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Well ID: 0595260207003 | Loading map...
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Location: 00/07-02-059-26W5/3 | |
Location Alias: 00/07-02-59-26 W5M | |
Location Alias 2: 00/07-02-059-26 W5/03 | |
Country: Canada | |
Province: Alberta | |
Township: 059 | |
Meridian: 5 | |
Range: 26 | |
Section: 02 | |
County/Municipality: Municipal District of Greenview No. 16 | |
Well Name: CNRL LELAND 7-2-59-26 | |
Operator Name: Canadian Natural Resources Limited | |
License Number: 0207242 | |
License Date: 1997-10-10 | |
License Status: Suspension | |
Spud Date: 1998-12-12 | |
Final Drill Date: 1999-03-31 | |
Well Total Depth: 3951.50 m | |
Surface Hole Latitude: 54.071686 | |
Surface Hole Longitude: -117.786499 |
Date | Event |
---|---|
1997-10-10 | Obtained License |
1998-12-14 | Surface Casing Operation Performed |
1998-12-29 | Lost Circulation Occurred |
1999-02-08 | Direction Drilling Operation Performed - Sidetrack Fish |
1999-02-21 | Intermediate Casing Operation Performed |
1999-03-29 | Direction Drilling Operation Performed - Sidetrack Fish |
1999-03-31 | Finished Drilling |
1999-03-31 | Well Log Performed |
1999-04-02 | Liner Casing Operation Performed |
1999-04-03 | Rig Released |
1999-04-03 | Well Mode changed to Drilled and Cased |
1999-06-26 | Perforation Treatment Performed - Jet Perforation |
1999-06-26 | Well Log Performed |
1999-06-28 | Perforation Treatment Performed - Acid Squeeze - Press Used |
1999-06-29 | Perforation Treatment Performed - Acid Squeeze - Press Used |
1999-07-01 | Perforation Treatment Performed - Jet Perforation |
1999-07-01 | Well Log Performed |
1999-07-03 | Perforation Treatment Performed - Acid Squeeze - Press Used |
1999-07-04 | Perforation Treatment Performed - Acid Squeeze - Press Used |
1999-08-21 | Perforation Treatment Performed - Jet Perforation |
1999-08-21 | Well Log Performed |
1999-08-22 | Perforation Treatment Performed - Cement Squeeze |
1999-08-26 | Well Log Performed |
1999-08-27 | Well Log Performed |
1999-09-08 | Well Log Performed |
1999-09-09 | Perforation Treatment Performed - Casing Patch (Over Perfs) |
1999-09-09 | Well Log Performed |
1999-09-20 | Perforation Treatment Performed - Cement Squeeze |
1999-12-17 | Well Began Production |
1999-12-17 | Well Fluid changed to Gas |
1999-12-17 | Well Mode changed to Flowing |
2009-06-14 | Well Fluid changed to Gas |
2009-06-14 | Well Mode changed to Suspended |
For data sources see[3]
Start Date | Depth (m) | Reason |
---|---|---|
1999-02-08 | 3248.40 | Sidetrack fish |
1999-03-29 | 3787.00 | Sidetrack fish |
For data sources see[4]
Perforation Date | Perforation Type | Interval Top (m) | Interval Base (m) | Number of Shots |
---|---|---|---|---|
1999-06-26 | Perforation | 3911.00 | 3915.00 | 13 |
1999-06-28 | Acid Treatment | 3911.00 | 3915.00 | 0 |
1999-06-29 | Acid Treatment | 3911.00 | 3915.00 | 0 |
1999-07-01 | Perforation | 3872.00 | 3875.00 | 13 |
1999-07-01 | Perforation | 3878.00 | 3884.00 | 13 |
1999-07-01 | Perforation | 3889.00 | 3901.00 | 13 |
1999-07-03 | Acid Treatment | 3872.00 | 3901.00 | 0 |
1999-07-04 | Acid Treatment | 3872.00 | 3901.00 | 0 |
1999-08-21 | Perforation | 2190.00 | 2190.50 | 14 |
1999-08-21 | Perforation | 1905.00 | 1905.50 | 14 |
1999-08-22 | Cement Squeeze | 1905.00 | 1905.50 | 0 |
1999-09-09 | Casing Patch | 2190.00 | 2190.50 | 0 |
1999-09-20 | Cement Squeeze | 1905.00 | 2190.50 | 0 |
For data sources see[5]
Period | Total Production Hours | Gas Quantity (m3) | Oil Quantity (m3) | Water Quantity (m3) |
---|---|---|---|---|
1999 | 347 | 0.0 | 0.0 | 0.0 |
2000 | 7132 | 0.0 | 0.0 | 0.0 |
2001 | 7051 | 0.0 | 0.0 | 0.0 |
2002 | 7449 | 0.0 | 0.0 | 0.0 |
2003 | 6925 | 0.0 | 0.0 | 0.0 |
2004 | 6001 | 0.0 | 0.0 | 0.0 |
2005 | 6648 | 0.0 | 0.0 | 0.0 |
2006 | 7490 | 0.0 | 0.0 | 0.0 |
2007 | 7246 | 0.0 | 0.0 | 0.0 |
2008 | 6835 | 0.0 | 0.0 | 0.0 |
2009 | 948 | 0.0 | 0.0 | 0.0 |
For data sources see[6]
Occurence Date | Occurence Type | Occurence Depth (m) | Occurence Control Depth (m) |
---|---|---|---|
1998-12-29 | Lost Circulation | 3070.00 | 3951.50 |
For data sources see[7]