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34-111-24468

Well Details

Well ID: 34-111-24468
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2014-05-02
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 39.7074446322
Longitude: -81.2499136648

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
1399314709 2014-05-05 The said well was spudded on 05/02/2014 by Zigenfoose Inc top hole rig with 100' of 24 conductor being set with no annular space, on this day I found the current drilling depth to be 440' using a 22.875 diameter drill bit in the surface borehole well bore section with a projected total depth to be drilled of 500'. I shall GPS the well head when we cement the surface pipe.
1399572318 2014-05-08 On 05/08/2014 494' of 20 .375 well surface pipe was set and cemented to surface by Baker Hughes cement services using 507 sacks of class A 2% calcium .25 pound per sack cement, the mix water was tested and showed no chlorides above 250 parts per million, with good cement returns to surface. Due to restrictions within the working area of the rig mast the cement head would not fit and no wiper plug was ran, the casing shall be pressure tested at a later time.