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34-119-28610

Well Details

Well ID: 34-119-28610
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County: Muskingum
Municipality:
Operator Name: ENERVEST OPERATING L
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2007-04-23
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 40.11592034
Longitude: -81.95057365

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2007-0 6592.0 295.0
2008-0 976.0 314.0
2009-0 906.0 242.0
2010-0 664.0 334.0
2011-0 258.0 91.0
2012-0 0.0 0.0
2013-0 0.0 0.0
2014-0 0.0 0.0 0.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
119739994 2011-01-14 The well is not producing. Last years production shows that the well made a lot of brine some oil and not much gas. Produce or plug
1366823323 2013-04-24 This is a follow up to NOV # 119739994. Well is on plugging list and I have permit in hand. Tanks and pumping unit have been removed.
1393434470 2014-02-26 Chipco is setting Bottom plug thru 1.5tubing. They ran in to depth of 5949'. They will set plug from 5949-5549. Set a 30 sack plug with Class A cement. The well circulated.
1393564448 2014-02-27 Chipco is setting a rip/Clinton plug. They ripped at 4470'. Chipco pumped an 80 barrel load of 10lb per gallon brine down. The well did not circulate but it was blowing on backside. After the pump shut down well went on vacume. The truck went to get 2nd load of brine water. The decision was made to pull up to the bottom of the clinton and set the clinton and rip plug together. Rig pulled casing to 3878 and then Chipco set a 400'cement plug. The plug was set from 3878'-3478'. After the displacing down the rig could not pull the pipe. The rig shut down and will tag in morning.
1393600894 2014-02-28 Chipco ran tools in hole and tagged cement at 3200'. They then ripped pipe at 3100'. They pulled 8 joints at 42'per joint. The Big Lime plug will be set at 2750-2450'. Ran 86 sacks at the Lime. Bottom of 8.625plug is at 1250-1050' with 60 sacks of class A ran. 200-0' there were 60 sacks of class A cement ran.
1393958706 2014-02-28 Well was plugged by Chipco for Enervest resolving the Compliance Notice on 2-28-14 by Patrick Shreve.
1394025722 2014-02-24 Chipco is running in 2.375upset tubing with tools and they can not get past 2000'. They decided to pull tubing and run in with 1.5 tubing and spot bottom plug tomarrow.
1399912941 2014-05-12 Final Restoration passed on 5-12-14 by Patrick Shreve.
1700450860 2011-01-14 FOLLOW UP TO NOV # 119739994 The well is not producing. Last years production shows that the well made a lot of brine some oil and not much gas. Produce or plug
1903438060 2007-06-12 Reclamation in progress. Tanks set and well in producing
407919772 2011-04-18 Moving big rig off and smaller rig on to swab. Big water from Black River.
-412085943 2013-04-10 Per Request on the status of the well. Well is not in compliance with 1509. Waiting on Enervest to Plug well. Plug Permit in hand.
74215975 2008-11-13 there is now a pump jack on this well. Pumping. No problems noted.
954656162 2007-06-27 Final grade, seeded and mulching in progress. Looks good.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.