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34-121-21939

Well Details

Well ID: 34-121-21939
County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date:
Unconventional:
Horizontal:
Producing:
Violations:
Latitude:
Longitude:

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1278567587 2014-08-04 My inspection finds the well is equipped with 4.5" casing and 1.5" tubing. The tubing has a large hole at the top of the 4.5" by 1.5" wellhead. The casing appears to have partially collapsed at the top of the surface casing head.
-1990508827 2006-11-06 Plug back permit expired 8/30/06 will call company and discuss future plans for well at present time well is setting idle!
-223774724 2013-11-06 My inspection today finds the well is equipped with 4.5" casing and 1.5" tubing. The tubing has a rotted off at the top of the well head. A significant amount of gas is leaking from the tubing. A production unit is present off site but is not hooked up. The well is not capable of production.
1097896989 2014-02-25 My inspection finds the well is equipped with 4.5" casing and 1.5" tubing. The tubing has a large hole in it at the top of the 4.5" by 1.5" wellhead. Gas can be heard leaking. The casing appears to have partially collapsed at the top of the 8" and is beginning to lean. A production unit is present off site. There is no tank for this well. The company reported gas production for the well in 2012, as well as 72 bbl of brine. Previous inspections have indicated the well is not capable of production. I called and left a message for John Snyder to call me to discuss this well at 12:06 pm.
1259784279 2009-10-21 Inspected site along with supervisor and determined that well is idle and incapable of producing in its present state of repair,it is equipped with 8' surface casing and 4.5' production casing and 1.5' tubing which has hole in it at tubing head,the last production reported was back in 1998 and I have had several conversations with company rep requesting that they plug or produce said well. 9-9-05(A)10
1259784279 2009-10-21 Inspected site along with supervisor and determined that well is idle and incapable of producing in its present state of repair,it is equipped with 8' surface casing and 4.5' production casing and 1.5' tubing which has hole in it at tubing head,the last production reported was back in 1998 and I have had several conversations with company rep requesting that they plug or produce said well. NONE
1834179882 2013-07-11 I called and spoke to Mr. John Snyder. I told him that the plug back permit for the well would be expiring soon and that something needed to be done with the well. Mr. Snyder stated that he intended to begin work on the well in the next two months weather permitting.
2129607595 2014-02-28 I called Mr. John Snyder of Stonebridge Operating at 11:17 am. I discussed the outstanding violations against the well with Mr. Snyder. Mr. Snyder stated that he was planning to get a permit to plug the well. He also stated that the proper identification would be in place by 3/7/14.