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37-015-20282

Well Details

Well ID: 37-015-20282
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County: Bradford
Municipality: Monroe Township
Operator Name: CHIEF OIL & GAS LLC
Well Pad ID:
Farm/Lease Name: ELLIOT UNIT 1H
First Permit Date: 2009-05-19
Last Permit Date: 2010-05-14
Spud Date:
Unconventional: Yes
Configuration: Horizontal
Well Status: ACTIVE
Violations: 0
Latitude: 41.714325
Longitude: -76.422633

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2010-3 0.0 0.0 0.0 0.0 0.0 0.0
2009-0 0.0 0.0 0.0 0.0 0.0 0.0
2010-2 0.0 0.0 0.0 0.0 0.0 0.0
2010-2 0.0 0.0 0.0 0.0 0.0 0.0
2011-1 0.0 0.0 0.0 0.0 0.0 0.0
2011-2 0.0 0.0 0.0 0.0 0.0 0.0
2009-0 0.0 0.0 0.0 0.0 0.0 0.0
2010-3 0.0 0.0 0.0 0.0 0.0 0.0
2010-2 0.0 0.0 0.0 0.0 0.0 0.0
2011-1 0.0 0.0 0.0 0.0 0.0 0.0
2011-2 0.0 0.0 0.0 0.0 0.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
2199488 2013-08-14 No Violations Noted NOMAC 44, Comp. Man - Roy Funck, at 7833'.

Gas shows: 481'MD =204 units,1153' =118 units, 5508' = 115 u, 6080' = 209 u. Tully @ 5508', Hamilton @ 5608', U. Marc. @ 7550' 20" @ 69' 13 3/8" @ 726' w/ 780 sx, 15.6 ppg Prem H cement w/ 42 bbls of 15.3 ppg cement to surf. Pkr (inflat) @ 410' 9 5/8" @ 1998' w/ 840 sx, 15.6 ppg Prem H w/ 27 bbls good 15.6 cement to surf. frac pkr @ 1071' (top) Waiting on Cement. Lost piece of motor in hole so set a plug from 7820 - 7100'. Will do a side track.

Site looks good.

For data sources see[2]

References