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Difference between revisions of "37-125-28571"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 37-125-28571
 
| Well ID: 37-125-28571
| style="height=100%; align=center" rowspan="14" | {{#display_map: 40.197581, -80.189806 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.197581, -80.189806 | width=100% | height=100% }}
 
|-
 
|-
 
| Country: United States
 
| Country: United States
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| Spud Date:  
 
| Spud Date:  
 
|-
 
|-
| Permit Date: 5/29/2018
+
| Permit Date: 2018-05-29
 +
|-
 +
| Well Type: GAS
 
|-
 
|-
 
| Unconventional Well: Y
 
| Unconventional Well: Y
 
|-
 
|-
 
| Configuration: Horizontal Well
 
| Configuration: Horizontal Well
 +
|-
 +
| Conservation: Yes
 
|-
 
|-
 
| Latitude: 40.197581
 
| Latitude: 40.197581
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  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | accessdate = 2019-05-21 }}</ref>
 
  | accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Date
 +
!scope="col" | Event
 +
|-
 +
| 2018-05-29
 +
| New Permit Application
 +
|-
 +
| 2019-05-15
 +
| Permit Renewal Application
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Compiled from multiple data sources - see Pennsylvania Oil and Gas Data Sources
 +
| date = 2020-02-27
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-02-27 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Job Number
 +
!scope="col" | Job Start Date
 +
!scope="col" | Job End Date
 +
!scope="col" | True Vertical Depth (ft)
 +
!scope="col" | Total Water Volume (gal)
 +
!scope="col" | Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Job Number
 +
!scope="col" | Trade Name
 +
!scope="col" | Supplier
 +
!scope="col" | Purpose
 +
!scope="col" | Ingredient Name
 +
!scope="col" | CAS Number
 +
!scope="col" | Additive Percentage by Mass
 +
!scope="col" | Job Percentage by Mass
 +
!scope="col" | Mass Used (lb)
 +
|-
 +
|}-->
 +
 +
<!--== Stimulation Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Stimulation Date
 +
!scope="col" | Phase Number
 +
!scope="col" | Chemical Agent
 +
!scope="col" | Volume (gal)
 +
!scope="col" | Treating Pressure (psi)
 +
!scope="col" | Breakdown Pressure (psi)
 +
|-
 +
|}-->
 +
 
<!--== Production Data ==
 
<!--== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
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{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | Period
 
!scope="col" | Period
 +
!scope="col" | Operator
 
!scope="col" | Waste Type
 
!scope="col" | Waste Type
 
!scope="col" | Quantity
 
!scope="col" | Quantity
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  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | accessdate = 2019-05-21 }}</ref>
 
  | accessdate = 2019-05-21 }}</ref>
<!--== Fracking Activities ==
 
==== Fracking Jobs ====
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | Job Number
 
!scope="col" | Job Start Date
 
!scope="col" | Job End Date
 
!scope="col" | True Vertical Depth (ft)
 
!scope="col" | Total Water Volume (gal)
 
!scope="col" | Total Non-Water Volume (gal)
 
|-
 
|}-->
 
<!--==== Fluid Composition Data ====
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | Job Number
 
!scope="col" | Trade Name
 
!scope="col" | Supplier
 
!scope="col" | Purpose
 
!scope="col" | Ingredient Name
 
!scope="col" | CAS Number
 
!scope="col" | Additive Percentage by Mass
 
!scope="col" | Job Percentage by Mass
 
!scope="col" | Mass Used (lb)
 
|-
 
|}-->
 
 
 
==References==
 
==References==
 
<references/>
 
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Pennsylvania Wells]]
 
[[Category:Pennsylvania Wells]]

Latest revision as of 16:00, 15 May 2020

Well Details

Well ID: 37-125-28571
Loading map...
Country: United States
State: Pennsylvania
County: Washington
Municipality: South Strabane Township
Operator Name: RANGE RESOURCES APPALACHIA LLC
Well Pad ID: 153759
Farm/Lease Name: MUNCE WILLIAM 10060 12H
License Status:
Spud Date:
Permit Date: 2018-05-29
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: Yes
Latitude: 40.197581
Longitude: -80.189806

For data sources see[1][2][3]

Well History

Date Event
2018-05-29 New Permit Application
2019-05-15 Permit Renewal Application

For data sources see[4]



Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2749427 Primary Facility 2018-06-19 Compliance Evaluation No Violations Noted On 6/14/2018, a follow up inspection was conducted in response to an operator reported spill (CTS ID: 334975), the following was observed:

>>Three roll off boxes remained on site at the time of inspection in the immediate vicinity of the area of the spill. The excavation for the spill cleanup remained open and was partially filled with water. Field testing of the water indicated normal ground water conductivity between 300-500µS. Cleanup appears to be in compliance with policy. No violation.

2753838 Primary Facility 2018-07-18 Routine/Partial Inspection In Compliance with Policy On 7/16/2018 at 1712, a spill was reported to the PA DEP hotline by Range Resources which had occurred at 1600 on 7/16/2018. On 7/18/2018 at approximately 0930, I conducted an incident response inspection. I met with Nicholas Reda (Range Resources) to discuss the incident and associated remediation.

Approximately 10 gallons of produced water were released to the graveled well pad under previously set containment. The cause of the release remains unknown. Specialized Professional Services Inc. (SPSI) responded and remediated the impacted area placing it into one roll-off box.

The wells on site were clearly marked and within secondary containment. The production fluid/condensate tanks were within secondary containment and appeared to be in good condition. The GPUs on site appeared to be in good condition and had secondary containment.

The spill was addressed in compliance with the spill policy.

2825861 Primary Facility 2019-01-11 Compliance Evaluation No Violations Noted On 1/11/19 a compliance evaluation inspection of the Munce Site was conducted in response to violations noted on 6/14/18. The following was observed:

>>No residual impact was found in the area of the spill.

>>The site was found to be in good condition with no violations found.

>>Minimal activity was viewed on site at the time of inspection.

For data sources see[5]

References