X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-087-60133

Well Details

Well ID: 34-087-60133
Loading map...
County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1933-08-05
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 38.4429814121
Longitude: -82.4503250594

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1241894683 2011-09-28 Casing has not been cut off below grade. Pit is open and full of water. Steel tank is on location. Took photos. I called Chip Smith and he told me that they are coming back to area next week and will reclaim site.
-1293785019 2011-03-14 Showed Chipco rig where the well was located.
-1915949146 2011-03-21 Cut 3" head and welded 3" pup joint. Tried to pull 3" with 30,000 lbs. 3" is not free. Welder cut off 14" that connected to 6 5/8". This revealed the 10" casing. 6 5/8" annulus inside 10" has cement in top. (no record as to how much) 3" was pulled again to 20,000 lbs and the casing jumped.
-2056080761 2011-12-19 Pit has been filled in. Casing cut off. Site graded. Tank removed. Seed and mulch applied. Vegetative growth is established in spots (new growth). Gas line and meter set are owned by Ohio River Gas Delivery LTD.
-864078268 2011-03-25 1800' 3" retrieved. 6 5/8" hit obstruction at 57'. Cannot run jars past 57'. Casing is open to 1200' with 4" tools. Plan on finishing plug job with clay.
1020420552 2004-11-19 RBMS coordinates are a bit off.
1151128153 2011-03-18 1950' of 1.5" tubing ran inside 3" casing. 3" perfed at 1952' with 15 shots. 3" casing cut at 1800'. 600' cement plug figured for 6 5/8" hole. 3" tubing has open valve. Pump to clear tubing with water (no water to surface). Pump cement through tubing. No fluid to surface. Displacement 5 bbls. Pulled tubing.
1306939429 2011-05-10 No LEL's recorded at well casing. No bubbles in water surrounding well casing. Pit is open with water in it. Small steel tank is on location. Clay inside casing is at the surface. Photos were taken. I called Justin Smith and left message to cut off casing and to close the pit. Restore location.
1309964047 2011-03-15 Chipco is rigged up. They are waiting on a sub joint to try and pull the packer.
1435852483 2011-03-29 Inspector witnessed approximately 200 feet of a prepared clay plug washed into hole.
1568942776 2011-03-17 2041' of 1.5" tubing recovered (release packer attached) Appalachian wire line ran bond log on 3" casing. Wire line set down at 1952'. 15 shots to perf for cement job. Casing cutter in 3" at 1800' (3" packer at 1880')
1678095178 2009-04-23 Talked to Chip Smith (well owner) today at 9:42 am. We discussed the Idle well violations on his wells. He took over the wells to plug them for salvage. Chip told me that he is working a deal with North Coast Energy to plug some of their wells also. He plans to start plugging as soon as it dries out. I told chip that I had not seen any plug permits issued for his wells. He said that the permits will be filled with in a week.