X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

37-005-27384

Well Details

Well ID: 37-005-27384
Loading map...
Country: United States
State: Pennsylvania
County: Armstrong
Municipality: Kittanning Township
Operator Name: KRIEBEL WELLS DISSOLUTION CO LLC
Well Pad ID:
Farm/Lease Name: ALTMEYER LAWTHER 2
License Status: Active
Spud Date: 01/31/2004
Permit Date: 10/10/2003
Unconventional Well: N
Configuration: Vertical Well
Latitude: 40.757516
Longitude: -79.397578

For data sources see[1][2][3]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2004 EDWARD G KRIEBEL GAS CO 7,958.00 246 0.00 0.00
2005 KRIEBEL MINERALS INC 9,738.00 345 0.00 0.00
2006 KRIEBEL MINERALS INC 6,654.00 346 30.00 346 0.00
2007 KRIEBEL MINERALS INC 3,186.00 365 0.00 0.00
2008 KRIEBEL MINERALS INC 7,603.00 349 0.00 0.00
2009 KRIEBEL MINERALS INC 4,226.00 332 0.00 0.00
2010 KRIEBEL MINERALS INC 4,630.00 365 0.00 0.00
2011 KRIEBEL MINERALS INC 3,444.00 334 0.00 0.00
2012 KRIEBEL MINERALS INC 3,108.00 333 0.00 0.00
2013 KRIEBEL MINERALS INC 2,844.00 324 0.00 0.00
2014 KRIEBEL MINERALS INC 2,325.00 321 0.00 0.00
2015 KRIEBEL MINERALS INC 2,339.00 318 0.00 0.00
2016 KRIEBEL MINERALS INC 2,164.00 328 0.00 0.00
2017 KRIEBEL WELLS DISSOLUTION CO LLC 1,767.00 320 0.00 0.00
2018 KRIEBEL WELLS DISSOLUTION CO LLC 1,899.00 322 0.00 0.00

For data sources see[4]

Waste Data

Period Waste Type Quantity Disposal Method Waste Facility ID
2004-0 Fracking Fluid 340.00 Bbl Other
2004-0 Fracking Fluid 820.00 Bbl Other PA0095443

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1274096 Primary Facility 09/24/2003 Routine/Complete Inspection No Violations Noted well staked - site not made/waiver review ok
1330301 Primary Facility 04/13/2004 Complaint Inspection No Violations Noted Responded due to smell of gas. 4.5 and 1.5 production strings. Other equip: separator, meter run, 100 bbl tank. Pits reclaimed.
1369272 Primary Facility 08/10/2004 Routine/Complete Inspection No Violations Noted Well producing. ES ok, Vegetation ok. Site reclaimed.

For data sources see[6]

References