X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

37-131-20023

Well Details

Well ID: 37-131-20023
Loading map...
County: Wyoming
Municipality: Mehoopany Township
Operator Name: CHESAPEAKE APPALACHIA LLC
Well Pad ID: 147921
Farm/Lease Name: CAPPUCCI 2H
First Permit Date: 2009-12-17
Last Permit Date: 2009-12-17
Spud Date: 2010-03-09
Unconventional: Yes
Horizontal: Yes
Well Status: ACTIVE
Violations: 4
Latitude: 41.565636
Longitude: -76.101008

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2010-3 0.0 0.0 0.0 0.0 0.0 0.0
2010-2 0.0 0.0 0.0 0.0 0.0 0.0
2010-2 0.0 0.0 0.0 0.0 0.0 0.0
2011-1 0.0 0.0 0.0 0.0 0.0 0.0
2011-2 0.0 0.0 0.0 0.0 0.0 0.0
2012-1 0.0 0.0 0.0 0.0 0.0 0.0
2012-2 0.0 0.0 0.0 0.0 0.0 0.0
2013-1 48166.0 4.0 0.0 0.0 0.0 0.0
2013-2 1745231.0 184.0 0.0 0.0 0.0 0.0
2014-1 1158212.0 181.0 0.0 0.0 0.0 0.0
2014-2 505732.0 150.0 0.0 0.0 0.0 0.0
2015-02 25167.0 13.0 0.0 0.0 0.0 0.0
2015-01 3836.0 3.0 0.0 0.0 0.0 0.0
2015-03 109152.0 17.0 0.0 0.0 0.0 0.0

For data sources see[1]

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2012-1 DRILL CUTTINGS 35.18 Tons LANDFILL THR029 TUNNELL HILL RECLAMATION LANDFILL NEWLEXINGTON OH
2012-1 PRODUCED FLUID 17.33 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING
2012-2 PRODUCED FLUID 353.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING
2013-2 FRACING FLUID WASTE 27.0 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123NC008 SHARER TEMP CENTRALIZED FLUIDS PROCESSING FACILITY PA
2013-2 PRODUCED FLUID 109.0 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR0123 HYDRO RECOVERY LP BLOSSBURG FACILITY BLOSSBURG PA
2013-2 PRODUCED FLUID 2.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE WITHOUT PROCESSING AT A PERMITTED FACILITY
2014-1 PRODUCED FLUID 659.12 Bbl REUSE OTHER THAN ROAD SPREADING REUSE WITHOUT PROCESSING AT A PERMITTED FACILITY
2014-2 FLOWBACK FRACTURING SAND 17.0 Tons LANDFILL 301626 WHITE PINES LANDFILL MILLVILLE PA
2014-2 FRACING FLUID WASTE 70.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE WITHOUT PROCESSING AT A PERMITTED FACILITY
2014-2 FRACING FLUID WASTE 33.33 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123NC008 SHARER TEMP CENTRALIZED FLUIDS PROCESSING FACILITY PA
2014-2 PRODUCED FLUID 103.45 Bbl REUSE OTHER THAN ROAD SPREADING REUSE WITHOUT PROCESSING AT A PERMITTED FACILITY

For data sources see[2]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
1856583 2010-01-15 Violation(s) Noted No E&S Plan available for review, Some BMPs not installed correctly, need waiver for encroachment on man made wetland 579642 102.4NOPLAN - No E&S plan developed, plan not on site See Insp ID 1861838.
1856583 2010-01-15 Violation(s) Noted No E&S Plan available for review, Some BMPs not installed correctly, need waiver for encroachment on man made wetland 579643 102.4 - Failure to minimize accelerated erosion, implement E&S plan, maintain E&S controls. Failure to stabilize site until total site restoration under OGA Sec 206(c)(d) See Insp ID 1861838.
1856583 2010-01-15 Violation(s) Noted No E&S Plan available for review, Some BMPs not installed correctly, need waiver for encroachment on man made wetland 579644 601.101 - O&G Act 223-General. Used only when a specific O&G Act code cannot be used 601.205(b) - See Insp ID 1861838.
1861838 2010-02-08 No Violations Noted RWE-insp result initially entered as DVN, 10:20 AM insp found minor 102.4 viols, follow-up 2:10 PM insp found 102.4 viols corrected, wetland encroachment waiver ultimately granted 02/24/2010, all past viols noted in 01/15/2010 3rd page NOV, Enf ID 255434, resolved.

MBC 02/25/2010

1872341 2010-03-25 De minimus Violations Noted
1873064 2010-03-25 Viol(s) Noted & Immediately Corrected Drillers log not filled out. Company Man indicated he has geologst on site logging hole and will have him fill out the drillers log and keep it up to date as drilling continues. Violation was immediately corrected. 584088 78.122 - Drillers Log not on site
1940135 2010-12-14 No Violations Noted Some frac sand on location not posing any environmental threat. All guages on casing sting annuli read 0. 9 5/8" annulus vented open.
1944365 2011-01-04 No Violations Noted Well completed. No pressure on annuli guages.
1949995 2011-02-15 No Violations Noted The Department received a complaint on 2/14/11 regarding unusual activity at the site. The complaintant reported seeing vacuum trucks and workers on the site involved in cleanup activities. The site has been drilled and fracked. I inspected the site and although there was no activity, it was determined that the vehicles were removing the water from the cellars. Nothing unusual. No violations noted.
1958418 2011-03-18 No Violations Noted Cellar full of water, gas meter reading in vent of what we think is 13 5/8" annulus is 0.5
1969963 2011-05-03 No Violations Noted
1990498 2011-07-13 Pending Bubbles in cellar of 2H. See video.
1990503 2011-07-19 Pending Cellar has water. Bubbles observed.

Kevin Costello accompanied me.

1991558 2011-07-28 Pending Bubbling is inside conductor, 1 bubble every 5 sec.

Chesapeake guy was on site to fix signs(permit #) He covered mousehole, after he fell in. Well was fraced.

1993345 2011-08-03 Pending Entrance sign and well tag corrected.

Mouse hole covered with grating. Still bubbling inside 20" conductor.

1993356 2011-07-25 Pending Still bubbling - conductor - surf annulus, a little water in cellar.

131-2-223 wrong on sign, should be 131-20023

1995753 2011-08-15 Pending Checking on bubbling - in cond-surf annulus. Still bubbling, see video.
1999480 2011-08-30 No Violations Noted Cellar full of water, no bubbles observed.
2003601 2011-09-19 Pending Some water inside conductor, minor bubbles. (see video)
2106028 2012-10-04 No Violations Noted Well pad has lots of water, about 6" around wells. A surf - cond cap has been installed, with a vent, but couldn't get near due to water.
2207272 2013-09-23 No Violations Noted Comp Man - Jeff Baker

Crews on site changing out wellhead, master valve cut out. Using 10000 psi wellhead instead of 5000 psi due to higher then usual pressure, 4000+. They like a 20% safety factor.

2209770 2013-09-26 No Violations Noted crew that was changing well head has moved off site. All 3 wells are back on line. Tbg press is 2166 psi. Noise level is much lower than several weeks ago. Well tag has incorrect permit number.
2341157 2015-02-04 No Violations Noted

For data sources see[3]

References