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Difference between revisions of "34-155-20975"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-155-20975
 
| Well ID: 34-155-20975
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.3151144727, -80.8266560156 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.31511447, -80.82665602 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Trumbull County, Ohio|Trumbull]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[ENERVEST OPERATING L]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 1978-07-17
 
| Spud Date: 1978-07-17
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Producing
 
|-
 
|-
| Violations: 3
+
| Violations: 0
 
|-
 
|-
| Latitude: 41.3151144727
+
| Latitude: 41.31511447
 
|-
 
|-
| Longitude: -80.8266560156
+
| Longitude: -80.82665602
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 1984-0
 +
| style="text-align:right;" | 13549.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 63.0
 +
|
 +
|-
 +
|-
 +
| 1985-0
 +
| style="text-align:right;" | 10642.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1986-0
 +
| style="text-align:right;" | 8510.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 44.0
 +
|
 +
|-
 +
|-
 +
| 1987-0
 +
| style="text-align:right;" | 14188.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 76.0
 +
|
 +
|-
 +
|-
 +
| 1988-0
 +
| style="text-align:right;" | 11231.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 60.0
 +
|
 +
|-
 +
|-
 +
| 1989-0
 +
| style="text-align:right;" | 11681.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 56.0
 +
|
 +
|-
 +
|-
 +
| 1990-0
 +
| style="text-align:right;" | 10163.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1991-0
 +
| style="text-align:right;" | 7877.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1992-0
 +
| style="text-align:right;" | 5987.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 57.0
 +
|
 +
|-
 +
|-
 +
| 1993-0
 +
| style="text-align:right;" | 9481.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1994-0
 +
| style="text-align:right;" | 7263.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 34.0
 +
|
 +
|-
 +
|-
 +
| 1995-0
 +
| style="text-align:right;" | 5419.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1996-0
 +
| style="text-align:right;" | 6422.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1997-0
 +
| style="text-align:right;" | 8000.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1998-0
 +
| style="text-align:right;" | 1934.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 41.0
 +
|
 +
|-
 +
|-
 +
| 1999-0
 +
| style="text-align:right;" | 3317.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2000-0
 +
| style="text-align:right;" | 4633.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2001-0
 +
| style="text-align:right;" | 888.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2002-0
 +
| style="text-align:right;" | 3151.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2003-0
 +
| style="text-align:right;" | 4899.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2004-0
 +
| style="text-align:right;" | 4025.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2005-0
 +
| style="text-align:right;" | 3107.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2006-0
 +
| style="text-align:right;" | 2430.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2007-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2008-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2009-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2010-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2011-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2012-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2013-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2014-0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 337:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
|-
 
| 1367931740
 
| 2013-05-06
 
|
 
| I received a call on 5/4/2013 at 9:15 pm from ODNR communications (614-799-9538) about a well in Champion that had been shot and was leaking fluid.  I found the well belonged to Enervest and called their field supervisor at 216-570-8708, Larry Lower.  He immediately dispatched a well tender to assess the situation and make repairs.  Larry found the 1.5" tubing on the plunger lift unit had a small hole from a gun shot.  Also, a coupling on the flow line had a mark from a gun shot.  The well tender placed a clamp on the tubing to stop the leaking.  On 5/5/2013, I received a call from Trumbull County 911 that the tubing was leaking again.  I called Larry Lower and he dispatched the well tender.  The well tender replaced the clamp with a new full circle clamp until further repairs could be made.  My inspection on 5/6/2013 found the clamp holding.  I noticed a 10' grassy area around the well that had been impacted from the leak.  Enervest had peat sorb and absorbent pads in place.  A Bobcat was dispatched to the location to remove all of the grass and soil impacted.  Approximately 3 to 4 barrels of brine was released.  I researched our database and found the well had not produced since 2006 under Belden and Blake Corporation.  The tank battery contained one, 100 barrel production tank.  The dike was weathered and did not meet containment requirements.  The heat, treated separator was surrounded by debris from the resident.  There was an identification sign posted on the production tank.  The was no lease road to the tank battery.  Larry Lower informed me that Enervest was working on contacting the landowner to get access to the tank battery and well.  Enervest was issued a plugging permit on 3/6/2013.
 
|
 
| 9-1-02
 
|
 
|-
 
|-
 
| 1367931740
 
| 2013-05-06
 
|
 
| I received a call on 5/4/2013 at 9:15 pm from ODNR communications (614-799-9538) about a well in Champion that had been shot and was leaking fluid.  I found the well belonged to Enervest and called their field supervisor at 216-570-8708, Larry Lower.  He immediately dispatched a well tender to assess the situation and make repairs.  Larry found the 1.5" tubing on the plunger lift unit had a small hole from a gun shot.  Also, a coupling on the flow line had a mark from a gun shot.  The well tender placed a clamp on the tubing to stop the leaking.  On 5/5/2013, I received a call from Trumbull County 911 that the tubing was leaking again.  I called Larry Lower and he dispatched the well tender.  The well tender replaced the clamp with a new full circle clamp until further repairs could be made.  My inspection on 5/6/2013 found the clamp holding.  I noticed a 10' grassy area around the well that had been impacted from the leak.  Enervest had peat sorb and absorbent pads in place.  A Bobcat was dispatched to the location to remove all of the grass and soil impacted.  Approximately 3 to 4 barrels of brine was released.  I researched our database and found the well had not produced since 2006 under Belden and Blake Corporation.  The tank battery contained one, 100 barrel production tank.  The dike was weathered and did not meet containment requirements.  The heat, treated separator was surrounded by debris from the resident.  There was an identification sign posted on the production tank.  The was no lease road to the tank battery.  Larry Lower informed me that Enervest was working on contacting the landowner to get access to the tank battery and well.  Enervest was issued a plugging permit on 3/6/2013.
 
|
 
| 9-9-05(A)9
 
|
 
|-
 
 
|-
 
|-
 
| 1367931740
 
| 1367931740
 
| 2013-05-06
 
| 2013-05-06
|
+
|  
| I received a call on 5/4/2013 at 9:15 pm from ODNR communications (614-799-9538) about a well in Champion that had been shot and was leaking fluid.  I found the well belonged to Enervest and called their field supervisor at 216-570-8708, Larry Lower.  He immediately dispatched a well tender to assess the situation and make repairs.  Larry found the 1.5" tubing on the plunger lift unit had a small hole from a gun shot.  Also, a coupling on the flow line had a mark from a gun shot.  The well tender placed a clamp on the tubing to stop the leaking.  On 5/5/2013, I received a call from Trumbull County 911 that the tubing was leaking again.  I called Larry Lower and he dispatched the well tender.  The well tender replaced the clamp with a new full circle clamp until further repairs could be made.  My inspection on 5/6/2013 found the clamp holding.  I noticed a 10' grassy area around the well that had been impacted from the leak.  Enervest had peat sorb and absorbent pads in place.  A Bobcat was dispatched to the location to remove all of the grass and soil impacted.  Approximately 3 to 4 barrels of brine was released.  I researched our database and found the well had not produced since 2006 under Belden and Blake Corporation.  The tank battery contained one, 100 barrel production tank.  The dike was weathered and did not meet containment requirements.  The heat, treated separator was surrounded by debris from the resident.  There was an identification sign posted on the production tank.  The was no lease road to the tank battery.  Larry Lower informed me that Enervest was working on contacting the landowner to get access to the tank battery and well.  Enervest was issued a plugging permit on 3/6/2013.
+
| I received a call on 5/4/2013 at 9:15 pm from ODNR communications (614-799-9538) about a well in Champion that had been shot and was leaking fluid.  I found the well belonged to Enervest and called their field supervisor at 216-570-8708, Larry Lower.  He immediately dispatched a well tender to assess the situation and make repairs.  Larry found the 1.5 tubing on the plunger lift unit had a small hole from a gun shot.  Also, a coupling on the flow line had a mark from a gun shot.  The well tender placed a clamp on the tubing to stop the leaking.  On 5/5/2013, I received a call from Trumbull County 911 that the tubing was leaking again.  I called Larry Lower and he dispatched the well tender.  The well tender replaced the clamp with a new full circle clamp until further repairs could be made.  My inspection on 5/6/2013 found the clamp holding.  I noticed a 10' grassy area around the well that had been impacted from the leak.  Enervest had peat sorb and absorbent pads in place.  A Bobcat was dispatched to the location to remove all of the grass and soil impacted.  Approximately 3 to 4 barrels of brine was released.  I researched our database and found the well had not produced since 2006 under Belden and Blake Corporation.  The tank battery contained one, 100 barrel production tank.  The dike was weathered and did not meet containment requirements.  The heat, treated separator was surrounded by debris from the resident.  There was an identification sign posted on the production tank.  The was no lease road to the tank battery.  Larry Lower informed me that Enervest was working on contacting the landowner to get access to the tank battery and well.  Enervest was issued a plugging permit on 3/6/2013.
|
+
|  
| NONE_
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 14:20, 16 July 2015

Well Details

Well ID: 34-155-20975
Loading map...
County: Trumbull
Municipality:
Operator Name: ENERVEST OPERATING L
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1978-07-17
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 41.31511447
Longitude: -80.82665602

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 13549.0 63.0
1985-0 10642.0 0.0
1986-0 8510.0 44.0
1987-0 14188.0 76.0
1988-0 11231.0 60.0
1989-0 11681.0 56.0
1990-0 10163.0 0.0
1991-0 7877.0 0.0
1992-0 5987.0 57.0
1993-0 9481.0 0.0
1994-0 7263.0 34.0
1995-0 5419.0 0.0
1996-0 6422.0 0.0
1997-0 8000.0 0.0
1998-0 1934.0 41.0
1999-0 3317.0 0.0
2000-0 4633.0 0.0
2001-0 888.0 0.0
2002-0 3151.0 0.0
2003-0 4899.0 0.0
2004-0 4025.0 0.0
2005-0 3107.0 0.0
2006-0 2430.0 0.0
2007-0 0.0 0.0
2008-0 0.0 0.0
2009-0 0.0 0.0
2010-0 0.0 0.0
2011-0 0.0 0.0
2012-0 0.0 0.0
2013-0 0.0 0.0
2014-0 0.0 0.0 0.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1367931740 2013-05-06 I received a call on 5/4/2013 at 9:15 pm from ODNR communications (614-799-9538) about a well in Champion that had been shot and was leaking fluid. I found the well belonged to Enervest and called their field supervisor at 216-570-8708, Larry Lower. He immediately dispatched a well tender to assess the situation and make repairs. Larry found the 1.5 tubing on the plunger lift unit had a small hole from a gun shot. Also, a coupling on the flow line had a mark from a gun shot. The well tender placed a clamp on the tubing to stop the leaking. On 5/5/2013, I received a call from Trumbull County 911 that the tubing was leaking again. I called Larry Lower and he dispatched the well tender. The well tender replaced the clamp with a new full circle clamp until further repairs could be made. My inspection on 5/6/2013 found the clamp holding. I noticed a 10' grassy area around the well that had been impacted from the leak. Enervest had peat sorb and absorbent pads in place. A Bobcat was dispatched to the location to remove all of the grass and soil impacted. Approximately 3 to 4 barrels of brine was released. I researched our database and found the well had not produced since 2006 under Belden and Blake Corporation. The tank battery contained one, 100 barrel production tank. The dike was weathered and did not meet containment requirements. The heat, treated separator was surrounded by debris from the resident. There was an identification sign posted on the production tank. The was no lease road to the tank battery. Larry Lower informed me that Enervest was working on contacting the landowner to get access to the tank battery and well. Enervest was issued a plugging permit on 3/6/2013.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.