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34-119-28154

Well Details

Well ID: 34-119-28154
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County: Muskingum
Municipality:
Operator Name: BAKERWELL INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1997-12-04
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 39.90806343
Longitude: -82.1605935

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1998-0 69094.0 166.0
2000-0 35187.0 212.0
2001-0 17413.0 960.0
2002-0 584.0 243.0
2003-0 49.0 602.0
2005-0 0.0 313.0
2006-0 0.0 155.0
2007-0 0.0 0.0
2008-0 0.0 0.0
2009-0 0.0 67.0
2010-0 0.0 32.0
2011-0 0.0 25.0
2012-0 0.0 0.0
2013-0 0.0 0.0
2014-0 0.0 365.0 0.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1396529921 2014-04-02 Baker well shot pipe off at 4370' with Appalachain wirline. The joints are 44' long. They are dragging and the rig is pulling 80,000lbs. The pipe weighs 15.5lb/ft so the string weight would be 67,735lbs. Hooked Formation to string and pumped on casing. There was 800 psi on fluid pressure. They pulled 6 joints after getting pipe moving. From 4106-3906' set a Trenton plug. Pulled up to the Clinton plug and shut down. No circulation at this point.
1396623836 2014-04-03 Bakerwell pulled 5.5casing up to 3468' to set Clinton plug. The plug was at 3468-3257'. The cement plug was set with class A cement and 2% CaCl with Cotton seed hulls. There was no circulation. The decision was made to pull all casing and run tubing after tagging cement top.
1396762631 2014-04-01 Setting Bottom plug on well. Bakerwell is running 2.375upset 8 round tubing. Formation is going to pump the cement plug at 5474'. There is 100' of 4.875open hole and 5.5casing is at 5336'. Formation pumped 60 sacks of regular class A cement. Plug was set at 5474'-5074'. There was good circulation.
1396888533 2014-04-07 The 2.375upset tubing was ran to depth of 2466'. The Big Lime was set from 2466-2266'. The bottom of the Surface was set at 1114-914' with 52 sacks ran of 2% gelled cement. Then tubing was pulled up to 350' where the plug was set at fluid level. From 350-150' set plug and ran 50 sacks of class A cement @ 2% gelled cement. The rig was instructed to pull all tubing out and then a bridge plug was set at 250'. Then set top plug of 96 sacks of regular class A cement. Well did not drop back.
1399229674 2014-04-08 Well was plugged and stopped in to check and see if cement dropped back. The plug was at top.
-1489090163 2014-04-04 Baker well was running tools in to tag cement plug. Set down was at 2970'. The plug could have had cave in on top of plug. Rig was running 2.375tubing at 2466' for the lime plug.
-318137109 2014-08-13 Final Restoration passed on 8-13-14 by Patrick Shreve.
iDIAN001014 1999-05-03

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.