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Well ID: 34-133-23979 | Loading map...
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County: Portage | |
Municipality: | |
Operator Name: PIPES PURSIE E | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1993-09-08 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Producing | |
Violations: 0 | |
Latitude: 41.00833983 | |
Longitude: -81.22355432 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1994-0 | 13789.0 | 11593.0 | ||||
1995-0 | 12840.0 | 7969.0 | ||||
1996-0 | 8059.0 | 4033.0 | ||||
1997-0 | 6463.0 | 2216.0 | ||||
1998-0 | 5446.0 | 1414.0 | ||||
1999-0 | 4804.0 | 1204.0 | ||||
2000-0 | 3530.0 | 895.0 | ||||
2001-0 | 1916.0 | 491.0 | ||||
2002-0 | 3361.0 | 288.0 | ||||
2003-0 | 5259.0 | 815.0 | ||||
2004-0 | 3602.0 | 461.0 | ||||
2005-0 | 4611.0 | 256.0 | ||||
2006-0 | 2944.0 | 310.0 | ||||
2007-0 | 2723.0 | 293.0 | ||||
2008-0 | 2790.0 | 247.0 | ||||
2009-0 | 2247.0 | 224.0 | ||||
2010-0 | 2264.0 | 304.0 | ||||
2011-0 | 2134.0 | 193.0 | ||||
2012-0 | 2158.0 | 189.0 | ||||
2013-0 | 2332.0 | 200.0 | ||||
2014-0 | 908.0 | 365.0 | 72.0 | 365.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1393523208 | 2014-02-14 | Status check inspection of this Rose Run well. I found Chipco's service rig at the wellhead and rigged down. The rig operator was on location with the rig hands. I inspected the wellhead and it appeared that the 4.5 casing was bent. I asked the rig operator what happened and he told me that the brakes were frozen on the rig and when they broke free, the rig bumped into the wellhead. They had finished running new rods into the tubing yesterday. Nothing was leaking at the wellhead and Mark Smith (PEP) was on his way to location to determine what repairs would be necessary. I inspected the tank battery to the east and found that it was diked and contained 2-210 barrel tanks and a horizontal separator. The proper ID was posted at the tank battery and wellhead. I will check back later on repairing the wellhead. No violations. | ||||
17179152 | 2002-05-16 | Random status check on tank battery. NO VIOLATIONS. |
For data sources see[2]