1342.0 0.0
1998-0 1917.0 0.0
1999-0 1869.0 0.0
2000-0 1710.0 0.0
2001-0 1375.0 0.0
2002-0 1336.0 0.0
2003-0 1255.0 0.0
2004-0 1397.0 0.0
2005-0 1524.0 84.0
2006-0 1717.0 0.0
2007-0 1496.0 0.0
2008-0 1230.0 0.0
2009-0 1114.0 0.0
2010-0 929.0 0.0
2011-0 1174.0 0.0
2012-0 1178.0 0.0
2013-0 1136.0 0.0
2014-0 117.0 365.0 69.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
104577530 2013-12-04 Amercian Energy Partners is moving equipment in to begin drilling today. They are moving past this well to drill the new one. Met with the land owner and went over the move and drilling of the new well.
1340119201 2014-02-25 Plug job for today cancelled due to rig repairs. Drilling line broke and blocks dropped after pulling stretch on the 4-1/2 inch casing.
1393433261 2014-02-26 I am on site today to check on the plugging operation. The rig is down for repairs due to a broken drilling line. The blocks have not been re-strung so no plugging today.
15459 PASSED Y WITNESSED 2/23/93 INSPECTOR MIKE KAVAGE DATE 02/2319/93 DATA FROM OLD VAX INFO
15460 PASSED Y WITNESSED 6/30/92 INSPECTOR MIKE KAVAGE DATE 06/3019/92 DATA FROM OLD VAX INFO
-1620233409 2014-02-24 Service hands are working on the rig today. Half of the total plugs were set on Monday. I was advised that they plan to finish plugging Tues. at 9 AM
2127715740 2014-02-21 Petroset Cementing set a 1000' cement plug over the Utica formation and a 300' plug over the Clinton formation. See the plugging report for details.
-225236382 2014-02-28 This well was plugged and abandoned this date. See the plugging report for the details.
-244353164 2014-02-10 This job was scheduled to set the bottom plug today but there is nobody on site at this time ? Will return later today to check on status. I did return later and found that they have a mill in the hole to drill out the obstruction at 5200 ft.
-8004672 2014-03-13 Production casing has been cut off and pits are pumped off ready to close. No leaks were detected in or around the casing.
-928969035 2014-03-31 The pits are closed and the area has been graded. The site will need further grading and seeding. Vegetation has not been established and some production equipment needs to be removed before final restoration can be passed.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.