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34-119-26474

Well Details

Well ID: 34-119-26474
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County: Muskingum
Municipality:
Operator Name: ATLAS NOBLE LLC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1983-01-20
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 39.81532815
Longitude: -81.76504667

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 12652.0 2616.0
1985-0 9077.0 1401.0
1986-0 11468.0 1386.0
1987-0 11505.0 1366.0
1988-0 6576.0 765.0
1989-0 2328.0 293.0
1990-0 5483.0 413.0
1991-0 4850.0 379.0
1992-0 4797.0 338.0
1993-0 5702.0 360.0
1994-0 4340.0 350.0
1995-0 3893.0 331.0
1996-0 3457.0 295.0
1997-0 3047.0 362.0
1998-0 2870.0 292.0
1999-0 2400.0 312.0
2000-0 2217.0 183.0
2001-0 1391.0 287.0
2002-0 2087.0 256.0
2003-0 1823.0 183.0
2004-0 1342.0 317.0
2005-0 1527.0 213.0
2006-0 1463.0 192.0
2007-0 1356.0 184.0
2008-0 1868.0 261.0
2009-0 1537.0 242.0
2010-0 1427.0 161.0
2011-0 1518.0 212.0
2012-0 1197.0 83.0
2013-0 1584.0 220.0
2014-0 1083.0 365.0 98.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1345122878 2012-08-10 Dave Ball called at 7:00am on tank struck by lighting on evening of 8-9-12.Mark Warehiem called him at 11:30 on 8-9-12. The Fire Department had killed the fire with a foam mix. The tank was still hot from night before. Upon inspection Atlas was pulling oil out the dike and retrieved top of 210 barrel tank from 150'down over the hill. Nothing as such as contamination left the dike. Atlas would keep on with clean up and tank removal and replacement.
1393182951 2012-08-15 Atlas had cleaned up contamination and replaced 210 barrel tank with a 100 barrel tank. The dike has been reinstalled and site is in compliance.
1647621359 2003-10-22
-1979630509 2009-07-28 Producing, no problems noted.
-227766336 2012-02-10 On day of inspection well is supplied with a pumping unit and a 210 barrel tank.No violations noted.
328644944 2007-11-01 Well is producing. No problems noted
PL8476 Preliminary Restoration done information from Data Point

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.