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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 37-081-21370 | | Well ID: 37-081-21370 | ||
− | | style="height=100%; align=center" rowspan=" | + | | style="height=100%; align=center" rowspan="15" | {{#display_map: 41.379572, -77.122619 | width=100% | height=100% }} |
|- | |- | ||
| Country: United States | | Country: United States | ||
Line 21: | Line 21: | ||
| License Status: Active | | License Status: Active | ||
|- | |- | ||
− | | Spud Date: 03 | + | | Spud Date: 2014-03-27 |
|- | |- | ||
− | | Permit Date: 12 | + | | Permit Date: 2013-12-03 |
|- | |- | ||
| Unconventional Well: Y | | Unconventional Well: Y | ||
Line 49: | Line 49: | ||
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
| accessdate = 2019-05-21 }}</ref> | | accessdate = 2019-05-21 }}</ref> | ||
+ | == Fracking Activities == | ||
+ | ==== Fracking Jobs ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Job Number | ||
+ | !scope="col" | Job Start Date | ||
+ | !scope="col" | Job End Date | ||
+ | !scope="col" | True Vertical Depth (ft) | ||
+ | !scope="col" | Total Water Volume (gal) | ||
+ | !scope="col" | Total Non-Water Volume (gal) | ||
+ | |- | ||
+ | | 1 | ||
+ | | 2014-05-31 | ||
+ | | 2014-06-04 | ||
+ | | style="text-align: right;" | 9079 | ||
+ | | style="text-align: right;" | 1,560,600.0 | ||
+ | | style="text-align: right;" | | ||
+ | |- | ||
+ | |} | ||
+ | ==== Fluid Composition Data ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Job Number | ||
+ | !scope="col" | Trade Name | ||
+ | !scope="col" | Supplier | ||
+ | !scope="col" | Purpose | ||
+ | !scope="col" | Ingredient Name | ||
+ | !scope="col" | CAS Number | ||
+ | !scope="col" | Additive Percentage by Mass | ||
+ | !scope="col" | Job Percentage by Mass | ||
+ | !scope="col" | Mass Used (lb) | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="11"| 1 | ||
+ | | rowspan="3"| WFR-65LA | ||
+ | | rowspan="3"| Weatherford | ||
+ | | rowspan="3"| Friction Reducer | ||
+ | | Petroleum Distillates | ||
+ | | 64742-47-8 | ||
+ | | style="text-align: right;" | 40 | ||
+ | | style="text-align: right;" | 0.0533 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | Water | ||
+ | | 7732-18-5 | ||
+ | | style="text-align: right;" | 55 | ||
+ | | style="text-align: right;" | 0.0732 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | Ammonium Acetate | ||
+ | | 631-61-8 | ||
+ | | style="text-align: right;" | 5 | ||
+ | | style="text-align: right;" | 0.0067 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="1"| MX 588-2 | ||
+ | | rowspan="1"| MultiChem | ||
+ | | rowspan="1"| Scale Inhibitor | ||
+ | | MX 588-2 | ||
+ | | NA | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0.0209 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="1"| MC MX 8-2544 | ||
+ | | rowspan="1"| MultiChem | ||
+ | | rowspan="1"| Antibacterial | ||
+ | | MC MX 8-2544 | ||
+ | | NA | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0.0105 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="1"| Water | ||
+ | | rowspan="1"| Range Resources | ||
+ | | rowspan="1"| Base/Carrier Fluid | ||
+ | | Water | ||
+ | | 7732-18-5 | ||
+ | | style="text-align: right;" | 100 | ||
+ | | style="text-align: right;" | 87.4847 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="2"| 35% HCL | ||
+ | | rowspan="2"| Weatherford | ||
+ | | rowspan="2"| Cleans perforations | ||
+ | | Hydrochloric Acid | ||
+ | | 7647-01-0 | ||
+ | | style="text-align: right;" | 35 | ||
+ | | style="text-align: right;" | 0.1319 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | Water | ||
+ | | 7732-18-5 | ||
+ | | style="text-align: right;" | 65 | ||
+ | | style="text-align: right;" | 0.245 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="2"| MX 5-2402 | ||
+ | | rowspan="2"| MultiChem | ||
+ | | rowspan="2"| Bacterial Nutritional Supplement | ||
+ | | Sodium Nitrate | ||
+ | | 7631-99-4 | ||
+ | | style="text-align: right;" | 40 | ||
+ | | style="text-align: right;" | 0.0512 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | Water | ||
+ | | 7732-18-5 | ||
+ | | style="text-align: right;" | 60 | ||
+ | | style="text-align: right;" | 0.0767 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="1"| Sand | ||
+ | | rowspan="1"| Weatherford | ||
+ | | rowspan="1"| Fracture Proppant | ||
+ | | Crystalline Silica | ||
+ | | 14808-60-7 | ||
+ | | style="text-align: right;" | 100 | ||
+ | | style="text-align: right;" | 11.8458 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title =FracFocus Fracking Chemicals Database | ||
+ | | date = 2019-04-02 | ||
+ | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-06-19 }}</ref> | ||
== Production Data == | == Production Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 268: | Line 399: | ||
| 2277742 | | 2277742 | ||
| Primary Facility | | Primary Facility | ||
− | | 06 | + | | 2014-06-06 |
| Incident- Response to Accident or Event | | Incident- Response to Accident or Event | ||
| Viol(s) Noted & Immediately Corrected | | Viol(s) Noted & Immediately Corrected | ||
Line 330: | Line 461: | ||
| 697954 | | 697954 | ||
| 06/06/2014 | | 06/06/2014 | ||
− | | 06 | + | | 2014-06-06 |
| 402CSL - Failure to adopt pollution prevention measures required or prescribed by DEP by handling materials that create a danger of pollution. | | 402CSL - Failure to adopt pollution prevention measures required or prescribed by DEP by handling materials that create a danger of pollution. | ||
| Environmental Health & Safety | | Environmental Health & Safety | ||
Line 338: | Line 469: | ||
| 697955 | | 697955 | ||
| 06/06/2014 | | 06/06/2014 | ||
− | | 06 | + | | 2014-06-06 |
| 78.54* - Failure to properly control or dispose of industrial or residual waste to prevent pollution of the waters of the Commonwealth. | | 78.54* - Failure to properly control or dispose of industrial or residual waste to prevent pollution of the waters of the Commonwealth. | ||
| Environmental Health & Safety | | Environmental Health & Safety | ||
Line 346: | Line 477: | ||
| 697956 | | 697956 | ||
| 06/06/2014 | | 06/06/2014 | ||
− | | 06 | + | | 2014-06-06 |
| SWMA301 - Failure to properly store, transport, process or dispose of a residual waste. | | SWMA301 - Failure to properly store, transport, process or dispose of a residual waste. | ||
| Environmental Health & Safety | | Environmental Health & Safety | ||
Line 370: | Line 501: | ||
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
| accessdate = 2019-05-21 }}</ref> | | accessdate = 2019-05-21 }}</ref> | ||
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==References== | ==References== | ||
<references/> | <references/> |
Well ID: 37-081-21370 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Lycoming | |
Municipality: Cogan House Township | |
Operator Name: RANGE RESOURCES APPALACHIA LLC | |
Well Pad ID: 146349 | |
Farm/Lease Name: NULL BOBST UNIT 5H | |
License Status: Active | |
Spud Date: 2014-03-27 | |
Permit Date: 2013-12-03 | |
Unconventional Well: Y | |
Configuration: Horizontal Well | |
Latitude: 41.379572 | |
Longitude: -77.122619 |
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 2014-05-31 | 2014-06-04 | 9079 | 1,560,600.0 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | WFR-65LA | Weatherford | Friction Reducer | Petroleum Distillates | 64742-47-8 | 40 | 0.0533 | 0 |
Water | 7732-18-5 | 55 | 0.0732 | 0 | ||||
Ammonium Acetate | 631-61-8 | 5 | 0.0067 | 0 | ||||
MX 588-2 | MultiChem | Scale Inhibitor | MX 588-2 | NA | 0 | 0.0209 | 0 | |
MC MX 8-2544 | MultiChem | Antibacterial | MC MX 8-2544 | NA | 0 | 0.0105 | 0 | |
Water | Range Resources | Base/Carrier Fluid | Water | 7732-18-5 | 100 | 87.4847 | 0 | |
35% HCL | Weatherford | Cleans perforations | Hydrochloric Acid | 7647-01-0 | 35 | 0.1319 | 0 | |
Water | 7732-18-5 | 65 | 0.245 | 0 | ||||
MX 5-2402 | MultiChem | Bacterial Nutritional Supplement | Sodium Nitrate | 7631-99-4 | 40 | 0.0512 | 0 | |
Water | 7732-18-5 | 60 | 0.0767 | 0 | ||||
Sand | Weatherford | Fracture Proppant | Crystalline Silica | 14808-60-7 | 100 | 11.8458 | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2014 | RANGE RESOURCES APPALACHIA LLC | 880,877.00 | 206 | 0.00 | 0 | 0.00 | 0 |
2015 | RANGE RESOURCES APPALACHIA LLC | 607,150.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | RANGE RESOURCES APPALACHIA LLC | 407,835.85 | 362 | 0.00 | 0 | 0.00 | 0 |
2017 | RANGE RESOURCES APPALACHIA LLC | 300,047.01 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | RANGE RESOURCES APPALACHIA LLC | 251,075.02 | 364 | 0.00 | 0 | 0.00 | 0 |
2019 | RANGE RESOURCES APPALACHIA LLC | 58,517.34 | 90 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|
2014-S01 | Drill Cuttings (in Tons) | 1,453.50 Tons | RESIDUAL WASTE PROCESSING FACILITY | WMGR097R017 |
2014-S02 | Fracing Fluid Waste (in Barrels) | 55.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2014-S02 | Produced Fluid (in Barrels) | 311.49 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2015-S01 | Produced Fluid (in Barrels) | 205.24 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2015-S02 | Produced Fluid (in Barrels) | 29.98 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123 |
2015-S02 | Produced Fluid (in Barrels) | 66.83 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2016-S01 | Other Oil & Gas Wastes (in Barrels) RWC 899 | 130.45 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2016-S02 | Other Oil & Gas Wastes (in Barrels) RWC 899 | 26.65 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2016-S02 | Produced Fluid (in Barrels) RWC 802 | 110.44 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2017-M01 | Other Oil & Gas Wastes (in Barrels) RWC 899 | 24.23 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2017-M01 | Produced Fluid (in Barrels) RWC 802 | 24.23 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2017-M02 | Other Oil & Gas Wastes (in Barrels) RWC 899 | 25.48 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2017-M03 | Produced Fluid (in Barrels) RWC 802 | 56.14 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2017-M09 | Produced Fluid (in Barrels) RWC 802 | 105.50 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2018-M01 | Produced Fluid (in Barrels) RWC 802 | 55.29 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2018-M02 | Produced Fluid (in Barrels) RWC 802 | 26.49 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2018-M06 | Produced Fluid (in Barrels) RWC 802 | 54.62 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2018-M07 | Other Oil & Gas Wastes (in Barrels) RWC 899 | 66.31 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2018-M07 | Produced Fluid (in Barrels) RWC 802 | 45.72 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2018-M12 | Produced Fluid (in Barrels) RWC 802 | 51.98 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2277742 | Primary Facility | 2014-06-06 | Incident- Response to Accident or Event | Viol(s) Noted & Immediately Corrected | On 6/6/2014, Andrea Mullen (DEP) and I met with Mr. Subra on the well pad and containment had been removed around the spill area. A failed seam between old containment and new containment was the suspected cause of the brine release. Mr. Subra was directing the excavation/remediation of the pad by soil conductivity. I asked Mr. Subra to test no less than 20 locations throughout the spill area which were still wet. No locations were found where soil conductivity was over 1,000 umhos/cm. Excavated pad material was being stockpiled (on liner) for disposal. Violations Noted and Immediately Corrected. |
2451667 | Primary Facility | 2016-02-08 | Administrative/File Review | No Violations Noted | The Well Site Restoration Report submitted to the Department for the Null Bobst 5H (081-21370) contains no waste disposal information and is considered incomplete. I recommend evaluating the PCSM (Post Construction Stormwater Management) requirements and re-submitting new Well Site Restoration Reports in the future. No Violations Noted. |
2471965 | Primary Facility | 2016-03-30 | Routine/Complete Inspection | No Violations Noted | Routein inspection of well in production. No violations noted. |
2517282 | Primary Facility | 2016-09-07 | Routine/Complete Inspection | No Violations Noted | Arrived @ 11:50. Weather: sunny, light breeze, low humidity. This was a routine inspection. There were no personnel on site. There were two producing wells. Cellars were gravel filled:
Null Bobst Unit 1H Top gauge: 620 psi (0-1500 psi analog), 13-3/8” x 9-5/8”: no combustible gas detected (Altair 5X gas meter calibrated 09/07/16), 9-5/8” x 5-1/2”: plumbed to 225-gallon polytank. no combustible gas at polytank vent. Null Bobst Unit 5H No top gauge, 5-1/2”: 600 psi (0-1000 psi analog), ), no 13-3/8” x 9-5/8: vent., 9-5/8” x 5-1/2”: plumbed to 225-gallon polytank, no combustible gas detected. Left location @ 12:20. |
2572079 | Primary Facility | 2017-03-08 | Routine/Complete Inspection | No Violations Noted | Arrived @ 13:49. Weather: windy. This was a routine inspection. There were no personnel on site. There were two producing wells. Cellars were gravel filled:
Null Bobst Unit 1H Top gauge: 640 psi (0-1500 psi analog), 13-3/8” x 9-5/8”: no combustible gas detected (Altair 5X gas meter calibrated 03/06/17), 9-5/8” x 5-1/2”: plumbed to 225-gallon polytank. no combustible gas at polytank vent. Null Bobst Unit 5H Top gauge: 600 psi (0-1000 psi analog), ), no 13-3/8” x 9-5/8: vent., 9-5/8” x 5-1/2”: 25% combustible gas detected. Left location @ 14:00. |
2791491 | Primary Facility | 2018-10-19 | Routine/Complete Inspection | No Violations Noted | Two wells staged for production phase. Two each water separators. No leaks detected from production equipment. No violations noted. |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2277742 | 697954 | 06/06/2014 | 2014-06-06 | 402CSL - Failure to adopt pollution prevention measures required or prescribed by DEP by handling materials that create a danger of pollution. | Environmental Health & Safety | On 6/6/2014, Andrea Mullen (DEP) and I met with Mr. Subra on the well pad and containment had been removed around the spill area. A failed seam between old containment and new containment was the suspected cause of the brine release. Mr. Subra was directing the excavation/remediation of the pad by |
2277742 | 697955 | 06/06/2014 | 2014-06-06 | 78.54* - Failure to properly control or dispose of industrial or residual waste to prevent pollution of the waters of the Commonwealth. | Environmental Health & Safety | On 6/6/2014, Andrea Mullen (DEP) and I met with Mr. Subra on the well pad and containment had been removed around the spill area. A failed seam between old containment and new containment was the suspected cause of the brine release. Mr. Subra was directing the excavation/remediation of the pad by |
2277742 | 697956 | 06/06/2014 | 2014-06-06 | SWMA301 - Failure to properly store, transport, process or dispose of a residual waste. | Environmental Health & Safety | On 6/6/2014, Andrea Mullen (DEP) and I met with Mr. Subra on the well pad and containment had been removed around the spill area. A failed seam between old containment and new containment was the suspected cause of the brine release. Mr. Subra was directing the excavation/remediation of the pad by |
For data sources see[7]