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37-115-20206

Well Details

Well ID: 42-115-20206
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County: Susquehanna
Municipality: Rush Township
Operator Name: WPX ENERGY APPALACHIA LLC
Well Pad ID: 144832
Farm/Lease Name: KNOSKY 1H
First Permit Date: 2010-01-19
Last Permit Date: 2010-01-19
Spud Date: 2010-03-20
Unconventional: Yes
Horizontal: Yes
Producing: Yes
Violations: 6
Latitude: 41.826332
Longitude: -76.063324

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID
1852639 2009-11-17 No Violations Noted
1965917 2011-04-15 No Violations Noted Well is shut in. Well is not online. Inspected well head. Observed intermittent bubbling around base of well head. A gauge on a 2" vent showed 0 psi. Gauge is 10000 lb ga. Cellar is filled with gravel with a small amount of standing water present. Rahole is ocvered with metal plate. Crew on site cleaning out mud tanks and solidifying waste for T&D. Secondary containment in place under work area.
1968298 2011-04-13 Violation(s) Noted 609524
1968298 2011-04-13 Violation(s) Noted 609525
1969017 2011-04-27 Violation(s) Noted 609751
1969017 2011-04-27 Violation(s) Noted 609752
1969017 2011-04-27 Violation(s) Noted 609753
1969017 2011-04-27 Violation(s) Noted 609754
1971000 2011-04-29 Outstanding Violations - No Viols Req'd
1977581 2011-06-01 No Violations Noted
2019858 2011-11-08 No Violations Noted
2029534 2011-12-21 Pending DEP on site 9:30. Production crews on site. Frac tanks on site and appear to be empty. Tanks being moved off location during insepction. Ryan Klemish (DEP-WQS) observed bubbling around well head during previous inspection. Confirmed minor bubbling around well head during this inspection. Was raining heavily during inspection, pooled water present around well head. Request Operator to report to DEP the cause of the leak and correct problem.

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2012-2 741753.79 182.0 0.0 0.0 0.0 0.0
2012-1 1148660.0 176.0 0.0 0.0 0.0 0.0
2011-2 3202.0 2.0 0.0 0.0 0.0 0.0
2011-1 0.0 0.0 0.0 0.0 0.0 0.0
2010-2 0.0 0.0 0.0 0.0 0.0 0.0
2010-3 0.0 0.0 0.0 0.0 0.0 0.0

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2010-2 DRILLING FLUID WASTE 571.4 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PAR000519462 ADVANCED WASTE SERVICES OF PA (NEW CASTLE) NEW CASTLE PA
2010-2 DRILLING FLUID WASTE 1171.4 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0008451 SUNBURY GENERATION WASTE WATER TRMT FAC SHAMOKIN DAM PA
2011-1 DRILLING FLUID WASTE 714.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0101508 PA BRINE TRT INC - FRANKLIN PLT - VENANGO CO FRANKLIN PA
2011-2 DRILLING FLUID WASTE 129.9 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PAD014286009 ARMSTRONG ENVIRONMENTAL SERVICES LANCASTER PA
2012-1 DRILLING FLUID WASTE 68.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR123NC006 CLEAN STREAMS, LLC WILLIAMSPORT PA

References