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Well ID: 34-055-22121 | Loading map...
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County: | |
Municipality: | |
Operator Name: | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2010-09-04 | |
Unconventional: | |
Horizontal: | |
Producing: No | |
Violations: 0 | |
Latitude: 41.5156224126 | |
Longitude: -81.3485983751 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
---|---|---|---|---|---|---|
-1094898692 | 2010-09-04 | The conductor pipe was installed and cemented. All conditions were satisfactory. | ||||
-1882905779 | 2010-09-05 | Surface casing was installed and cemented. Adequate cement returns were observed. Cement operation met all requirements. | ||||
-391689665 | 2012-01-04 | Well and battery are in good repair and all man doors are locked. An identification sign needs posted. | ||||
-831195134 | 2010-10-08 | Operator was flowing well back. Site was in good repair. Lease road was stable. Pits were closed. Bull plugs were in frac Tanks. | ||||
-833779958 | 2011-07-13 | Well is a rabbit well, the catcher is red in color. Zero psi on the annulus. Locks on load lines. Identification is posted. Valve on dike drain. 2 100Bbl production tanks 1500 gallon poly tank and a mechincal separator are in the battery. Lease road is stable. Locks on man doors. Spacing is correct. | ||||
1286378280 | 2010-10-05 | Frac crew was moving off site. Frac job per the operator went well. Operator submitted Bond/cement log for the GCC#2. The 5 day annulus test result was 66psi. Lockport Top is 3114 top of the cement is 3050. Operator has 64' of coverage above the Lockport. | ||||
1973566843 | 2013-05-28 | My inspection found the well to be equipped with a plunger lift unit. The annulus valve is open and plumbed into a pop off valve that is plumbed into the production tank. The tank battery and well are in good repair and surrounded by a chain link fence. The tank battery consists of two 100 BBL production tanks, a 50 BBL poly brine tank, and a mechanical separator. The vent stack on the production tank is plumbed into a 55 gallon charcoal filter. The vent stack is then plumbed up and topped with a spark arrestor. The proper identification is located on the tank battery. The lease road is in stable condition. |