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34-121-23592

Well Details

Well ID: 34-121-23592
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2013-04-01
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 39.7352602414
Longitude: -81.5773496593

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1074882612 2012-05-23 Inspection of the well head found 8.625 surface casing and the well producing off the 4.5 production casing with a current gas chart in meter and a single 210 barrel tank on site with proper well identification.
-1997801092 2014-07-31 My inspection finds the well is equipped with a pumping unit that is in operation at the time of inspection. The tank battery is comprised of one 210 barrel tank, one 100 barrel tank, and a separator set in a dike.
1852248906 2013-04-03 Northwood Energy ran tubing to a depth of 5700'. Cemenco set a 35 sk. plug and displaced it with 20 bbl of salt water.
2022235467 2013-04-05 The rig crew ripped the casing at 4200'. Material from the back side of the casing caused the tools to be stuck. The wire line parted at the top of the tools. The rig crew is trying to fish the tools with 2" tubing.
770527832 2013-04-15 I am on site to witness the casing cementing. Cemenco cemented 2565' of used 4.5" casing in place with 220 sks of class A Lafarge cement.
PL7337 Preliminary Restoration done information from Data Point