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Well ID: 34-055-21690 | Loading map...
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County: | |
Municipality: | |
Operator Name: | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1992-07-23 | |
Unconventional: | |
Horizontal: | |
Producing: No | |
Violations: 0 | |
Latitude: 41.5330042763 | |
Longitude: -81.3113252253 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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-1924858220 | 2014-07-07 | I am on location today in reference to complaint #4741. My inspection found the well to be equipped with a plunger lift unit. The annulus valve is plumbed above ground and is closed. The demco valve on the wellhead is leaking and needs repaired. The well and tank battery are surrounded by a locked chain link fence. The tank battery consists of a 210 BBL production tank, a 25 BBL poly brine tank, and a mechanical separator. The proper identification is located on the tank battery. The lease road is in stable condition. I have contacted Bruce Close a supervisor for Alliance Petroleum about replacing the valve on the wellhead and having the annulus plumbed up to a guage to monitor the pressure. | ||||
-2064574967 | 2014-08-13 | My inspection found the demco valve has been repaired. The annulus valve is plumbed up and there is no pressure on the annulus. No other changes to the location since my last inspection. | ||||
1408451914 | 2014-08-18 | I was on location at the request of DNR Hydrologist Kyle Tharp. My inspection found the well was currently in production. The annulus valve is plumbed up and has zero pressure on it. The valves on the wellhead have been repaired. No other changes to the location since my last inspection. No violations found. | ||||
1859 | PASSED Y WITNESSED 6/3/93 INSPECTOR HAROLD MORAVY DATE 06/0319/93 DATA FROM OLD VAX INFO |