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Well ID: 34-059-24341 | Loading map...
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County: Guernsey | |
Municipality: | |
Operator Name: AMERICAN ENERGY UTICA LLC | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2014-06-25 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Drilling | |
Violations: 0 | |
Latitude: 40.12758403 | |
Longitude: -81.34572085 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
12335113 | 2014-11-13 | On the day of my inspection I found that Nomac Drilling rig 80 had reached a total depth of 15985'. They were in the process of running new 5.5 production casing. AEU reported that a spill had just occurred prior to my arrival. They estimated that 20 gallons of oil based mud had been released from a CurryVac truck. The mud was released outside of containment. No fluid made it off of the drilling pad. The spill had been cleaned up by the time I was notified. The contaminated gravel had been scraped up and sent to the landfill. I did not observe any residual contamination at the spill site. | ||||
1403786729 | 2014-06-26 | On the day of my inspection accompanied by ODNR Inspector Brandon Trigg, I witnessed Precision Rathole Inc. drilled a 36 inch diameter hole to the depth of 100 feet and ran 100 feet of 30 inch 118.65#/ft. conductor pipe. O-Tex Pumping LLC was on site and gained circulation with 5bbls of fresh water, 15bbls of gel and 5bbls of fresh water. O-Tex cemented pipe with 370 sacks of class H cement with 2%CaCl, .4% C41P and | ||||
1414428206 | 2014-10-27 | On the date of inspection I was informed by American Energy Utica (AEU) consultant Van Dietrich that the Nomac 80 rig had drilled a 17.5 inch diameter hole to a depth of 970 feet. Wyoming Casing Crew set 13.375 inch 54.50lbs/ft casing on bottom. O-Tex Pumping, LLC pumped 1270sk of Class H cement, 15.6ppg, 1.2 yield, 2% CaCl, 0.25lbs/sk flake, 0.4% C-41P. O-Tex released the plug and approximately 2bbl into displacement the pressure spiked to 625psi. O-Tex stopped pumping and bled off pressure but still continued to pressure up. AEU plans to drill out the plug and cement, run a Cement Bond Log to find the top of cement, and then decide how to bring cement to surface from there. | ||||
1428589695 | 2015-04-09 | On the day of my inspection production equipment has been installed and awaiting on frac. The site passed preliminary restoration according to ORC 1509.072A. | ||||
-1866798004 | 2014-06-25 | On the day of my inspection I was on location to set conductor and I witnessed that Precision Rathole Inc. was drilling a 36 inch diameter hole at a depth of 90 feet with a planned td of 100 | ||||
-382273940 | 2014-06-26 | On the date of inspection I accompanied ODNR Inspector Doug Bennett to witness a conductor cement string. Refer to Doug Bennett's report for further details. | ||||
750026647 | 2014-07-09 | On the day of my inspection I witnessed Precision Rathole Inc. was on site drilling mouse holes. I met with Drilling Supervisor Garry Reynolds and verified that top of cement was tagged inside conductor at 77 feet. | ||||
975637734 | 2014-11-05 | On the day of my inspection I found that Nomac Drilling rig 80 had new 9.625 casing ran to a depth of 6486'. The casing was equipped with a DV tool at 3516'. They were circulating when I arrived. O-Tex Pumping attempted to cement the casing to surface in one stage. Although good circulation was maintained throughout the job, no cement was circulated to surface. There were approximately 3 barrels of gel spacer circulated to surface when O-Tex reached their maximum displacement volume. Nomac 80 opened the DV tool and circulated for 12 hours. O-Tex cemented the second stage of the job. Good circulation was maintained throughout the job with approximately 80 barrels of cement returns. |
For data sources see[1]