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Well ID: 37-115-20728 | Loading map...
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County: Susquehanna | |
Municipality: Dimock Township | |
Operator Name: CABOT OIL & GAS CORP | |
Well Pad ID: 148519 | |
Farm/Lease Name: R HESS 5 | |
First Permit Date: 2011-11-18 | |
Last Permit Date: 2011-11-18 | |
Spud Date: 2012-02-06 | |
Unconventional: Yes | |
Horizontal: Yes | |
Producing: Yes | |
Violations: None | |
Latitude: 41.759452 | |
Longitude: -75.868772 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID |
---|---|---|---|---|
2047097 | 2012-02-28 | No Violations Noted | H&P 290. At 2820' while drilling on air encountered @4000 units of gas. Initially killed well with mud. Tried drilling out on fluid, then lost circulation and continued to get gas. Set 2 - 500' cement plugs and capped well. Skidded over to Hess 2H well. Currently no pressure on 5H well. At this time no plans made to continue on this well. | |
2047100 | 2012-02-29 | No Violations Noted | Follow up on Well pressure on well. Well has been capped due to high pressure encountered while drilling on air at @ 2800'. Two cement plugs have been set to seal off gas. There are three gauges on the capped well. All three are showing no pressure at this time. | |
2065316 | 2012-05-01 | No Violations Noted | H&P 290. Tripping in hole now to resume drilling lateral. Had previously hit large gas due to fracture encountered at 2820'. At that time set two (2) 500' cement plugs and moved off hole to drill other wells on pad. Drilled offset of cement plugs to avoid fracture. Company Man indicated that some mud loss was observed at same depth (2820'), but no gas kick occurred this time mainly because this time drilling on fluid. TD proposed is @ 13,300'. 7" casing was set at 3317' with 44.1 bbls cement. FIT run @ 3317' at 1121 psi on 8.5 ppg = 15 ppg EMW. Drillers log on site and up to date. |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2012-2 | 2164063.57 | 162.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2012-1 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-2 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|---|---|---|---|---|---|---|---|
2012-2 | FRACING FLUID WASTE | 6474.74 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE FOR HYDRAULIC FRACTURING | |||
2012-2 | PRODUCED FLUID | 3472.01 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE FOR HYDRAULIC FRACTURING | |||
2012-2 | FRACING FLUID WASTE | 1674.74 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123NE001 | SOMERSET REG WATER/SUSQ BENEFICIAL REUSE FAC | SPRINGVILLE | PA |
2012-2 | PRODUCED FLUID | 59.36 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123NE001 | SOMERSET REG WATER/SUSQ BENEFICIAL REUSE FAC | SPRINGVILLE | PA |
2012-2 | BASIC SEDIMENT | 33.93 | Bbl | LANDFILL | THR029 | TUNNELL HILL RECLAMATION LANDFILL | NEWLEXINGTON | OH |
2012-2 | FLOWBACK FRACTURING SAND | 7.73 | Tons | LANDFILL | THR029 | TUNNELL HILL RECLAMATION LANDFILL | NEWLEXINGTON | OH |
2012-2 | FLOWBACK FRACTURING SAND | 0.51 | Tons | LANDFILL | 101534 | WASTE MANAGEMENT, INC - LAUREL HIGHLANDS LANDFILL | JOHNSTOWN | PA |
2012-2 | FLOWBACK FRACTURING SAND | 6.31 | Tons | LANDFILL | 100081 | WASTE MANAGEMENT, INC - SOUTHERN ALLEGHENIES | DAVIDSVILLE | PA |
2012-1 | DRILL CUTTINGS | 555.58 | Tons | LANDFILL | NY STATE #32S11 | ALLIED WASTE SYSTEMS | NIAGARA FALLS | NY |
2012-1 | DRILLING FLUID WASTE | 373.33 | Bbl | LANDFILL | NY STATE #32S11 | ALLIED WASTE SYSTEMS | NIAGARA FALLS | NY |
2012-1 | FLOWBACK FRACTURING SAND | 16.21 | Tons | LANDFILL | 100945 | CUMBERLAND COUNTY LANDFILL | NEWBURG | PA |
2012-1 | FLOWBACK FRACTURING SAND | 4.0 | Tons | LANDFILL | 101571 | MOSTOLLER LANDFILL | SOMERSET | PA |
2012-1 | DRILLING FLUID WASTE | 371.25 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE FOR HYDRAULIC FRACTURING | |||
2012-1 | FRACING FLUID WASTE | 3212.01 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE FOR HYDRAULIC FRACTURING | |||
2012-1 | DRILL CUTTINGS | 904.23 | Tons | LANDFILL | THR029 | TUNNELL HILL RECLAMATION LANDFILL | NEWLEXINGTON | OH |
2012-1 | DRILLING FLUID WASTE | 785.04 | Bbl | LANDFILL | THR029 | TUNNELL HILL RECLAMATION LANDFILL | NEWLEXINGTON | OH |
2012-1 | DRILLING FLUID WASTE | 5.45 | Bbl | LANDFILL | 101534 | WASTE MANAGEMENT, INC - LAUREL HIGHLANDS LANDFILL | JOHNSTOWN | PA |
2012-1 | FLOWBACK FRACTURING SAND | 8.81 | Tons | LANDFILL | 101534 | WASTE MANAGEMENT, INC - LAUREL HIGHLANDS LANDFILL | JOHNSTOWN | PA |
2012-1 | DRILLING FLUID WASTE | 4.67 | Bbl | LANDFILL | 100081 | WASTE MANAGEMENT, INC - SOUTHERN ALLEGHENIES | DAVIDSVILLE | PA |