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Well ID: 37-063-24065 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Indiana | |
Municipality: Washington Township | |
Operator Name: ALLIANCE PETROLEUM CO LLC | |
Well Pad ID: | |
Farm/Lease Name: DAVID L CARNAHAN ET UX 1 | |
License Status: Active | |
Spud Date: 03/12/1978 | |
Permit Date: 1/13/1978 | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Latitude: 40.728530 | |
Longitude: -79.207896 |
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1993 | PHILLIPS PROD CO | 9,395.00 | 365 | 0.00 | 0.00 | ||
1994 | PHILLIPS PROD CO | 8,658.00 | 365 | 0.00 | 0.00 | ||
1995 | PHILLIPS PROD CO | 4,045.00 | 120 | 0.00 | 0.00 | ||
1996 | PHILLIPS PROD CO | 8,815.00 | 365 | 0.00 | 0.00 | ||
1997 | PHILLIPS PROD CO | 6,923.00 | 365 | 0.00 | 0.00 | ||
1998 | PHILLIPS PROD CO | 5,093.00 | 234 | 0.00 | 0.00 | ||
1999 | PHILLIPS PROD CO | 6,798.00 | 305 | 0.00 | 0.00 | ||
2000 | PHILLIPS PROD CO | 4,161.00 | 293 | 0.00 | 0.00 | ||
2001 | PHILLIPS PROD CO | 5,424.00 | 335 | 0.00 | 0.00 | ||
2002 | PHILLIPS PROD CO | 6,012.00 | 365 | 0.00 | 0.00 | ||
2003 | PHILLIPS PROD CO | 5,666.00 | 365 | 0.00 | 0.00 | ||
2004 | PHILLIPS PROD CO | 6,888.00 | 366 | 0.00 | 0.00 | ||
2005 | PHILLIPS PROD CO | 5,256.00 | 365 | 0.00 | 0.00 | ||
2006 | PHILLIPS PROD CO | 6,248.00 | 365 | 0.00 | 0.00 | ||
2007 | PHILLIPS PROD CO | 5,089.00 | 365 | 0.00 | 0.00 | ||
2008 | PHILLIPS PROD CO | 5,859.00 | 366 | 0.00 | 0.00 | ||
2009 | PHILLIPS PROD CO | 5,495.00 | 365 | 0.00 | 0.00 | ||
2010 | PHILLIPS PROD CO | 5,068.00 | 365 | 0.00 | 0.00 | ||
2011 | PHILLIPS PROD CO | 4,175.00 | 352 | 0.00 | 0.00 | ||
2012 | XTO ENERGY INC | 5,216.00 | 366 | 0.00 | 0.00 | ||
2013 | XTO ENERGY INC | 3,160.00 | 365 | 0.00 | 0.00 | ||
2014 | XTO ENERGY INC | 3,234.00 | 351 | 0.00 | 0.00 | ||
2015 | XTO ENERGY INC | 4,313.00 | 365 | 0.00 | 0.00 | ||
2016 | XTO ENERGY INC | 3,611.00 | 366 | 0.00 | 0.00 | ||
2017 | ALLIANCE PETROLEUM CO LLC | 2,630.00 | 334 | 0.00 | 0.00 | ||
2018 | ALLIANCE PETROLEUM CO LLC | 3,252.00 | 365 | 0.00 | 0.00 |
For data sources see[4]
Period | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|
2003-0 | Brine | 0.00 Bbl | Brine or Industrial Waste Treatment Plt | |
2009-0 | Brine | 50.00 Bbl | Brine or Industrial Waste Treatment Plt | |
2014-0 | Produced Fluid (in Barrels) | 156.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
2014-0 | Produced Fluid (in Barrels) | 70.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095443 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2238846 | Primary Facility | 01/22/2014 | Incident- Response to Accident or Event | In Compliance with Policy | Admin inspt. Operator representatives Jason Canose and Matt Streams notified Department at approximately 1150 via phone of water leaking out from between the conductor and casing of a conventional well. Water appears to be tinted orange with a flow rate calculated to be approximately 2 gal/hr. |
2240937 | Primary Facility | 01/29/2014 | Routine/Complete Inspection | No Violations Noted | |
2241490 | Primary Facility | 01/22/2014 | Routine/Complete Inspection | Pending | Opeartaor reports a fluid discharge from well: No discharge at time of inspection. Gas present at conductor surface annulus. operator to sample fluids and determine source of gas. |
2242593 | Primary Facility | 02/03/2014 | Administrative/File Review | In Compliance with Policy | Admin inspt as follow-up to inspt record 2238846 in which fluids reported to be leaking out from between the conductor and casing of a conventional well. |
2248177 | Primary Facility | 02/20/2014 | Routine/Complete Inspection | No Violations Noted | |
2248641 | Primary Facility | 02/20/2014 | Routine/Partial Inspection | No Violations Noted | RTPT inspt as follow-up to inspt record 2238846 in which fluids reported to be leaking out from between the conductor and casing of a conventional well. |
2248645 | Primary Facility | 02/20/2014 | Administrative/File Review | In Compliance with Policy | Conference call held between OGI Rick Hoover, WQS Samantha Foulk, and XTO reps Jason Canose and Mike West as requested by Opr in response to inspt record 2238846 in which fluids reported to be leaking out from between the conductor and casing of a conventional well.Opr and Dept discussed possible scenarios as to why gas and fluids are being discharged from the 11 ¾” X 8 5/8” annulus.Operator intends to monitor annular gas for two weeks. Monitor will identify gas and record levels of each type (i.e. CO2, methane, etc.). Mr. West stated records of surrounding wells were inspected and no abnormalities were observed. Mr. West also stated that well tender checks well every day and no fluids were reported to be discharged over the weekend. Department informed Operator that fluids were being discharged today (inspt record 2248641).Operator agreed to collect isotopic samples of gas. Mutual decision between Operator and Department to wait for results of fluid samples (inspt record 2248641) to be received before developing and implementing an action plan. |
2266846 | Primary Facility | 04/22/2014 | Routine/Complete Inspection | In Compliance with Policy | On-site meeting requested by Operator as follow-up to inspt record 2238846 in which fluids reported to be leaking out from between the conductor and casing of a conventional well. |
2282543 | Primary Facility | 06/24/2014 | Routine/Complete Inspection | No Violations Noted | |
2292055 | Primary Facility | 07/23/2014 | Routine/Complete Inspection | No Violations Noted |
For data sources see[6]