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Difference between revisions of "37-005-26293"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 37-005-26293
 
| Well ID: 37-005-26293
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.74696, -79.264712 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.746960, -79.264712 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Armstrong County, Pennsylvania|Armstrong]]
+
| Country: United States
 
|-
 
|-
| Municipality: [[Atwood Borough, Armstrong County, Pennsylvania|Atwood Borough]]
+
| State: Pennsylvania
 +
|-
 +
| County: [[Armstrong_County,_Pennsylvania|Armstrong]]
 +
|-
 +
| Municipality: [[Atwood Borough,_Armstrong_County,_Pennsylvania|Atwood Borough]]
 
|-
 
|-
 
| Operator Name: [[BLX INC]]
 
| Operator Name: [[BLX INC]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name: -
+
| Farm/Lease Name: JASON WICK #1
 
|-
 
|-
| First Permit Date: 2000-05-25
+
| License Status:  
 
|-
 
|-
| Last Permit Date: 2000-05-25
+
| Spud Date:  
 
|-
 
|-
| Spud Date: 2001-01-18
+
| Permit Date: 2000-05-25
 
|-
 
|-
| Unconventional: No
+
| Well Type: GAS
 
|-
 
|-
| Horizontal: No
+
| Unconventional Well: N
 
|-
 
|-
| Well Status: ACTIVE
+
| Configuration: Vertical Well
 
|-
 
|-
| Violations: 1
+
| Conservation: No
 
|-
 
|-
| Latitude: 40.74696
+
| Latitude: 40.746960
 
|-
 
|-
 
| Longitude: -79.264712
 
| Longitude: -79.264712
|-
 
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Permits Issued Detail Report
 +
|publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2019-05-20
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref><ref>{{cite web
 +
| title = Spud Data Report
 +
|publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2019-04-30
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-16 }}</ref><ref>{{cite web
 +
| title = Oil and Gas Well Pad Report
 +
|publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2019-05-20
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" | Date
!scope="col" | GAS QUANTITY
+
!scope="col" | Event
!scope="col" | GAS PRODUCTION DAYS
 
!scope="col" | CONDENSATE QUANTITY
 
!scope="col" | CONDENSATE PRODUCTION DAYS
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
 
|-
 
|-
| 2001-0
+
| 2000-05-25
| style="text-align:right;" | 20424.0
+
| New Permit Application
| style="text-align:right;" | 269.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
 
|-
 
|-
 +
| 2001-01-18
 +
| Performed Spud Operation
 
|-
 
|-
| 2002-0
+
|}
| style="text-align:right;" | 18794.0
+
For data sources see<ref>{{cite web
| style="text-align:right;" | 317.0
+
| title = Compiled from multiple data sources - see Pennsylvania Oil and Gas Data Sources
| style="text-align:right;" | 0.0
+
| date = 2020-02-27
| style="text-align:right;" | 0.0
+
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
| style="text-align:right;" | 0.0
+
| accessdate = 2020-02-27 }}</ref>
| style="text-align:right;" | 0.0
+
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Job Number
 +
!scope="col" | Job Start Date
 +
!scope="col" | Job End Date
 +
!scope="col" | True Vertical Depth (ft)
 +
!scope="col" | Total Water Volume (gal)
 +
!scope="col" | Total Non-Water Volume (gal)
 
|-
 
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Job Number
 +
!scope="col" | Trade Name
 +
!scope="col" | Supplier
 +
!scope="col" | Purpose
 +
!scope="col" | Ingredient Name
 +
!scope="col" | CAS Number
 +
!scope="col" | Additive Percentage by Mass
 +
!scope="col" | Job Percentage by Mass
 +
!scope="col" | Mass Used (lb)
 
|-
 
|-
| 2003-0
+
|}-->
| style="text-align:right;" | 15500.0
+
 
| style="text-align:right;" | 330.0
+
<!--== Stimulation Data ==
| style="text-align:right;" | 0.0
+
{| class="wikitable sortable" width="95%"
| style="text-align:right;" | 0.0
+
!scope="col" | Stimulation Date
| style="text-align:right;" | 0.0
+
!scope="col" | Phase Number
| style="text-align:right;" | 0.0
+
!scope="col" | Chemical Agent
 +
!scope="col" | Volume (gal)
 +
!scope="col" | Treating Pressure (psi)
 +
!scope="col" | Breakdown Pressure (psi)
 
|-
 
|-
 +
|}-->
 +
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Period
 +
!scope="col" | Operator Name
 +
!scope="col" | Gas Quantity (mcf)
 +
!scope="col" | Gas Production Days
 +
!scope="col" | Oil Quantity (bbl)
 +
!scope="col" | Oil Production Days
 +
!scope="col" | Water Quantity (bbl)
 +
!scope="col" | Water Production Days
 
|-
 
|-
| 2004-0
+
| 2001
| style="text-align:right;" | 14712.0
+
| [[BLX INC]]
| style="text-align:right;" | 359.0
+
| style="text-align: right;" | 20,424.00
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 269
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
| 2002
 +
| [[BLX INC]]
 +
| style="text-align: right;" | 18,794.00
 +
| style="text-align: right;" | 317
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2005-0
+
| 2003
| style="text-align:right;" | 13999.0
+
| [[BLX INC]]
| style="text-align:right;" | 365.0
+
| style="text-align: right;" | 15,500.00
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 330
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
| 2004
 +
| [[BLX INC]]
 +
| style="text-align: right;" | 14,712.00
 +
| style="text-align: right;" | 359
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2006-0
+
| 2005
| style="text-align:right;" | 12082.0
+
| [[BLX INC]]
| style="text-align:right;" | 349.0
+
| style="text-align: right;" | 13,999.00
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
| 2006
 +
| [[BLX INC]]
 +
| style="text-align: right;" | 12,082.00
 +
| style="text-align: right;" | 349
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2007-0
+
| 2007
| style="text-align:right;" | 11581.0
+
| [[BLX INC]]
| style="text-align:right;" | 355.0
+
| style="text-align: right;" | 11,581.00
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 355
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
| 2008
 +
| [[BLX INC]]
 +
| style="text-align: right;" | 11,128.00
 +
| style="text-align: right;" | 345
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2008-0
+
| 2009
| style="text-align:right;" | 11128.0
+
| [[BLX INC]]
| style="text-align:right;" | 345.0
+
| style="text-align: right;" | 9,919.00
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 353
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
| 2010
 +
| [[BLX INC]]
 +
| style="text-align: right;" | 8,978.14
 +
| style="text-align: right;" | 362
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2009-0
+
| 2011
| style="text-align:right;" | 9919.0
+
| [[BLX INC]]
| style="text-align:right;" | 353.0
+
| style="text-align: right;" | 8,798.63
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 343
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
| 2012
 +
| [[BLX INC]]
 +
| style="text-align: right;" | 8,615.84
 +
| style="text-align: right;" | 354
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2010-0
+
| 2013
| style="text-align:right;" | 8978.14
+
| [[BLX INC]]
| style="text-align:right;" | 362.0
+
| style="text-align: right;" | 8,675.50
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 351
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
| 2014
 +
| [[BLX INC]]
 +
| style="text-align: right;" | 7,744.86
 +
| style="text-align: right;" | 353
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2011-0
+
| 2015
| style="text-align:right;" | 8798.63
+
| [[BLX INC]]
| style="text-align:right;" | 343.0
+
| style="text-align: right;" | 7,766.14
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 351
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
| 2016
 +
| [[BLX INC]]
 +
| style="text-align: right;" | 7,498.13
 +
| style="text-align: right;" | 352
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2012-0
+
| 2017
| style="text-align:right;" | 8615.84
+
| [[BLX INC]]
| style="text-align:right;" | 354.0
+
| style="text-align: right;" | 7,098.89
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 363
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
| 2018
 +
| [[BLX INC]]
 +
| style="text-align: right;" | 7,293.81
 +
| style="text-align: right;" | 361
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2013-0
+
| 2019
| style="text-align:right;" | 8675.5
+
| [[BLX INC]]
| style="text-align:right;" | 351.0
+
| style="text-align: right;" | 6,741.31
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 363
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
|-
+
| style="text-align: right;" | 0
|-
 
| 2014-0
 
| style="text-align:right;" | 7744.86
 
| style="text-align:right;" | 353.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Oil and Gas Historical Production Report
+
  | title =Oil and Gas Production Reports
| publisher = [[Pennsylvania Department of Environmental Protection]]
+
|publisher = [[Pennsylvania Department of Environmental Protection]]
| date = 2015-05-26
+
| date = 2019-03-31
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources#Production
+
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
  | accessdate = 2015-05-27 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
 
== Waste Data ==
 
== Waste Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" | Period
!scope="col" | TYPE
+
!scope="col" | Operator
!scope="col" | QUANTITY
+
!scope="col" | Waste Type
!scope="col" | UNITS
+
!scope="col" | Quantity
!scope="col" | DISPOSAL METHOD
+
!scope="col" | Disposal Method
!scope="col" | WASTE FACILITY PERMIT ID
+
!scope="col" | Waste Facility ID
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
 
|-
 
|-
| 2014-0
+
| 2014
| PRODUCED FLUID
+
| [[BLX INC]]
| style="text-align:right;" | 35.0
+
| Produced Fluid
| Bbl
+
| style="text-align: right;" | 35.00 Bbl
 
| CENT WASTE TRT FAC NPDES DISCHARGE
 
| CENT WASTE TRT FAC NPDES DISCHARGE
 
| PA0095443
 
| PA0095443
| CREEKSIDE TREATMENT FACILITY
+
|-
| CREEKSIDE
+
| 2014
| PA
+
| [[BLX INC]]
 +
| Produced Fluid
 +
| style="text-align: right;" | 35 Bbl
 +
| CENT WASTE TRT FAC NPDES
 +
| PA0095443
 +
|-
 +
| 2015
 +
| [[BLX INC]]
 +
| Produced Fluid
 +
| style="text-align: right;" | 45 Bbl
 +
| CENT WASTE TRT FAC NPDES
 +
| PA0095273
 +
|-
 +
| 2015
 +
| [[BLX INC]]
 +
| Produced Fluid
 +
| style="text-align: right;" | 45.00 Bbl
 +
| CENT WASTE TRT FAC NPDES DISCHARGE
 +
| PA0095273
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Oil and Gas Historical Waste Report
+
  | title =Oil and Gas Waste Reports
| publisher = [[Pennsylvania Department of Environmental Protection]]
+
|publisher = [[Pennsylvania Department of Environmental Protection]]
| date = 2015-05-26
+
| date = 2019-03-31
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources#Waste
+
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
  | accessdate = 2015-05-26 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" | Inspection ID
!scope="col" | DATE
+
!scope="col" | Inspection Category
!scope="col" | DESCRIPTION
+
!scope="col" | Inspection Date
!scope="col" | COMMENT
+
!scope="col" | Inspection Type
!scope="col" | VIOLATION ID
+
!scope="col" | Inspection Result
!scope="col" | VIOLATION CODE
+
!scope="col" | Inspection Comments
!scope="col" | VIOLATION_COMMENT
 
 
|-
 
|-
 
| 1170287
 
| 1170287
 +
| Primary Facility
 
| 2002-09-23
 
| 2002-09-23
 +
| Routine/Complete Inspection
 
| No Violations Noted
 
| No Violations Noted
 
| Producing gas. Tag and e&s ok.
 
| Producing gas. Tag and e&s ok.
|
 
|
 
|
 
 
|-
 
|-
 +
| 2372073
 +
| Primary Facility
 +
| 2015-05-20
 +
| Complaint Inspection
 +
| Violation(s) Noted
 +
| Inspection was performed as a follow-up an anonymous complaint outlining a discharge of production fluids to the ground.  Preliminary phone conversation with BLX representative Tom Bock confirmed that work had been performed at the well recently, i.e. the removal of the brine tank.  A field inspection of the site by WQS Higgins found evidence that a discharge of some sort had ocured recently at the well-site.  There was an area immediately downslope of the well apparatus, and former location of the brine tank, stretching for apprximately 30 feet which had been recently regraded and mulched.  Additionally Mr. Bock informed WQS Higgins via phone and e-mail that he had spoken with the complainant, both prior to the filing of the complaint and after.  Mr. Bock agreed with WQS Higgins that a discharge of some sort had ocurred and that BLX would be undertaking measures directly to begin addressing the affected area.  Mr. Bock stated via phone that the remediation process would most likley begin early the following week, after the Memorial Day Holiday.
 +
|-
 +
| 2425208
 +
| Primary Facility
 +
| 2015-11-17
 +
| Compliance Evaluation
 +
| No Violations Noted
 +
| Well appeared to be equipped for production.  The area affected by the discharge had been excavated, removed and restored.  The restored area had vegtation attaining 70% uniform coverage.
 +
|-
 +
|}
 +
==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Inspection ID
 +
!scope="col" | Violation ID
 +
!scope="col" | Violation Date
 +
!scope="col" | Date Resolved
 +
!scope="col" | Violation Code
 +
!scope="col" | Violation Type
 +
!scope="col" | Violation Comments
 
|-
 
|-
 
| 2372073
 
| 2372073
 +
| 723634
 +
| 05/20/2015
 
| 2015-05-20
 
| 2015-05-20
| Violation(s) Noted
+
| 78.57(a) - CONTROL, STORAGE AND DISPOSAL OF PRODUCTION FLUIDS - Operator failed to collect the brine and other fluids produced during operation, service and plugging of the well in a tank, pit or a series of pits or tanks, or other device approved by
| Inspection was performed as a follow-up an anonymous complaint outlining a discharge of production fluids to the ground. Preliminary phone conversation with BLX representative Tom Bock confirmed that work had been performed at the well recently
+
| Environmental Health & Safety
 +
|
 +
|-
 +
|}
 +
==== Penalties Applied ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Violation ID
 +
!scope="col" | Penalty ID
 +
!scope="col" | Penalty Code
 +
!scope="col" | Penalty Status
 +
!scope="col" | Penalty Date
 +
!scope="col" | Enforcement Date
 +
!scope="col" | Penalty Amount
 +
!scope="col" | Amount Collected
 +
|-
 
| 723634
 
| 723634
| 78.57(a) - CONTROL
+
| 323571
| service and plugging of the well in a tank
+
| NOV - Notice of Violation
 +
| Comply/Closed
 +
|
 +
| 2015-12-02
 +
| style="text-align: right;" |
 +
| style="text-align: right;" |
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Oil and Gas Historical Inspection Report
+
  | title =Oil and Gas Compliance Report
| publisher = [[Pennsylvania Department of Environmental Protection]]
+
|publisher = [[Pennsylvania Department of Environmental Protection]]
| date = 2015-05-26
+
| date = 2019-05-20
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources#Inspections
+
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
  | accessdate = 2015-05-27 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Pennsylvania Wells]]

Latest revision as of 02:33, 21 May 2020

Well Details

Well ID: 37-005-26293
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Country: United States
State: Pennsylvania
County: Armstrong
Municipality: Atwood Borough
Operator Name: BLX INC
Well Pad ID:
Farm/Lease Name: JASON WICK #1
License Status:
Spud Date:
Permit Date: 2000-05-25
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.746960
Longitude: -79.264712

For data sources see[1][2][3]

Well History

Date Event
2000-05-25 New Permit Application
2001-01-18 Performed Spud Operation

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2001 BLX INC 20,424.00 269 0.00 0 0.00 0
2002 BLX INC 18,794.00 317 0.00 0 0.00 0
2003 BLX INC 15,500.00 330 0.00 0 0.00 0
2004 BLX INC 14,712.00 359 0.00 0 0.00 0
2005 BLX INC 13,999.00 365 0.00 0 0.00 0
2006 BLX INC 12,082.00 349 0.00 0 0.00 0
2007 BLX INC 11,581.00 355 0.00 0 0.00 0
2008 BLX INC 11,128.00 345 0.00 0 0.00 0
2009 BLX INC 9,919.00 353 0.00 0 0.00 0
2010 BLX INC 8,978.14 362 0.00 0 0.00 0
2011 BLX INC 8,798.63 343 0.00 0 0.00 0
2012 BLX INC 8,615.84 354 0.00 0 0.00 0
2013 BLX INC 8,675.50 351 0.00 0 0.00 0
2014 BLX INC 7,744.86 353 0.00 0 0.00 0
2015 BLX INC 7,766.14 351 0.00 0 0.00 0
2016 BLX INC 7,498.13 352 0.00 0 0.00 0
2017 BLX INC 7,098.89 363 0.00 0 0.00 0
2018 BLX INC 7,293.81 361 0.00 0 0.00 0
2019 BLX INC 6,741.31 363 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2014 BLX INC Produced Fluid 35.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095443
2014 BLX INC Produced Fluid 35 Bbl CENT WASTE TRT FAC NPDES PA0095443
2015 BLX INC Produced Fluid 45 Bbl CENT WASTE TRT FAC NPDES PA0095273
2015 BLX INC Produced Fluid 45.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1170287 Primary Facility 2002-09-23 Routine/Complete Inspection No Violations Noted Producing gas. Tag and e&s ok.
2372073 Primary Facility 2015-05-20 Complaint Inspection Violation(s) Noted Inspection was performed as a follow-up an anonymous complaint outlining a discharge of production fluids to the ground. Preliminary phone conversation with BLX representative Tom Bock confirmed that work had been performed at the well recently, i.e. the removal of the brine tank. A field inspection of the site by WQS Higgins found evidence that a discharge of some sort had ocured recently at the well-site. There was an area immediately downslope of the well apparatus, and former location of the brine tank, stretching for apprximately 30 feet which had been recently regraded and mulched. Additionally Mr. Bock informed WQS Higgins via phone and e-mail that he had spoken with the complainant, both prior to the filing of the complaint and after. Mr. Bock agreed with WQS Higgins that a discharge of some sort had ocurred and that BLX would be undertaking measures directly to begin addressing the affected area. Mr. Bock stated via phone that the remediation process would most likley begin early the following week, after the Memorial Day Holiday.
2425208 Primary Facility 2015-11-17 Compliance Evaluation No Violations Noted Well appeared to be equipped for production. The area affected by the discharge had been excavated, removed and restored. The restored area had vegtation attaining 70% uniform coverage.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2372073 723634 05/20/2015 2015-05-20 78.57(a) - CONTROL, STORAGE AND DISPOSAL OF PRODUCTION FLUIDS - Operator failed to collect the brine and other fluids produced during operation, service and plugging of the well in a tank, pit or a series of pits or tanks, or other device approved by Environmental Health & Safety

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
723634 323571 NOV - Notice of Violation Comply/Closed 2015-12-02

For data sources see[7]

References