X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-151-25700

Well Details

Well ID: 34-151-25700
Loading map...
County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2010-11-09
Unconventional:
Horizontal:
Producing: No
Violations: 1
Latitude: 40.9221768885
Longitude: -81.2373098389

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-467860966 2010-11-08 PEP Drilling is moving onto the location this morning.
-644809362 2010-10-28 Pyramid Pipeline is building the access road today. PEP Drilling will be moving in on 11-1-10.
1109809909 2010-11-15 Dusting at 2200'. The water level in the drilling pit is pumped down and the pit liner that slipped down will be repaired today.
1288041287 2010-10-22 Located drilling access road.
1288189259 2010-10-26 I walked the access route and located the well stake. Pep Drilling will be moving in on the location in the next 2 or 3 days.
1288719110 2010-11-02 The drilling location has been rocked. The drilling rig has not arrived on the location.
1289328087 2010-11-09 The drilling pits are being dug this morning. PEP Drilling will spud this afternoon.
1290106139 2010-11-18 Drilling at 4800'. Soaping thru the Clinton sandstone.
1290803808 2010-11-24 Reached T.D. 7556'. Ran and cemented 4-1/2 dia casing.
1307376191 2011-06-03 The Uniontown office received a complaint in February 2011 from Jim Pastore regarding a drop in the water level in the lake on his property. Jim believes that the drop in the lake level is associated with the drilling and cementing operations conducted at the Schnase # 3 oil and gas well. The complaint was discussed on 2-16-2011 in the Uniontown office with Barry Lay (EnerVest), Rick Simmers (ODNR), Kyle Tharp (ODNR) and myself. Due to the flooding conditions at the wellhead, I was unable to gain access until 6-3-2011. I inspected the well constuction with Joe Bolinger (EnerVest) and Ron (Alborn Excavating). We excavated around the wellhead and checked the 4 dia shut off valves located on the annulus between the 16" dia casing and the 11-3/4 dia casing. These valves were used to cement off the artesian aquifer during drilling operations. The valves were found in the closed position. The west side valve could not be opened. The cementing nipple from the squeeze job to seal off the artesian flow was still screwed into the valve. The east side valve could be opened. There was no pressure on the valve and less than 1 quart of water trickled from the valve. The valve was left open and observed for 30 minutes. No pressure, no gurgling, and no flow was observed. All three of us agreed that there was no evidence of any aquifer flow observed. The excavated valves were placed in the closed position and buried.
1307471824 2011-06-03 The drilling pits are closed and the well is in production. The location has been rough graded. Due to the flooding conditions on the site, the previously stacked sills and timbers are now scattered over the location. Remove all the timbers, sills, and debris from the location. Spread the stockpiled topsoil, grade, seed, and mulch the site. I did not pass the Preliminary Restoration at this time. NONE5
1311021172 2011-07-18 The well is in production and the site is reclaimed in agricultural crops. The Preliminary Restoration is PASSED.
1457993706 2010-12-20 The drilling pits are closed.
1907102502 2012-01-06 On 1/6/2912, I performed a status check on the above well site. The well is in production, the site is reclaimed and identification signs are posted. The Preliminary Inspection is PASSED.
1986462821 2011-07-18 The Compliance Notice to restore the site is RESOLVED.