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Well ID: 37-063-25419 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Indiana | |
Municipality: Green Township | |
Operator Name: ALLIANCE PETROLEUM CO LLC | |
Well Pad ID: | |
Farm/Lease Name: GERMAINE LENZ 2C630 | |
License Status: Active | |
Spud Date: 03/03/1981 | |
Permit Date: 3/18/1980 | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Latitude: 40.722974 | |
Longitude: -78.991615 |
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1996 | PENTEX ENERGY INC | 544.00 | 365 | 0.00 | 0.00 | ||
1997 | PENTEX ENERGY INC | 230.00 | 365 | 0.00 | 0.00 | ||
1998 | PENTEX ENERGY INC | 316.00 | 365 | 0.00 | 0.00 | ||
1999 | PENTEX ENERGY INC | 331.00 | 365 | 0.00 | 0.00 | ||
2000 | PENTEX ENERGY INC | 429.00 | 236 | 0.00 | 0.00 | ||
2001 | 0.00 | 0.00 | 0.00 | ||||
2002 | 0.00 | 0.00 | 0.00 | ||||
2003 | 0.00 | 0.00 | 0.00 | ||||
2004 | 0.00 | 0.00 | 0.00 | ||||
2005 | 0.00 | 0.00 | 0.00 | ||||
2006 | LINN OPR INC | 206.00 | 365 | 0.00 | 0.00 | ||
2007 | LINN OPR INC | 320.00 | 365 | 0.00 | 0.00 | ||
2008 | XTO ENERGY INC | 655.00 | 365 | 0.00 | 0.00 | ||
2009 | 0.00 | 0.00 | 0.00 | ||||
2010 | 0.00 | 0.00 | 0.00 | ||||
2011 | XTO ENERGY INC | 133.00 | 365 | 0.00 | 0.00 | ||
2012 | XTO ENERGY INC | 148.00 | 186 | 0.00 | 0.00 | ||
2013 | XTO ENERGY INC | 68.00 | 180 | 0.00 | 0.00 | ||
2014 | 0.00 | 0.00 | 0.00 | ||||
2015 | 0.00 | 0.00 | 0.00 | ||||
2016 | XTO ENERGY INC | 132.85 | 346 | 0.00 | 0.00 | ||
2017 | ALLIANCE PETROLEUM CO LLC | 42.00 | 334 | 0.00 | 0.00 | ||
2018 | 0.00 | 0.00 | 0.00 |
For data sources see[4]
Period | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|
1996-0 | Brine | 20.00 Bbl | Injection Disposal Well | 063-20246 |
1999-0 | Brine | 25.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0095443 |
2005-0 | Brine | 25.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0095273 |
2006-0 | Brine | 80.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0095273 |
2013-0 | Produced Fluid (in Barrels) | 15.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2580796 | Primary Facility | 2017-04-10 | Routine/Complete Inspection | No Violations Noted | At time of inspection, well appears equipped for production. Well tag present, legible. No brine tank on-site.
When standing on access road facing meter box, Department observed rapid bubbling in puddle of water located to right of meter box where pipeline enters ground. Faint gas odor observed. Forwarded to Environmental Group Manager for follow-up as appropriate. |
2580919 | Primary Facility | 2017-04-10 | Routine/Complete Inspection | No Violations Noted | Responded to small line leak from this well. Contacted operator who is responding to fix leak. Well tagged-in production. Annulus shut. Well head casing-meter run looked ok. |
For data sources see[6]