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Difference between revisions of "34-031-22317"

m
 
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Line 3: Line 3:
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-031-22317
 
| Well ID: 34-031-22317
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.1722464206, -82.0823025529 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.17239082, -82.08174813 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Coshocton County, Ohio|Coshocton]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[KNOX ENERGY INC.]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 1974-04-09
 
| Spud Date: 1974-04-09
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Plugged and Abandoned
 
|-
 
|-
| Violations: 2
+
| Violations: 0
 
|-
 
|-
| Latitude: 40.1722464206
+
| Latitude: 40.17239082
 
|-
 
|-
| Longitude: -82.0823025529
+
| Longitude: -82.08174813
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 1984-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 301.0
 +
|
 +
|-
 +
|-
 +
| 1985-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 227.0
 +
|
 +
|-
 +
|-
 +
| 1986-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 262.0
 +
|
 +
|-
 +
|-
 +
| 1987-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 225.0
 +
|
 +
|-
 +
|-
 +
| 1988-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 220.0
 +
|
 +
|-
 +
|-
 +
| 1989-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 190.0
 +
|
 +
|-
 +
|-
 +
| 1990-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 185.0
 +
|
 +
|-
 +
|-
 +
| 1992-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 209.0
 +
|
 +
|-
 +
|-
 +
| 1993-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 77.0
 +
|
 +
|-
 +
|-
 +
| 1994-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 150.0
 +
|
 +
|-
 +
|-
 +
| 1995-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 96.0
 +
|
 +
|-
 +
|-
 +
| 1996-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 143.0
 +
|
 +
|-
 +
|-
 +
| 1997-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 130.0
 +
|
 +
|-
 +
|-
 +
| 1998-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 148.0
 +
|
 +
|-
 +
|-
 +
| 1999-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 70.0
 +
|
 +
|-
 +
|-
 +
| 2000-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 120.0
 +
|
 +
|-
 +
|-
 +
| 2001-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 120.0
 +
|
 +
|-
 +
|-
 +
| 2002-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 120.0
 +
|
 +
|-
 +
|-
 +
| 2003-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 120.0
 +
|
 +
|-
 +
|-
 +
| 2004-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 65.0
 +
|
 +
|-
 +
|-
 +
| 2005-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 100.0
 +
|
 +
|-
 +
|-
 +
| 2006-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 100.0
 +
|
 +
|-
 +
|-
 +
| 2007-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 80.0
 +
|
 +
|-
 +
|-
 +
| 2008-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 40.0
 +
|
 +
|-
 +
|-
 +
| 2009-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 70.0
 +
|
 +
|-
 +
|-
 +
| 2011-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 78.0
 +
|
 +
|-
 +
|-
 +
| 2012-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 28.0
 +
|
 +
|-
 +
|-
 +
| 2013-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2014-0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 319:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
 
| -1005357698
 
| -1005357698
 
| 2014-03-12
 
| 2014-03-12
|
+
|  
| On the day of my inspection I found that the clay was sitting firm approximately one foot down after settling overnight. Knox Energy cut the conductor casing off approximately 30" below grade and capped the casing with a steel plate inscribed with 2317.
+
| On the day of my inspection I found that the clay was sitting firm approximately one foot down after settling overnight. Knox Energy cut the conductor casing off approximately 30 below grade and capped the casing with a steel plate inscribed with 2317.
|
+
|  
|
+
|  
|
+
| Compliance Notice
 
|-
 
|-
 
|-
 
|-
 
| -1091325694
 
| -1091325694
 
| 2014-03-05
 
| 2014-03-05
|
+
|  
 
| Berry Well Service fished their lost tools out of the hole. Then they pulled production casing to the top of the Big Lime.
 
| Berry Well Service fished their lost tools out of the hole. Then they pulled production casing to the top of the Big Lime.
|
+
|  
|
+
|  
|
+
|  
|-
 
|-
 
| -72487718
 
| 2005-03-16
 
|
 
| Oil around motor on pumping unit . Lead line repaired no clean up at leak . Well head and storage tank not identified .
 
|
 
| 9-1-07
 
|
 
|-
 
|-
 
| -72487718
 
| 2005-03-16
 
|
 
| Oil around motor on pumping unit . Lead line repaired no clean up at leak . Well head and storage tank not identified .
 
|
 
| 9-9-05(A)10
 
|
 
|-
 
|-
 
| -726132751
 
| 2014-03-07
 
|
 
| On the day of my inspection Berry Well Service attempted to pull the 8.625" casing with no success. They got a telegraph at 460' and attempted to part the casing with no success.
 
|
 
|
 
|
 
 
|-
 
|-
 
|-
 
|-
 
| 1127843307
 
| 1127843307
 
| 2005-09-27
 
| 2005-09-27
|
+
|  
 
| Well in production , old line leak approximately 200' from well , needs contaminated soil removed  (5' Area .)
 
| Well in production , old line leak approximately 200' from well , needs contaminated soil removed  (5' Area .)
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1314591440
 
| 1314591440
 
| 2014-03-11
 
| 2014-03-11
|
+
|  
| On the day of my inspection Berry Well Service pulled 454' of 8.625" casing from the well. They washed approximately 12 more tons of clay down the well, filling it to surface. It will be allowed to settle overnight. Knox Energy removed all of the tank battery components and pulled all of the flow line from the tank battery back to the well.
+
| On the day of my inspection Berry Well Service pulled 454' of 8.625 casing from the well. They washed approximately 12 more tons of clay down the well, filling it to surface. It will be allowed to settle overnight. Knox Energy removed all of the tank battery components and pulled all of the flow line from the tank battery back to the well.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1393540792
 
| 1393540792
 
| 2014-02-27
 
| 2014-02-27
|
+
|  
 
| On the day of my inspection I found that Berry Well Service was pulling rods and tubing. They will run in to tag the top of the fluid to determine the method used to set the bottom plug.
 
| On the day of my inspection I found that Berry Well Service was pulling rods and tubing. They will run in to tag the top of the fluid to determine the method used to set the bottom plug.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1393858620
 
| 1393858620
 
| 2014-03-03
 
| 2014-03-03
|
+
|  
| The records for this well show that the production casing is a mixed string of 4.5" and 5.5" casing. Berry Well Service ran in with their 5.5" ripping tool and tagged the top of the 4.5" at 720'. Then they ran back in with their 4.5" tools and got to the bottom. They determined that the fluid level was only 300' up from bottom.
+
| The records for this well show that the production casing is a mixed string of 4.5 and 5.5 casing. Berry Well Service ran in with their 5.5 ripping tool and tagged the top of the 4.5 at 720'. Then they ran back in with their 4.5 tools and got to the bottom. They determined that the fluid level was only 300' up from bottom.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1394110117
 
| 1394110117
 
| 2014-03-04
 
| 2014-03-04
|
+
|  
 
| On the day of my inspection Berry Well Service washed two tons of clay down the production casing. They got a telegraph at 3070' and ripped the casing. They lost their ripping tools down hole when they were coming out.
 
| On the day of my inspection Berry Well Service washed two tons of clay down the production casing. They got a telegraph at 3070' and ripped the casing. They lost their ripping tools down hole when they were coming out.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1394546283
 
| 1394546283
 
| 2014-03-10
 
| 2014-03-10
|
+
|  
| On the day of my inspection I found that Berry Well Service was successful at ripping the 8.625" and they started to pull it from the well.
+
| On the day of my inspection I found that Berry Well Service was successful at ripping the 8.625 and they started to pull it from the well.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1573436889
 
| 1573436889
 
| 2006-07-10
 
| 2006-07-10
|
+
|  
 
| Compliance
 
| Compliance
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 566346427
 
| 566346427
 
| 2004-02-04
 
| 2004-02-04
|
+
|  
 
| Well pumping
 
| Well pumping
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -72487718
 +
| 2005-03-16
 +
|
 +
| Oil around motor on pumping unit . Lead line repaired no clean up at leak . Well head and storage tank not identified .
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -726132751
 +
| 2014-03-07
 +
|
 +
| On the day of my inspection Berry Well Service attempted to pull the 8.625 casing with no success. They got a telegraph at 460' and attempted to part the casing with no success.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 945678683
 
| 945678683
 
| 2014-03-06
 
| 2014-03-06
|
+
|  
 
| On the day of my inspection I found that Berry Well Service had pulled the production casing up to 2283', at which point they washed 10 more tons of clay into the well. They pulled the remaining production casing from the well. Then they set a pre-cast cement plug at 1180' and washed 5 tons of clay down the well.
 
| On the day of my inspection I found that Berry Well Service had pulled the production casing up to 2283', at which point they washed 10 more tons of clay into the well. They pulled the remaining production casing from the well. Then they set a pre-cast cement plug at 1180' and washed 5 tons of clay down the well.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 13:58, 16 July 2015

Well Details

Well ID: 34-031-22317
Loading map...
County: Coshocton
Municipality:
Operator Name: KNOX ENERGY INC.
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1974-04-09
Unconventional: No
Configuration: Vertical
Well Status: Plugged and Abandoned
Violations: 0
Latitude: 40.17239082
Longitude: -82.08174813

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 0.0 301.0
1985-0 0.0 227.0
1986-0 0.0 262.0
1987-0 0.0 225.0
1988-0 0.0 220.0
1989-0 0.0 190.0
1990-0 0.0 185.0
1992-0 0.0 209.0
1993-0 0.0 77.0
1994-0 0.0 150.0
1995-0 0.0 96.0
1996-0 0.0 143.0
1997-0 0.0 130.0
1998-0 0.0 148.0
1999-0 0.0 70.0
2000-0 0.0 120.0
2001-0 0.0 120.0
2002-0 0.0 120.0
2003-0 0.0 120.0
2004-0 0.0 65.0
2005-0 0.0 100.0
2006-0 0.0 100.0
2007-0 0.0 80.0
2008-0 0.0 40.0
2009-0 0.0 70.0
2011-0 0.0 78.0
2012-0 0.0 28.0
2013-0 0.0 0.0
2014-0 0.0 0.0 0.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1005357698 2014-03-12 On the day of my inspection I found that the clay was sitting firm approximately one foot down after settling overnight. Knox Energy cut the conductor casing off approximately 30 below grade and capped the casing with a steel plate inscribed with 2317. Compliance Notice
-1091325694 2014-03-05 Berry Well Service fished their lost tools out of the hole. Then they pulled production casing to the top of the Big Lime.
1127843307 2005-09-27 Well in production , old line leak approximately 200' from well , needs contaminated soil removed (5' Area .)
1314591440 2014-03-11 On the day of my inspection Berry Well Service pulled 454' of 8.625 casing from the well. They washed approximately 12 more tons of clay down the well, filling it to surface. It will be allowed to settle overnight. Knox Energy removed all of the tank battery components and pulled all of the flow line from the tank battery back to the well.
1393540792 2014-02-27 On the day of my inspection I found that Berry Well Service was pulling rods and tubing. They will run in to tag the top of the fluid to determine the method used to set the bottom plug.
1393858620 2014-03-03 The records for this well show that the production casing is a mixed string of 4.5 and 5.5 casing. Berry Well Service ran in with their 5.5 ripping tool and tagged the top of the 4.5 at 720'. Then they ran back in with their 4.5 tools and got to the bottom. They determined that the fluid level was only 300' up from bottom.
1394110117 2014-03-04 On the day of my inspection Berry Well Service washed two tons of clay down the production casing. They got a telegraph at 3070' and ripped the casing. They lost their ripping tools down hole when they were coming out.
1394546283 2014-03-10 On the day of my inspection I found that Berry Well Service was successful at ripping the 8.625 and they started to pull it from the well.
1573436889 2006-07-10 Compliance
566346427 2004-02-04 Well pumping
-72487718 2005-03-16 Oil around motor on pumping unit . Lead line repaired no clean up at leak . Well head and storage tank not identified .
-726132751 2014-03-07 On the day of my inspection Berry Well Service attempted to pull the 8.625 casing with no success. They got a telegraph at 460' and attempted to part the casing with no success.
945678683 2014-03-06 On the day of my inspection I found that Berry Well Service had pulled the production casing up to 2283', at which point they washed 10 more tons of clay into the well. They pulled the remaining production casing from the well. Then they set a pre-cast cement plug at 1180' and washed 5 tons of clay down the well.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.