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Well ID: 37-007-20396 | Loading map...
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Operator Name: PENNENERGY RESOURCES LLC | |
Well Pad ID: 145356 | |
First Permit Date: 2013-07-08 | |
Last Permit Date: 2013-07-08 | |
Spud Date: 2013-09-11 | |
Unconventional: Yes | |
Horizontal: No | |
Violations: None | |
Latitude: 40.73963 | |
Longitude: -80.1691 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2013-2 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|---|---|---|---|---|---|---|---|
2013-2 | DRILL CUTTINGS | 752.0 | Tons | LANDFILL | CID # 28726 | CARBON LIMESTONE LANDFILL - BFI | LOWELLVILLE | OH |
2013-2 | DRILLING FLUID WASTE | 3835.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | EPA ID: 748-163 | PATRIOT WATER TREATMENT | WARREN | OH |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID |
---|---|---|---|---|
2201875 | 2013-09-05 | Beaver | New Sewickley Twp | No Violations Noted |
2205409 | 2013-09-18 | Beaver | New Sewickley Twp | No Violations Noted |
2206056 | 2013-09-11 | Beaver | New Sewickley Twp | No Violations Noted |
2206058 | 2013-09-18 | Beaver | New Sewickley Twp | No Violations Noted |
2212252 | 2013-10-08 | Beaver | New Sewickley Twp | No Violations Noted |
2213881 | 2013-10-16 | Beaver | New Sewickley Twp | No Violations Noted |
2223187 | 2013-11-14 | Beaver | New Sewickley Twp | No Violations Noted |
2227170 | 2013-11-25 | Beaver | New Sewickley Twp | No Violations Noted |
2227173 | 2013-12-05 | Beaver | New Sewickley Twp | No Violations Noted |
2231780 | 2013-12-11 | Beaver | New Sewickley Twp | No Violations Noted |
2232278 | 2013-10-10 | Beaver | New Sewickley Twp | No Violations Noted |
2232813 | 2013-11-05 | Beaver | New Sewickley Twp | No Violations Noted |
2232823 | 2013-11-12 | Beaver | New Sewickley Twp | No Violations Noted |
2236882 | 2014-01-13 | No Violations Noted | This well targets the Geneseo Shale formation. The inspection for this well was conducted concurrently with the inspection for site number 768793 (inspection report # 2236823.) Two minor slips were noted on pad's embankments. Crews were erecting equipment in preparation for stimulation operations. An above ground storage tank (AST) was being erected. Inspector confirmed with operator's representative that it would be used for flow back fluids. Operator's representative agreed to provide a copy of the OG-71 for the AST. | |
2247357 | 2014-01-02 | No Violations Noted | the site is being prepared for pressure test and frac.
the site isok. |
|
2247360 | 2014-01-14 | No Violations Noted | WELL IS BEING TESTED AS PART OF THE STIMULUS PROCESS.
THE PAD IS IN GOOD CONDITION. |
|
2251836 | 2014-02-11 | No Violations Noted | WELL IS DRILLED. RIG IS GONE. SNOW REMOVAL IS THE ONLY ACTIVITY. |