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34-115-23289

Well Details

Well ID: 34-115-23289
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1983-11-04
Unconventional:
Horizontal:
Producing: No
Violations: 4
Latitude: 39.6767403872
Longitude: -81.9527355173

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1262131398 2014-03-21 Compliance Action Follow-up -1940659686: I met with Andy and he has repaired and cleaned up the separator. The well is still idle and without electric line. He will try to get power to the well and get it back in production in the next few months.
-1940659686 2013-08-19 I was here to inspect the wells on this property at the landowner's request. I arrived to location with the well tender and he and the landowner both stated that the well has not produced in over a year and there is no electric running to the well location. The well has some contamination around base of wellhead due to leaking stuffing box. The well shares a tank battery up at top of the road and the separator is leaking crude. Operator must clean up contamination at the wellhead and separator, repair faulty equipment, and make well capable of production within 60 days; or plugging is required in 60 days. 9-1-07
-1940659686 2013-08-19 I was here to inspect the wells on this property at the landowner's request. I arrived to location with the well tender and he and the landowner both stated that the well has not produced in over a year and there is no electric running to the well location. The well has some contamination around base of wellhead due to leaking stuffing box. The well shares a tank battery up at top of the road and the separator is leaking crude. Operator must clean up contamination at the wellhead and separator, repair faulty equipment, and make well capable of production within 60 days; or plugging is required in 60 days. 9-9-05(A)8
-1940659686 2013-08-19 I was here to inspect the wells on this property at the landowner's request. I arrived to location with the well tender and he and the landowner both stated that the well has not produced in over a year and there is no electric running to the well location. The well has some contamination around base of wellhead due to leaking stuffing box. The well shares a tank battery up at top of the road and the separator is leaking crude. Operator must clean up contamination at the wellhead and separator, repair faulty equipment, and make well capable of production within 60 days; or plugging is required in 60 days. NONE
-1940659686 2013-08-19 I was here to inspect the wells on this property at the landowner's request. I arrived to location with the well tender and he and the landowner both stated that the well has not produced in over a year and there is no electric running to the well location. The well has some contamination around base of wellhead due to leaking stuffing box. The well shares a tank battery up at top of the road and the separator is leaking crude. Operator must clean up contamination at the wellhead and separator, repair faulty equipment, and make well capable of production within 60 days; or plugging is required in 60 days. NONE_
-674076898 2014-03-28 Andy called and stated he and the landowner are going to work on finding where the issues is with the buried electric line. Once that is resolved they can get well back in production.
1236478628 2009-03-06 Inspection revealed that well is equipped with pumping unit and 4.5" production casing and 1.5" tubing&rods and fluids are being stored in1-210 bbl tank shared with other wells on lease,there is a some old oil staining around wellhead will contact owner and request cleanup needed.
130240831 2013-12-09 Compliance Action Follow-up -1940659686: Andy Corp put some gravel down on at the base of the separator, however he still needs to cleanup the contamination.
1378610760 2013-10-21 Compliance Action Follow-up -1940659686: There has been no resolution to any of the issues.
1384276450 2013-11-12 Compliance Action Follow-up -1940659686: There has been no resolution to any of the issues. I called the field supervisor Rusty Hudson and left a message regarding the multiple well issues in this area.
1404920484 2014-07-09 Compliance Action Follow-up -1940659686: The well was pumping when I arrived on location. The landowner was present and stated that the well was tied into the meter with all of the others wells on the property. The well is in compliance.
PL9676 Preliminary Restoration done information from Data Point