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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 37-129-27627 | | Well ID: 37-129-27627 | ||
− | | style="height=100%; align=center" rowspan=" | + | | style="height=100%; align=center" rowspan="15" | {{#display_map: 40.202967, -79.734063 | width=100% | height=100% }} |
|- | |- | ||
| Country: United States | | Country: United States | ||
Line 21: | Line 21: | ||
| License Status: Active | | License Status: Active | ||
|- | |- | ||
− | | Spud Date: 09 | + | | Spud Date: 2008-09-10 |
|- | |- | ||
− | | Permit Date: | + | | Permit Date: 2008-08-29 |
|- | |- | ||
| Unconventional Well: N | | Unconventional Well: N | ||
Line 49: | Line 49: | ||
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
| accessdate = 2019-05-21 }}</ref> | | accessdate = 2019-05-21 }}</ref> | ||
+ | <!--== Fracking Activities == | ||
+ | ==== Fracking Jobs ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Job Number | ||
+ | !scope="col" | Job Start Date | ||
+ | !scope="col" | Job End Date | ||
+ | !scope="col" | True Vertical Depth (ft) | ||
+ | !scope="col" | Total Water Volume (gal) | ||
+ | !scope="col" | Total Non-Water Volume (gal) | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--==== Fluid Composition Data ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Job Number | ||
+ | !scope="col" | Trade Name | ||
+ | !scope="col" | Supplier | ||
+ | !scope="col" | Purpose | ||
+ | !scope="col" | Ingredient Name | ||
+ | !scope="col" | CAS Number | ||
+ | !scope="col" | Additive Percentage by Mass | ||
+ | !scope="col" | Job Percentage by Mass | ||
+ | !scope="col" | Mass Used (lb) | ||
+ | |- | ||
+ | |}--> | ||
+ | |||
== Production Data == | == Production Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 67: | Line 92: | ||
| style="text-align: right;" | 366 | | style="text-align: right;" | 366 | ||
| style="text-align: right;" | 0.00 | | style="text-align: right;" | 0.00 | ||
− | | style="text-align: right;" | | + | | style="text-align: right;" | 0 |
|- | |- | ||
| 2009 | | 2009 | ||
Line 76: | Line 101: | ||
| style="text-align: right;" | 365 | | style="text-align: right;" | 365 | ||
| style="text-align: right;" | 0.00 | | style="text-align: right;" | 0.00 | ||
− | | style="text-align: right;" | | + | | style="text-align: right;" | 0 |
|- | |- | ||
| 2010 | | 2010 | ||
Line 85: | Line 110: | ||
| style="text-align: right;" | 365 | | style="text-align: right;" | 365 | ||
| style="text-align: right;" | 0.00 | | style="text-align: right;" | 0.00 | ||
− | | style="text-align: right;" | | + | | style="text-align: right;" | 0 |
|- | |- | ||
| 2011 | | 2011 | ||
Line 94: | Line 119: | ||
| style="text-align: right;" | 365 | | style="text-align: right;" | 365 | ||
| style="text-align: right;" | 0.00 | | style="text-align: right;" | 0.00 | ||
− | | style="text-align: right;" | | + | | style="text-align: right;" | 0 |
|- | |- | ||
| 2012 | | 2012 | ||
Line 103: | Line 128: | ||
| style="text-align: right;" | 366 | | style="text-align: right;" | 366 | ||
| style="text-align: right;" | 0.00 | | style="text-align: right;" | 0.00 | ||
− | | style="text-align: right;" | | + | | style="text-align: right;" | 0 |
|- | |- | ||
| 2013 | | 2013 | ||
Line 112: | Line 137: | ||
| style="text-align: right;" | 365 | | style="text-align: right;" | 365 | ||
| style="text-align: right;" | 0.00 | | style="text-align: right;" | 0.00 | ||
− | | style="text-align: right;" | | + | | style="text-align: right;" | 0 |
|- | |- | ||
| 2014 | | 2014 | ||
Line 121: | Line 146: | ||
| style="text-align: right;" | 365 | | style="text-align: right;" | 365 | ||
| style="text-align: right;" | 0.00 | | style="text-align: right;" | 0.00 | ||
− | | style="text-align: right;" | | + | | style="text-align: right;" | 0 |
|- | |- | ||
| 2015 | | 2015 | ||
Line 130: | Line 155: | ||
| style="text-align: right;" | 365 | | style="text-align: right;" | 365 | ||
| style="text-align: right;" | 0.00 | | style="text-align: right;" | 0.00 | ||
− | | style="text-align: right;" | | + | | style="text-align: right;" | 0 |
|- | |- | ||
| 2016 | | 2016 | ||
Line 139: | Line 164: | ||
| style="text-align: right;" | 366 | | style="text-align: right;" | 366 | ||
| style="text-align: right;" | 0.00 | | style="text-align: right;" | 0.00 | ||
− | | style="text-align: right;" | | + | | style="text-align: right;" | 0 |
|- | |- | ||
| 2017 | | 2017 | ||
Line 148: | Line 173: | ||
| style="text-align: right;" | 365 | | style="text-align: right;" | 365 | ||
| style="text-align: right;" | 0.00 | | style="text-align: right;" | 0.00 | ||
− | | style="text-align: right;" | | + | | style="text-align: right;" | 0 |
|- | |- | ||
| 2018 | | 2018 | ||
Line 157: | Line 182: | ||
| style="text-align: right;" | 365 | | style="text-align: right;" | 365 | ||
| style="text-align: right;" | 0.00 | | style="text-align: right;" | 0.00 | ||
− | | style="text-align: right;" | | + | | style="text-align: right;" | 0 |
|- | |- | ||
|} | |} | ||
Line 271: | Line 296: | ||
| 1736764 | | 1736764 | ||
| Primary Facility | | Primary Facility | ||
− | | 09 | + | | 2008-09-12 |
| Drilling/Alteration | | Drilling/Alteration | ||
| No Violations Noted | | No Violations Noted | ||
Line 278: | Line 303: | ||
| 2389917 | | 2389917 | ||
| Primary Facility | | Primary Facility | ||
− | | 07 | + | | 2015-07-15 |
| Routine/Complete Inspection | | Routine/Complete Inspection | ||
| Repairs or Upgrade Required | | Repairs or Upgrade Required | ||
Line 285: | Line 310: | ||
| 2390315 | | 2390315 | ||
| Primary Facility | | Primary Facility | ||
− | | 07 | + | | 2015-07-15 |
| Incident- Response to Accident or Event | | Incident- Response to Accident or Event | ||
| Violation(s) Noted | | Violation(s) Noted | ||
Line 292: | Line 317: | ||
| 2390323 | | 2390323 | ||
| Primary Facility | | Primary Facility | ||
− | | 07 | + | | 2015-07-16 |
| Follow-up Inspection | | Follow-up Inspection | ||
| Outstanding Violations - No Viols Req'd | | Outstanding Violations - No Viols Req'd | ||
Line 299: | Line 324: | ||
| 2390324 | | 2390324 | ||
| Primary Facility | | Primary Facility | ||
− | | 07 | + | | 2015-07-17 |
| Follow-up Inspection | | Follow-up Inspection | ||
| Outstanding Violations - No Viols Req'd | | Outstanding Violations - No Viols Req'd | ||
Line 306: | Line 331: | ||
| 2390827 | | 2390827 | ||
| Primary Facility | | Primary Facility | ||
− | | 07 | + | | 2015-07-20 |
| Follow-up Inspection | | Follow-up Inspection | ||
| Outstanding Violations - No Viols Req'd | | Outstanding Violations - No Viols Req'd | ||
Line 313: | Line 338: | ||
| 2393192 | | 2393192 | ||
| Primary Facility | | Primary Facility | ||
− | | 07 | + | | 2015-07-27 |
| Follow-up Inspection | | Follow-up Inspection | ||
| No Violations Noted | | No Violations Noted | ||
Line 320: | Line 345: | ||
| 2393290 | | 2393290 | ||
| Primary Facility | | Primary Facility | ||
− | | 07 | + | | 2015-07-22 |
| Follow-up Inspection | | Follow-up Inspection | ||
| Outstanding Violations - No Viols Req'd | | Outstanding Violations - No Viols Req'd | ||
Line 327: | Line 352: | ||
| 2393300 | | 2393300 | ||
| Primary Facility | | Primary Facility | ||
− | | 07 | + | | 2015-07-24 |
| Follow-up Inspection | | Follow-up Inspection | ||
| Outstanding Violations - No Viols Req'd | | Outstanding Violations - No Viols Req'd | ||
Line 334: | Line 359: | ||
| 2397191 | | 2397191 | ||
| Primary Facility | | Primary Facility | ||
− | | 08 | + | | 2015-08-06 |
| Follow-up Inspection | | Follow-up Inspection | ||
| Outstanding Violations - No Viols Req'd | | Outstanding Violations - No Viols Req'd | ||
Line 341: | Line 366: | ||
| 2398412 | | 2398412 | ||
| Primary Facility | | Primary Facility | ||
− | | 08 | + | | 2015-08-13 |
| Administrative/File Review | | Administrative/File Review | ||
| Outstanding Violations - No Viols Req'd | | Outstanding Violations - No Viols Req'd | ||
Line 348: | Line 373: | ||
| 2403465 | | 2403465 | ||
| Primary Facility | | Primary Facility | ||
− | | 08 | + | | 2015-08-28 |
| Compliance Evaluation | | Compliance Evaluation | ||
| No Violations Noted | | No Violations Noted | ||
Line 367: | Line 392: | ||
| 729803 | | 729803 | ||
| 07/15/2015 | | 07/15/2015 | ||
− | | | + | | 2015-07-15 |
| OGA 3217(A) - Failure to control and dispose of brines produced from the drilling, alteration or operation of a well consistent with the Clean Streams Law. | | OGA 3217(A) - Failure to control and dispose of brines produced from the drilling, alteration or operation of a well consistent with the Clean Streams Law. | ||
| Environmental Health & Safety | | Environmental Health & Safety | ||
Line 375: | Line 400: | ||
| 729804 | | 729804 | ||
| 07/15/2015 | | 07/15/2015 | ||
− | | | + | | 2015-07-15 |
| 78.54 - GENERAL REQUIREMENTS - Operator failed to control and dispose of fluids, residual waste and drill cuttings, including tophole water, brines, drilling fluids, drilling muds, stimulation fluids, well servicing fluids, oil, and production fluids | | 78.54 - GENERAL REQUIREMENTS - Operator failed to control and dispose of fluids, residual waste and drill cuttings, including tophole water, brines, drilling fluids, drilling muds, stimulation fluids, well servicing fluids, oil, and production fluids | ||
| Environmental Health & Safety | | Environmental Health & Safety | ||
Line 417: | Line 442: | ||
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
| accessdate = 2019-05-21 }}</ref> | | accessdate = 2019-05-21 }}</ref> | ||
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==References== | ==References== | ||
<references/> | <references/> | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Pennsylvania Wells]] | [[Category:Pennsylvania Wells]] |
Well ID: 37-129-27627 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Westmoreland | |
Municipality: South Huntingdon Township | |
Operator Name: DIVERSIFIED OIL & GAS LLC | |
Well Pad ID: | |
Farm/Lease Name: BRANTHOOVER 6 | |
License Status: Active | |
Spud Date: 2008-09-10 | |
Permit Date: 2008-08-29 | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Latitude: 40.202967 | |
Longitude: -79.734063 |
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2008 | ATLAS RESOURCES LLC | 48.00 | 366 | 52.00 | 366 | 0.00 | 0 |
2009 | ATLAS RESOURCES LLC | 7,357.00 | 365 | 390.00 | 365 | 0.00 | 0 |
2010 | ATLAS RESOURCES LLC | 4,673.00 | 365 | 152.00 | 365 | 0.00 | 0 |
2011 | ATLAS RESOURCES LLC | 3,990.00 | 365 | 170.00 | 365 | 0.00 | 0 |
2012 | ATLAS RESOURCES LLC | 3,301.00 | 366 | 58.00 | 366 | 0.00 | 0 |
2013 | ATLAS RESOURCES LLC | 2,779.00 | 365 | 146.00 | 365 | 0.00 | 0 |
2014 | ATLAS RESOURCES LLC | 2,744.00 | 365 | 80.00 | 365 | 0.00 | 0 |
2015 | ATLAS RESOURCES LLC | 2,459.00 | 365 | 80.00 | 365 | 0.00 | 0 |
2016 | ATLAS RESOURCES LLC | 2,609.00 | 366 | 47.00 | 366 | 0.00 | 0 |
2017 | ATLAS RESOURCES LLC | 1,902.00 | 365 | 62.00 | 365 | 0.00 | 0 |
2018 | DIVERSIFIED OIL & GAS LLC | 1,796.00 | 365 | 42.00 | 365 | 0.00 | 0 |
For data sources see[4]
Period | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|
2008-A00 | Brine | 75.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0091472 |
2008-A00 | Brine | 45.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0095273 |
2008-A00 | Brine | 2,120.00 Bbl | Municipal Sewage Treatment Plant | PA0026891 |
2009-A00 | Brine | 24.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0091472 |
2009-A00 | Brine | 108.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0095273 |
2010-A00 | Produced Fluid (in Barrels) | 36.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 |
2011-A00 | Produced Fluid (in Barrels) | 35.00 Bbl | INJECTION DISPOSAL WELL | 34-121-2-3995 |
2012-A00 | Produced Fluid (in Barrels) | 5.00 Bbl | INJECTION DISPOSAL WELL | 34-121-23995 |
2013-A00 | Produced Fluid (in Barrels) | 24.00 Bbl | INJECTION DISPOSAL WELL | 34-121-23995 |
2016-A00 | Produced Fluid (in Barrels) RWC 802 | 12.00 Bbl | INJECTION DISPOSAL WELL | 34-167-23862 |
2016-A00 | Produced Fluid (in Barrels) RWC 802 | 12.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123SW001 |
2017-A00 | Produced Fluid (in Barrels) RWC 802 | 23.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123SW001 |
2018-A00 | Produced Fluid (in Barrels) RWC 802 | 7.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123SW010 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1736764 | Primary Facility | 2008-09-12 | Drilling/Alteration | No Violations Noted | Well spudded. Location/pit/freeboard/E&S controls Ok. |
2389917 | Primary Facility | 2015-07-15 | Routine/Complete Inspection | Repairs or Upgrade Required | On site a produced fluids tank ruptured due to the plumbing of the relief valve into an unvented tank. When the relief valve relieved presure to the tank the presure caused the tank to swell then rupture. Rupturing of the produced fluids tank caused a release of multiple barrels of crude oil and brine water mixed to disperse over the site and down over an embankment into the waters of the Commonwealth. WQS S. Steingrabe is onsite gathering water samples. |
2390315 | Primary Facility | 2015-07-15 | Incident- Response to Accident or Event | Violation(s) Noted | remarks to large for entry |
2390323 | Primary Facility | 2015-07-16 | Follow-up Inspection | Outstanding Violations - No Viols Req'd | remards to large for entry |
2390324 | Primary Facility | 2015-07-17 | Follow-up Inspection | Outstanding Violations - No Viols Req'd | remards to large for entry |
2390827 | Primary Facility | 2015-07-20 | Follow-up Inspection | Outstanding Violations - No Viols Req'd | The drill pit that had been encapsulated during well development had been located and and shown to the small excavator operator for avoidance. Excavation was in process to remove and delineate the affected area in the immediate vicinity of the well site. Subsuequently excavation will be undertaken along the pathway that brine/oil traveled to the tributary to Sewickley Creek to remove the affected media. According to Mr. Elkin, Moody & Associates personnel will be onsite later today, 07/20/15, to begin background and confirmation sampling. WQS Higgins suggested that Atlas Resources consider utilizing a vac truck to remove contaminated fluids from the tributary to Sewickley Creek, especially if significant precipitation is expected, both before and after the rain event. There was a a light sheen observed in tributary both before and after the underflow dams. This is likely attributed to oil and brine that had been deposited on the vegetation and streambanks during the recent high water period. |
2393192 | Primary Facility | 2015-07-27 | Follow-up Inspection | No Violations Noted | see hard copy for remarks |
2393290 | Primary Facility | 2015-07-22 | Follow-up Inspection | Outstanding Violations - No Viols Req'd | Site inspection performed as part of the follow-up to the crude oil/brine release. Site excavation. confirmation sampling and background sampling had been completed on 07/20/15. The excavated area immediately around the well-head and tank left onsite was left open to allow for additional excavation should sample results indicate more excavation is necessary. Temporary erosion controls had been implemented in this area. The area affected by the breakout flow of the brine/crude and precipitation had been excavated, confirmation and background samples taken, regraded and temporarily stabilzed with erosion control blankets. The underflow dams implemented in the UNT were functioning properly. There was little to no sheen observed in the UNT. The small wisps of sheen observed were likely attributable to product that had been absorbed by the vegetation along the stream banks. |
2393300 | Primary Facility | 2015-07-24 | Follow-up Inspection | Outstanding Violations - No Viols Req'd | Site inspection found that the site was in much the same condition as was observed in the 07/22/15 inspection. Site inspection performed as part of the follow-up to the crude oil/brine release. Site excavation. confirmation sampling and background sampling had been completed on 07/20/15. The excavated area immediately around the well-head and tank left onsite was left open to allow for additional excavation should sample results indicate more excavation is necessary. Temporary erosion controls had been implemented in this area. The area affected by the breakout flow of the brine/crude and precipitation had been excavated, confirmation and background samples taken, regraded and temporarily stabilzed with erosion control blankets. The underflow dams implemented in the UNT were functioning properly. There was little to no sheen observed in the UNT. The small wisps of sheen observed were likely attributable to product that had been absorbed by the vegetation along the stream banks. |
2397191 | Primary Facility | 2015-08-06 | Follow-up Inspection | Outstanding Violations - No Viols Req'd | see hard copy. |
2398412 | Primary Facility | 2015-08-13 | Administrative/File Review | Outstanding Violations - No Viols Req'd | Administrative review of the 15 day response document received by the Department on 8/5/2015, pertaining to the Brine and Oil spill that occurred on 7/15/2015. |
2403465 | Primary Facility | 2015-08-28 | Compliance Evaluation | No Violations Noted | Compliance Inspection pertaining to the Brine and Oil release that occurred on 7/15/2015. |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2390315 | 729803 | 07/15/2015 | 2015-07-15 | OGA 3217(A) - Failure to control and dispose of brines produced from the drilling, alteration or operation of a well consistent with the Clean Streams Law. | Environmental Health & Safety | |
2390315 | 729804 | 07/15/2015 | 2015-07-15 | 78.54 - GENERAL REQUIREMENTS - Operator failed to control and dispose of fluids, residual waste and drill cuttings, including tophole water, brines, drilling fluids, drilling muds, stimulation fluids, well servicing fluids, oil, and production fluids | Environmental Health & Safety |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
729803 | 327408 | NOV - Notice of Violation | |||||
729804 | 327408 | NOV - Notice of Violation |
For data sources see[6]