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Well ID: 37-115-21140 | Loading map...
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County: Susquehanna | |
Municipality: New Milford Township | |
Operator Name: SOUTHWESTERN ENERGY PROD CO | |
Well Pad ID: 144552 | |
Farm/Lease Name: FOLGER 2H | |
First Permit Date: 2013-02-04 | |
Last Permit Date: 2013-02-04 | |
Spud Date: 2011-11-23 | |
Unconventional: Yes | |
Horizontal: Yes | |
Well Status: ACTIVE | |
Violations: 3 | |
Latitude: 41.827636 | |
Longitude: -75.742419 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2013-1 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2013-2 | 568986.0 | 122.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2014-1 | 832345.0 | 178.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2014-2 | 683680.0 | 184.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2015-02 | 87260.0 | 28.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2015-01 | 105783.0 | 31.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2015-03 | 90565.0 | 31.0 | 0.0 | 0.0 | 0.0 | 0.0 |
For data sources see[1]
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|---|---|---|---|---|---|---|---|
2013-1 | DRILL CUTTINGS | 607.53 | Tons | LANDFILL | 101247 | KEYSTONE SANITARY LANDFILL | DUNMORE | PA |
2013-1 | FRACING FLUID WASTE | 3.0 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE WITHOUT PROCESSING AT A PERMITTED FACILITY | |||
2013-2 | DRILL CUTTINGS | 26.53 | Tons | LANDFILL | 101247 | KEYSTONE SANITARY LANDFILL | DUNMORE | PA |
2013-2 | FRACING FLUID WASTE | 5.0 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE WITHOUT PROCESSING AT A PERMITTED FACILITY | |||
2013-2 | PRODUCED FLUID | 3.0 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE WITHOUT PROCESSING AT A PERMITTED FACILITY | |||
2014-1 | PRODUCED FLUID | 469.0 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE WITHOUT PROCESSING AT A PERMITTED FACILITY | |||
2014-2 | PRODUCED FLUID | 38.0 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE WITHOUT PROCESSING AT A PERMITTED FACILITY |
For data sources see[2]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
---|---|---|---|---|---|---|
2152521 | 2013-03-29 | No Violations Noted | ||||
2173999 | 2013-05-07 | No Violations Noted | 20-76'
13 3/8 - 642' - damp at 152' (595 sacks, 22 bbls returned) 9 5/8 - 1636 - 652 sacks, 33 blls returned) Reentered at 6185 KO - 5920' ETD - 10849' BOPs tested 4/14/13 |
|||
2208531 | 2013-09-24 | Violation(s) Noted | On 9/24/13 at 11:05 AM SWN contacted the Department to report a release of approximately 105 gallons of ethylene glycol to the pad surface of the SWN RU 32 Folger Pad. Reported cause of release was a production equipment problem. Arrived on-site at approximately 12:30 PM. Mike Deming was on-site and explained that a well tender had identified the spill while responding to an automatic shut in of the Folger 2H (permit # 115-21140). The production unit which services the 2H had malfunctioned and overheated causing the fluid loss to the pad surface under the unit. The equipment failure caused the well and unit to automatically shut down. Equipment is being brought in to begin the cleanup of the spill. Explained to Mike that this case would probably be referred to the Departmentï¾’s EC&B Program. | 679315 | 402CSL - Failure to adopt pollution prevention measures required or prescribed by DEP by handling materials that create a danger of pollution. | Spill of 120 gallons ethylene glycol to well pad surface |
2208531 | 2013-09-24 | Violation(s) Noted | On 9/24/13 at 11:05 AM SWN contacted the Department to report a release of approximately 105 gallons of ethylene glycol to the pad surface of the SWN RU 32 Folger Pad. Reported cause of release was a production equipment problem. Arrived on-site at approximately 12:30 PM. Mike Deming was on-site and explained that a well tender had identified the spill while responding to an automatic shut in of the Folger 2H (permit # 115-21140). The production unit which services the 2H had malfunctioned and overheated causing the fluid loss to the pad surface under the unit. The equipment failure caused the well and unit to automatically shut down. Equipment is being brought in to begin the cleanup of the spill. Explained to Mike that this case would probably be referred to the Departmentï¾’s EC&B Program. | 682088 | SWMA301 - Failure to properly store, transport, process or dispose of a residual waste. | SWMA 6018.610 Ethylene glycol was allowed to impact the surface of the ground |
2208531 | 2013-09-24 | Violation(s) Noted | On 9/24/13 at 11:05 AM SWN contacted the Department to report a release of approximately 105 gallons of ethylene glycol to the pad surface of the SWN RU 32 Folger Pad. Reported cause of release was a production equipment problem. Arrived on-site at approximately 12:30 PM. Mike Deming was on-site and explained that a well tender had identified the spill while responding to an automatic shut in of the Folger 2H (permit # 115-21140). The production unit which services the 2H had malfunctioned and overheated causing the fluid loss to the pad surface under the unit. The equipment failure caused the well and unit to automatically shut down. Equipment is being brought in to begin the cleanup of the spill. Explained to Mike that this case would probably be referred to the Departmentï¾’s EC&B Program. | 682090 | 91.34A - Failure to take all necessary measures to prevent spill. Inadequate diking, potential pollution | Spill of 120 gallons ethylene glycol to well pad surface |
2208798 | 2013-09-24 | No Violations Noted | Refer to inspection ID # 2208782 | |||
2359312 | 2015-04-07 | No Violations Noted |
For data sources see[3]