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Difference between revisions of "37-051-24328"

m
m
Line 3: Line 3:
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 37-051-24328
 
| Well ID: 37-051-24328
| style="height=100%; align=center" rowspan="14" | {{#display_map: 40.010133, -79.672622 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.010133, -79.672622 | width=100% | height=100% }}  
 
|-
 
|-
 
| County: [[Fayette County, Pennsylvania|Fayette]]
 
| County: [[Fayette County, Pennsylvania|Fayette]]
Line 9: Line 9:
 
| Municipality: [[Dunbar Township, Fayette County, Pennsylvania|Dunbar Township]]
 
| Municipality: [[Dunbar Township, Fayette County, Pennsylvania|Dunbar Township]]
 
|-
 
|-
| Operator Name: [[XTO ENERGY INC|XTO ENERGY INC]]
+
| Operator Name: [[XTO ENERGY INC]]
 
|-
 
|-
| Well Pad ID: [[148509]]
+
| Well Pad ID: [[148509|148509]]
 
|-
 
|-
 
| Farm/Lease Name: HELEN K BUKOVAC 4H
 
| Farm/Lease Name: HELEN K BUKOVAC 4H
Line 25: Line 25:
 
| Horizontal: Yes
 
| Horizontal: Yes
 
|-
 
|-
| Producing: Yes
+
| Well Status: ACTIVE
 
|-
 
|-
| Violations: None
+
| Violations: 1
 
|-
 
|-
 
| Latitude: 40.010133
 
| Latitude: 40.010133
Line 34: Line 34:
 
|-
 
|-
 
|}
 
|}
== Inspection Data ==
+
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" | PERIOD
!scope="col" | DATE
+
!scope="col" | GAS QUANTITY
!scope="col" | DESCRIPTION
+
!scope="col" | GAS PRODUCTION DAYS
!scope="col" | COMMENT
+
!scope="col" | CONDENSATE QUANTITY
!scope="col" | VIOLATION ID
+
!scope="col" | CONDENSATE PRODUCTION DAYS
 +
!scope="col" | OIL QUANTITY
 +
!scope="col" | OIL PRODUCTION DAYS
 
|-
 
|-
| 1889802
+
| 2010-3
| 2010-06-03
+
| style="text-align:right;" | 0.0
| No Violations Noted
+
| style="text-align:right;" | 0.0
|  
+
| style="text-align:right;" | 0.0
|  
+
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 
|-
 
|-
 
|-
 
|-
| 1893303
+
| 2010-2
| 2010-06-16
+
| style="text-align:right;" | 143357.0
| No Violations Noted
+
| style="text-align:right;" | 52.0
|  
+
| style="text-align:right;" | 0.0
|  
+
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 
|-
 
|-
 
|-
 
|-
| 1910105
+
| 2010-2
| 2010-08-20
+
| style="text-align:right;" | 143357.0
| No Violations Noted
+
| style="text-align:right;" | 52.0
| HORIZONTAL MARCELLUS, SAXON RIG -124 LANDING CURVE, TD ESTIMATED AT 11350', PITS AND E&S ARE GOOD.
+
| style="text-align:right;" | 0.0
|  
+
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 
|-
 
|-
 
|-
 
|-
| 2131364
+
| 2011-1
| 2013-01-15
+
| style="text-align:right;" | 475503.0
| No Violations Noted
+
| style="text-align:right;" | 181.0
| Notice of termination inspection. All areas reclaimed and had at least 70% growth.  Well labeled, tanks in containment, ID sign up.Site stable.
+
| style="text-align:right;" | 0.0
|  
+
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 
|-
 
|-
|}
 
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | PERIOD
 
!scope="col" | GAS QUANTITY
 
!scope="col" | GAS PRODUCTION DAYS
 
!scope="col" | CONDENSATE QUANTITY
 
!scope="col" | CONDENSATE PRODUCTION DAYS
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
 
|-
 
|-
| 2012-2
+
| 2011-2
| style="text-align:right;" | 196772.0
+
| style="text-align:right;" | 296529.0
 
| style="text-align:right;" | 184.0
 
| style="text-align:right;" | 184.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
Line 98: Line 98:
 
|-
 
|-
 
|-
 
|-
| 2011-2
+
| 2012-2
| style="text-align:right;" | 296529.0
+
| style="text-align:right;" | 196772.0
 
| style="text-align:right;" | 184.0
 
| style="text-align:right;" | 184.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
Line 107: Line 107:
 
|-
 
|-
 
|-
 
|-
| 2011-1
+
| 2013-1
| style="text-align:right;" | 475503.0
+
| style="text-align:right;" | 168164.0
 
| style="text-align:right;" | 181.0
 
| style="text-align:right;" | 181.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
Line 116: Line 116:
 
|-
 
|-
 
|-
 
|-
| 2010-2
+
| 2013-2
| style="text-align:right;" | 143357.0
+
| style="text-align:right;" | 154823.0
| style="text-align:right;" | 52.0
+
| style="text-align:right;" | 184.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
|-
 +
|-
 +
| 2014-1
 +
| style="text-align:right;" | 75532.0
 +
| style="text-align:right;" | 179.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
|-
 +
|-
 +
| 2014-2
 +
| style="text-align:right;" | 146944.0
 +
| style="text-align:right;" | 184.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
|-
 +
|-
 +
| 2015-02
 +
| style="text-align:right;" | 10051.0
 +
| style="text-align:right;" | 15.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
Line 125: Line 152:
 
|-
 
|-
 
|-
 
|-
| 2010-3
+
| 2015-01
 +
| style="text-align:right;" | 16332.0
 +
| style="text-align:right;" | 19.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 +
|-
 +
|-
 +
| 2015-03
 +
| style="text-align:right;" | 21460.0
 +
| style="text-align:right;" | 23.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
Line 134: Line 170:
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Oil and Gas Historical Production Report
 +
| publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2015-05-26
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources#Production
 +
| accessdate = 2015-05-27 }}</ref>
 
== Waste Data ==
 
== Waste Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 145: Line 187:
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
!scope="col" | FACILITY STATE
|-
 
| 2012-2
 
| PRODUCED FLUID
 
| style="text-align:right;" | 852.0
 
| Bbl
 
| CENTRALIZED TREATMENT PLANT FOR RECYCLE
 
| PA0254185
 
| RESERVED ENVIRONMENTAL SERVICES
 
| MOUNT PLEASANT
 
| PA
 
|-
 
|-
 
| 2012-2
 
| PRODUCED FLUID
 
| style="text-align:right;" | 92.0
 
| Bbl
 
| INJECTION DISPOSAL WELL
 
| 34-133-21076
 
| SALTYS DISPOSAL - MYERS INECTION WELL #1
 
| PARIS
 
| OH
 
|-
 
 
|-
 
|-
 
| 2010-2
 
| 2010-2
 
| PRODUCED FLUID
 
| PRODUCED FLUID
| style="text-align:right;" | 1815.0
+
| style="text-align:right;" | 1.0
 
| Bbl
 
| Bbl
 
| CENTRALIZED TREATMENT PLANT FOR RECYCLE
 
| CENTRALIZED TREATMENT PLANT FOR RECYCLE
 
| PAR000519462
 
| PAR000519462
| ADVANCED WASTE SERVICES OF PA (NEW CASTLE)
+
| ADVANCED WASTE SERVICES OF PA LLC
 
| NEW CASTLE
 
| NEW CASTLE
 
| PA
 
| PA
Line 181: Line 201:
 
| 2011-1
 
| 2011-1
 
| PRODUCED FLUID
 
| PRODUCED FLUID
| style="text-align:right;" | 2829.0
+
| style="text-align:right;" | 2.0
 
| Bbl
 
| Bbl
 
| CENTRALIZED TREATMENT PLANT FOR RECYCLE
 
| CENTRALIZED TREATMENT PLANT FOR RECYCLE
 
| PAR000519462
 
| PAR000519462
| ADVANCED WASTE SERVICES OF PA (NEW CASTLE)
+
| ADVANCED WASTE SERVICES OF PA LLC
 
| NEW CASTLE
 
| NEW CASTLE
 
| PA
 
| PA
Line 196: Line 216:
 
| INJECTION DISPOSAL WELL
 
| INJECTION DISPOSAL WELL
 
| 34-059-24067
 
| 34-059-24067
| DEVCO UNIT (SWIW #11) DAVID R HILL INC
+
| DEVCO UNIT #1 (SWIW #11)
 
| CAMBRIDGE
 
| CAMBRIDGE
 
| OH
 
| OH
Line 218: Line 238:
 
| CENTRALIZED TREATMENT PLANT FOR RECYCLE
 
| CENTRALIZED TREATMENT PLANT FOR RECYCLE
 
| PAR000519462
 
| PAR000519462
| ADVANCED WASTE SERVICES OF PA (NEW CASTLE)
+
| ADVANCED WASTE SERVICES OF PA LLC
 
| NEW CASTLE
 
| NEW CASTLE
 
| PA
 
| PA
Line 229: Line 249:
 
| CENTRALIZED TREATMENT PLANT FOR RECYCLE
 
| CENTRALIZED TREATMENT PLANT FOR RECYCLE
 
| PA0254185
 
| PA0254185
| RESERVED ENVIRONMENTAL SERVICES
+
| RESERVED ENV SVC WASTE WATER TREATMENT FACILITY
 
| MOUNT PLEASANT
 
| MOUNT PLEASANT
 
| PA
 
| PA
Line 243: Line 263:
 
|  
 
|  
 
|  
 
|  
 +
|-
 +
|-
 +
| 2012-1
 +
| PRODUCED FLUID
 +
| style="text-align:right;" | 92.0
 +
| Bbl
 +
| INJECTION DISPOSAL WELL
 +
|  34-133-24189
 +
| MEYERS #2 (SWIW #33)
 +
| ATWATER
 +
| OH
 
|-
 
|-
 
|-
 
|-
Line 251: Line 282:
 
| CENTRALIZED TREATMENT PLANT FOR RECYCLE
 
| CENTRALIZED TREATMENT PLANT FOR RECYCLE
 
| PA0254185
 
| PA0254185
| RESERVED ENVIRONMENTAL SERVICES
+
| RESERVED ENV SVC WASTE WATER TREATMENT FACILITY
 +
| MOUNT PLEASANT
 +
| PA
 +
|-
 +
|-
 +
| 2012-2
 +
| PRODUCED FLUID
 +
| style="text-align:right;" | 852.0
 +
| Bbl
 +
| CENTRALIZED TREATMENT PLANT FOR RECYCLE
 +
| PA0254185
 +
| RESERVED ENV SVC WASTE WATER TREATMENT FACILITY
 
| MOUNT PLEASANT
 
| MOUNT PLEASANT
 
| PA
 
| PA
 
|-
 
|-
 
|-
 
|-
| 2012-1
+
| 2012-2
 
| PRODUCED FLUID
 
| PRODUCED FLUID
 
| style="text-align:right;" | 92.0
 
| style="text-align:right;" | 92.0
 
| Bbl
 
| Bbl
 
| INJECTION DISPOSAL WELL
 
| INJECTION DISPOSAL WELL
| 34-133-24189
+
| 34-133-21076
| SALTY'S DISPOSAL - MEYERS #2 (SWIW #33)
+
| SALTYS DISPOSAL - MYERS INECTION WELL #1
| ATWATER
+
| PARIS
 
| OH
 
| OH
 +
|-
 +
|-
 +
| 2013-1
 +
| PRODUCED FLUID
 +
| style="text-align:right;" | 398.0
 +
| Bbl
 +
| CENTRALIZED TREATMENT PLANT FOR RECYCLE
 +
| PA0254185
 +
| RESERVED ENV SVC WASTE WATER TREATMENT FACILITY
 +
| MOUNT PLEASANT
 +
| PA
 +
|-
 +
|-
 +
| 2013-2
 +
| PRODUCED FLUID
 +
| style="text-align:right;" | 294.0
 +
| Bbl
 +
| CENT WASTE TRT FAC NPDES DISCHARGE
 +
| PA0254185
 +
| RESERVED ENV SVC WASTE WATER TREATMENT FACILITY
 +
| MOUNT PLEASANT
 +
| PA
 +
|-
 +
|-
 +
| 2014-1
 +
| PRODUCED FLUID
 +
| style="text-align:right;" | 110.0
 +
| Bbl
 +
| RESIDUAL WASTE PROC FAC (GENERAL PERMIT)
 +
| WMGR123NW009
 +
| RES WATER BUTLER
 +
|
 +
| PA
 +
|-
 +
|-
 +
| 2014-1
 +
| PRODUCED FLUID
 +
| style="text-align:right;" | 663.0
 +
| Bbl
 +
| CENT WASTE TRT FAC NPDES DISCHARGE
 +
| PA0254185
 +
| RESERVED ENV SVC WASTE WATER TREATMENT FACILITY
 +
| MOUNT PLEASANT
 +
| PA
 +
|-
 +
|-
 +
| 2014-2
 +
| PRODUCED FLUID
 +
| style="text-align:right;" | 100.0
 +
| Bbl
 +
| RESIDUAL WASTE PROC FAC (GENERAL PERMIT)
 +
| WMGR123NW009
 +
| RES WATER BUTLER
 +
|
 +
| PA
 +
|-
 +
|-
 +
| 2014-2
 +
| PRODUCED FLUID
 +
| style="text-align:right;" | 177.0
 +
| Bbl
 +
| RESIDUAL WASTE PROC FAC (GENERAL PERMIT)
 +
| WMGR123SW005
 +
| RESERVED ENV SVC HEMPFIELD TWP RESIDUAL WASTE OPER
 +
|
 +
| PA
 
|-
 
|-
 
|}
 
|}
==References==
+
For data sources see<ref>{{cite web
{{Reflist}}
+
| title = Oil and Gas Historical Waste Report
 +
| publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2015-05-26
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources#Waste
 +
| accessdate = 2015-05-26 }}</ref>
 +
== Inspection Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | INSPECTION ID
 +
!scope="col" | DATE
 +
!scope="col" | DESCRIPTION
 +
!scope="col" | COMMENT
 +
!scope="col" | VIOLATION ID
 +
!scope="col" | VIOLATION CODE
 +
!scope="col" | VIOLATION_COMMENT
 +
|-
 +
| 1889802
 +
| 2010-06-03
 +
| No Violations Noted
 +
|
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 1893303
 +
| 2010-06-16
 +
| No Violations Noted
 +
|
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 1910105
 +
| 2010-08-20
 +
| No Violations Noted
 +
| HORIZONTAL MARCELLUS, SAXON RIG -124 LANDING CURVE, TD ESTIMATED AT 11350', PITS AND E&S ARE GOOD.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 2131364
 +
| 2013-01-15
 +
| No Violations Noted
 +
| Notice of termination inspection.  All areas reclaimed and had at least 70% growth.  Well labeled, tanks in containment, ID sign up.Site stable.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 2239093
 +
| 2014-01-13
 +
| Violation(s) Noted
 +
| On Monday, January 13, 2014, the Department received a report about a spill that had occurred the previous day on XTOï¾’s Helen Bukovac #4H site; I investigated on January 14, 2014.
 +
 
 +
The site was a Marcellus well, some production equipment and two 210 bbl production tanks floating together for a total capacity of 420 bbl (17,640 gallon); these tanks contained primarily weak brine.
 +
Sometime during the night of January 11th and 12th the brine froze a valve causing #1 tank (the north tank) to fail.  The produce water went to containment, but, since the containment was earthen it seeped through to the outside.
 +
 
 +
XTO discovered the problem during the morning of the 12th, called the Department and initiated a response.  They closed in the wells, called in a vacuum truck that recovered 29 bbl of material and contracted an excavating company.  They were planning on excavating until tests indicated soil to background.  XTO also has plans to permanently remove the damaged tank.
 +
 
 +
 
 +
| 687336
 +
| 91.34A - Failure to take all necessary measures to prevent spill. Inadequate diking, potential pollution
 +
|
 +
|-
 +
|-
 +
| 2242810
 +
| 2014-01-23
 +
| Outstanding Violations - No Viols Req'd
 +
| On 1/24/2014, the Department conducted a follow -up inspection at the XTO Energy Incï¾’s Helen Bukovac 4H OG WELL in Dunbar Twp., Fayette County.
 +
 +
The purpose of the inspection was a follow - up to the spill that occurred on January 12, 2014.
 +
 
 +
There are 42 dumpsters full of material removed as the result of the spill.  10 dumpsters were at the well site and 32 were located up on a hill along the access road to the well.  The material removed so far was from inside the dike.
 +
 
 +
The tanks that leaked have been removed from the dike.
  
 +
|
 +
|
 +
|
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Oil and Gas Historical Inspection Report
 +
| publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2015-05-26
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources#Inspections
 +
| accessdate = 2015-05-27 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 22:00, 25 June 2015

Well Details

Well ID: 37-051-24328
Loading map...
County: Fayette
Municipality: Dunbar Township
Operator Name: XTO ENERGY INC
Well Pad ID: 148509
Farm/Lease Name: HELEN K BUKOVAC 4H
First Permit Date: 2010-03-12
Last Permit Date: 2010-03-12
Spud Date: 2010-05-26
Unconventional: Yes
Horizontal: Yes
Well Status: ACTIVE
Violations: 1
Latitude: 40.010133
Longitude: -79.672622

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2010-3 0.0 0.0 0.0 0.0 0.0 0.0
2010-2 143357.0 52.0 0.0 0.0 0.0 0.0
2010-2 143357.0 52.0 0.0 0.0 0.0 0.0
2011-1 475503.0 181.0 0.0 0.0 0.0 0.0
2011-2 296529.0 184.0 0.0 0.0 0.0 0.0
2012-1 231036.0 182.0 0.0 0.0 0.0 0.0
2012-2 196772.0 184.0 0.0 0.0 0.0 0.0
2013-1 168164.0 181.0 0.0 0.0 0.0 0.0
2013-2 154823.0 184.0 0.0 0.0 0.0 0.0
2014-1 75532.0 179.0 0.0 0.0 0.0 0.0
2014-2 146944.0 184.0 0.0 0.0 0.0 0.0
2015-02 10051.0 15.0 0.0 0.0 0.0 0.0
2015-01 16332.0 19.0 0.0 0.0 0.0 0.0
2015-03 21460.0 23.0 0.0 0.0 0.0 0.0

For data sources see[1]

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2010-2 PRODUCED FLUID 1.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PAR000519462 ADVANCED WASTE SERVICES OF PA LLC NEW CASTLE PA
2011-1 PRODUCED FLUID 2.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PAR000519462 ADVANCED WASTE SERVICES OF PA LLC NEW CASTLE PA
2011-1 PRODUCED FLUID 80.0 Bbl INJECTION DISPOSAL WELL 34-059-24067 DEVCO UNIT #1 (SWIW #11) CAMBRIDGE OH
2011-1 PRODUCED FLUID 219.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PBR RESERVED ENVIRONMENTAL SERVICES, LLC PITTSBURGH PA
2011-2 PRODUCED FLUID 200.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PAR000519462 ADVANCED WASTE SERVICES OF PA LLC NEW CASTLE PA
2011-2 PRODUCED FLUID 810.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0254185 RESERVED ENV SVC WASTE WATER TREATMENT FACILITY MOUNT PLEASANT PA
2011-2 PRODUCED FLUID 45.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE OF BRINE TO FRAC A WELL
2012-1 PRODUCED FLUID 92.0 Bbl INJECTION DISPOSAL WELL 34-133-24189 MEYERS #2 (SWIW #33) ATWATER OH
2012-1 PRODUCED FLUID 442.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0254185 RESERVED ENV SVC WASTE WATER TREATMENT FACILITY MOUNT PLEASANT PA
2012-2 PRODUCED FLUID 852.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0254185 RESERVED ENV SVC WASTE WATER TREATMENT FACILITY MOUNT PLEASANT PA
2012-2 PRODUCED FLUID 92.0 Bbl INJECTION DISPOSAL WELL 34-133-21076 SALTYS DISPOSAL - MYERS INECTION WELL #1 PARIS OH
2013-1 PRODUCED FLUID 398.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0254185 RESERVED ENV SVC WASTE WATER TREATMENT FACILITY MOUNT PLEASANT PA
2013-2 PRODUCED FLUID 294.0 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0254185 RESERVED ENV SVC WASTE WATER TREATMENT FACILITY MOUNT PLEASANT PA
2014-1 PRODUCED FLUID 110.0 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123NW009 RES WATER BUTLER PA
2014-1 PRODUCED FLUID 663.0 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0254185 RESERVED ENV SVC WASTE WATER TREATMENT FACILITY MOUNT PLEASANT PA
2014-2 PRODUCED FLUID 100.0 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123NW009 RES WATER BUTLER PA
2014-2 PRODUCED FLUID 177.0 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123SW005 RESERVED ENV SVC HEMPFIELD TWP RESIDUAL WASTE OPER PA

For data sources see[2]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
1889802 2010-06-03 No Violations Noted
1893303 2010-06-16 No Violations Noted
1910105 2010-08-20 No Violations Noted HORIZONTAL MARCELLUS, SAXON RIG -124 LANDING CURVE, TD ESTIMATED AT 11350', PITS AND E&S ARE GOOD.
2131364 2013-01-15 No Violations Noted Notice of termination inspection. All areas reclaimed and had at least 70% growth. Well labeled, tanks in containment, ID sign up.Site stable.
2239093 2014-01-13 Violation(s) Noted On Monday, January 13, 2014, the Department received a report about a spill that had occurred the previous day on XTOï¾’s Helen Bukovac #4H site; I investigated on January 14, 2014.

The site was a Marcellus well, some production equipment and two 210 bbl production tanks floating together for a total capacity of 420 bbl (17,640 gallon); these tanks contained primarily weak brine. Sometime during the night of January 11th and 12th the brine froze a valve causing #1 tank (the north tank) to fail. The produce water went to containment, but, since the containment was earthen it seeped through to the outside.

XTO discovered the problem during the morning of the 12th, called the Department and initiated a response. They closed in the wells, called in a vacuum truck that recovered 29 bbl of material and contracted an excavating company. They were planning on excavating until tests indicated soil to background. XTO also has plans to permanently remove the damaged tank.


687336 91.34A - Failure to take all necessary measures to prevent spill. Inadequate diking, potential pollution
2242810 2014-01-23 Outstanding Violations - No Viols Req'd On 1/24/2014, the Department conducted a follow -up inspection at the XTO Energy Incï¾’s Helen Bukovac 4H OG WELL in Dunbar Twp., Fayette County.

The purpose of the inspection was a follow - up to the spill that occurred on January 12, 2014.

There are 42 dumpsters full of material removed as the result of the spill. 10 dumpsters were at the well site and 32 were located up on a hill along the access road to the well. The material removed so far was from inside the dike.

The tanks that leaked have been removed from the dike.

For data sources see[3]

References