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34-163-20541

Well Details

Well ID: 34-163-20541
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1981-04-01
Unconventional:
Horizontal:
Producing: No
Violations: 10
Latitude: 39.2345668457
Longitude: -82.3005655318

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1250754855 2004-07-29 No violations
-1269715938 2008-05-27 No violations were noted.
-13004891 2013-11-04 Inspected containment dike, tank, injection pump, injection line, annulus pressure, and injection pressure. Dike has 1.5" of water in it. Injection pump was off during the inspection. Identification posted on pole at the wellhead.
-1381752913 2010-03-22 An inspection revealed no violations at this time.
-1492189815 2009-09-01 An inspection was conducted with Mr. Jeff Fry, West Region Oil & Gas Supervisor and UIC Field Supervisor. No violations were noted.
-1492604096 2005-01-12 No violations.
-1675343980 2007-04-18 An inspection revealed that new identification and a 1/4" fitting would be needed on the injection side of the well. The dike is also leaking and will need repaired. An old tank within this dike will need replaced. The bottom of the tank appears to be corroded and leaking. Mr. Mike Merkle was contacted by telephone on 4/18/2007. Mr. Merkle came to the well site and was informed of the inspection results. 9-3-05(B)4
-1675343980 2007-04-18 An inspection revealed that new identification and a 1/4" fitting would be needed on the injection side of the well. The dike is also leaking and will need repaired. An old tank within this dike will need replaced. The bottom of the tank appears to be corroded and leaking. Mr. Mike Merkle was contacted by telephone on 4/18/2007. Mr. Merkle came to the well site and was informed of the inspection results. 9-3-08(A)
-1797409874 2012-06-14 There was 1.5-2 inches of fluid in the containment dike. Spoke with Mr. Manfred Merkle on site. He stated that he had plans to clean the inside of the dike anyway.
-1801521637 2003-01-30 No violations at this time.
-1974122974 2010-06-30 An inspection revealed no violations.
-2121330170 2010-12-30 An inspection revealed no violations at this time.
-228903759 2012-08-30 No violations noted at the time of inspection.
-320857302 2012-10-24 Good identification. Dike has 1.5" of brine in it. Used filters are being stored in two 5 gallon plastic buckets outside the dike. The buckets are full of fluid and running onto the ground ( less than 1 foot area is affected.) I called Progressive's office and informed them that they need to remove the old filters and dispose of them at a EPA approved landfill. We also discussed the brine in the dike. I told them to pump the brine into the steel tank. 9-3-05(A)6
-3406513 2007-06-26 An inspection revealed that the SWIW is in-compliance. The previously noted violations have been resolved.
-390102769 2010-09-23 An inspection revealed no violations. Note: The gauge utilized for this inspection will require calibration.
-482560998 2011-11-02 Used filters are being stored in a bucket out side of the dike.
-4930297 2003-07-02 No violations.
-594636375 2013-02-28 Inspected containment dike, injection pressure and annulus pressure. Accompanied by Kip Thompson MRI 2. Well owner was on site. We discussed the new requirements for pumping any water or fluids with-in the dike into a tank (inside the containment dike) and injecting the water into the injection well along with the brine. The identification was faded (still legible). We discussed the need for a legible identification.
-65661266 2007-04-26 A follow-up inspection revealed all violations resolved except dike repair and leaking tank.
-683431403 2003-05-08 No violations.
101772717 2013-09-10 Inspected the containment dike, tank, injection line, annulus pressure, and injection pressure. Containment dike is free of water.
1099894840 2011-08-04 No violations observed during inspection.
1118665306 2005-06-08 No violations.
1153713329 2006-07-12 An inspection was conducted at the facility owned by Progressive Oil & Gas on 7/12/2006. During the inspection, it was noted that the dike will need to be pumped. Also noted was that the oily soil surrounding this dike will need to be addressed. On 7/12/2006, Mr. Mike Merkle was verbally instructed of the deficiencies found during the inspection. 9-3-05(A)6
1219663166 2007-11-01 No violations were noted.
1260366593 2009-12-09 An inspection revealed no violations. Since the last inspection, Progressive Oil & Gas has performed preventative maintenance, on the concrete dike placed around the tank battery. Block sealer has been applied to the concrete blocks. Note: The battery consists of one (1) 210 bbl tank. No violations were noted.
1267844711 2006-01-25 No violations, will need tested in spring.
1269i1233 2002-07-23 No violations, injection pressure meets requirements.
1269i12451159 2001-03-29 Follow - up on NOV , In - Complaince
1269i15 2001-01-18 An inspection of the well revealed that the ID at the well says C&V Minerals , not the owner listed to the state. 1/4" valves need replaced on the injection and annulus of the well , unable to check well pressure. Filters and trash on and around well site needs cleaned up and hauled away from lease . 9-3-04(A)
1269i15 2001-01-18 An inspection of the well revealed that the ID at the well says C&V Minerals , not the owner listed to the state. 1/4" valves need replaced on the injection and annulus of the well , unable to check well pressure. Filters and trash on and around well site needs cleaned up and hauled away from lease . 9-3-05(A)3
1269i848 2002-03-06 No violations at this time.
1305057378 2009-03-02 An inspection revealed no violations at this time.
1352480607 2012-11-08 Dike is free of brine. Used filters have been removed from the location. Checked injection pressure and annulus pressure.
1374603667 2013-07-19 Inspected annulus pressure, injection pressure, containment dike, tank, and pump. Dike was free of water. Identification is posted. A drip between the check valve and the tee in the injection line was observed. I called Progressive and they are going to repair or replace the fittings by the 7-21-13.
1390788243 2008-02-11 No violations were noted.
1393433995 2014-02-26 Inspected containment dike, tank, annulus pressure and injection pressure. Identification posted at well site. Containment dike is free of water.
1400690461 2014-05-21 Inspected the containment dike, tank, injection pump, injection line, annulus pressure, and injection pressure. Good identification posted on pole at well site.
1550 2002-11-21 No violations at this time, lease rd will need graded and water breaks in spring.
1716022546 2004-03-04 No violations.
1773472902 2013-01-25 I accompanied Andy Thomas on the inspection of this well.
1882752934 2013-01-24 No violations are noted at this facility. The containment dike is free of fluid, good identification is posted, there is no pollution and contamination, and the pressures on the annulus and injection tubing are good.
1893765181 2006-09-21 A follow-up inspection was conducted at the facility owned by Progressive Oil & Gas on 9/21/2006. During the inspection, it was noted that the previously noted violations have been resolved.
1903548016 2011-11-02 Accompanied Jon Scott on inspection.
196054277 2007-01-11 An inspection conducted on 1/11/2007 revealed that a new 1/4" fitting would be needed along with new identification at the well head. 9-3-05(B)4
2133905839 2004-05-26 No vioaltions.
21414306 2004-01-15 No violations.
303017307 2014-06-25 Inspected the containment dike, tank, injection pump, injection line, annulus pressure and injection pressure. Identification posted on pole at well site.
330030537 2011-03-29 No violations at this time.
385119974 2008-09-16 No violations were noted.
53551075 2007-01-11 An inspection conducted on 1/11/2007 revealed that a new 1/4" fitting would be needed along with new identification at the well head. 9-3-05(A)3
56019552 2009-06-12 An inspection revealed no violations at this time.
5609i208 2001-06-01 No violations at this time.
602621653 2003-10-30 No violations
611310419 2008-12-10 An inspection revealed no violations at this time.
iTOMK000107 2001-01-18 9-3-04(A)
iTOMK000107 2001-01-18 9-3-05(A)3