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Difference between revisions of "37-063-33231"

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[[Category:Wells]]

Revision as of 02:45, 29 June 2014

Well Details

Well ID: 37-063-33231
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Operator Name: KEYROCK ENERGY LLC
First Permit Date: 2002-10-11
Last Permit Date: 2002-10-11
Spud Date: 2003-03-07
Unconventional: No
Horizontal: No
Violations: None
Latitude: 40.489185
Longitude: -79.238351

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2013-0 238.0 365.0 0.0 0.0 0.0 0.0
2012-0 196.0 365.0 0.0 0.0 0.0 0.0
2010-0 501.0 365.0 0.0 0.0 0.0 0.0
2009-0 0.0 0.0 0.0 0.0 0.0 0.0
2008-0 6636.79 366.0 0.0 0.0 0.0 366.0
2006-0 1841.0 365.0 0.0 0.0 0.0 0.0
2005-0 2059.0 365.0 0.0 0.0 0.0 365.0
2004-0 3259.0 366.0 0.0 0.0 0.0 0.0
2003-0 3399.0 365.0 0.0 0.0 0.0 0.0
2002-0 0.0 0.0 0.0 0.0 0.0 0.0

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2003-0 BRINE 8184.0 Bbl TREATED ON-SITE, NPDES DISCHARGE BLACKLICK RIVER DISCHARGE
2003-0 FRACKING FLUID 160.0 Bbl BRINE OR INDUSTRIAL WASTE TREATMENT PLT WASTE TREATMENT CORP
2004-0 BRINE 6436.86 Bbl TREATED ON-SITE, NPDES DISCHARGE BLACKLICK RIVER DISCHARGE
2005-0 BRINE 7810.0 Bbl TREATED ON-SITE, NPDES DISCHARGE BLACKLICK RIVER DISCHARGE
2006-0 BRINE 8451.0 Bbl TREATED ON-SITE, NPDES DISCHARGE BLACKLICK RIVER DISCHARGE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID
1214497 2003-03-07 No Violations Noted LK Drilling Corp rigging up on location. Pit, Notification and E&S OK. Site inspection conducted with Mike Morgart P.G.
2020375 2011-11-16 No Violations Noted At the time of inspection, no E&S or IW issues. Well tag present. CBM well was in production. Pump jack and meter box present. Meter box showed a reading of 50/5 psi.

References