X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-105-23719

Well Details

Well ID: 34-105-23719
Loading map...
County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2013-06-24
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 39.1559155301
Longitude: -81.9549796951

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1148815463 2013-06-24 Begin drilling operations today. Pit lined, blowline being laid out.
-617236392 2013-06-26 Witnessed the surface casing integrity pressure test. After multiple attempts, the surface casing was able to hold the required pressure for the 30 minute test period. Test pressure began at 410 psi and after 30 minutes was at 370 psi.
-71952199 2013-06-25 Witnessed 815' of used 7" 20 lb/ft surface casing set in 840' of 8 3/4" bore hole with 165 sacks of Class A neat cement with 3% CaCl-.Good returns stayed at the surface.
-867821130 2013-08-22 Requirements met for 2 month preliminary. Pits closed and there is no drilling equipment on site. There is a service rig on site and 5 frac tanks, 4 of which are full of water and one is half full.
1163522763 2013-06-26 Annular disposal mechanical integrity test (fresh water test) 815' of 7" casing cemented with 165 sacks. Tested at 445 psi for 15 minutes, at 15 minutes 428 psi. Multiple tests failed prior to passing due to faulty test equipment at the surface. Test equipment was replaced and the test passed.
1371822913 2013-06-21 Building location and excavating pit. Pit = 39.15582 -81.95575.
1373637291 2013-07-12 Upon review of the Cement Bond Log provided by the company it was determined the 4 1/2" production casing did not have the required 500 feet of coverage above the perforations. The completion of the well was halted and a remedial perf and squeeze job will be scheduled.
1387467570 2013-12-19 Annular disposal inspection. The 2" steel lines from the 100 Barrel salt water tank have been laid above ground and are welded at each union. System is water tight.
1764903433 2013-07-16 Service rig on well with 550 gallon poly tank to swab Acid into. Six frac tanks on site.
604610180 2013-06-24 98' feet of used , tested, 9 5/8" conductor set in 118' of 12.25" bore hole with 55 sacks of class A cement with 1% gel and 2% CaCl-. Good returns seen at the surface.