X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

Difference between revisions of "34-067-20600"

m
 
m
Line 3: Line 3:
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-067-20600
 
| Well ID: 34-067-20600
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.2028837057, -81.2798208714 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.20288371, -81.27982087 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Harrison County, Ohio|Harrison]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[EXCO - NORTH COAST ENERGY INC]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 1983-02-06
 
| Spud Date: 1983-02-06
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Final Restoration
 
|-
 
|-
 
| Violations: 0
 
| Violations: 0
 
|-
 
|-
| Latitude: 40.2028837057
+
| Latitude: 40.20288371
 
|-
 
|-
| Longitude: -81.2798208714
+
| Longitude: -81.27982087
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 1985-0
 +
| style="text-align:right;" | 28942.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 100.0
 +
|
 +
|-
 +
|-
 +
| 1987-0
 +
| style="text-align:right;" | 9558.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 116.0
 +
|
 +
|-
 +
|-
 +
| 1988-0
 +
| style="text-align:right;" | 4862.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1989-0
 +
| style="text-align:right;" | 2085.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 81.0
 +
|
 +
|-
 +
|-
 +
| 1990-0
 +
| style="text-align:right;" | 1191.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1991-0
 +
| style="text-align:right;" | 907.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1992-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1993-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1994-0
 +
| style="text-align:right;" | 121.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1995-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1996-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1997-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1998-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1999-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2000-0
 +
| style="text-align:right;" | 273.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2001-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2002-0
 +
| style="text-align:right;" | 82.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 211:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
|-
 
| -1155455712
 
| 2002-12-11
 
|
 
|  On location to witness plug job . Waited on location and nobody showed up to plug the well while I was on location . Departed location and went to the New Philadelphia office . Talked with Inspector Mark Moreland and he advised that he had talked with North Coast personel and they advised that they are going to plug the well tomorrow .
 
|
 
|
 
|
 
|-
 
|-
 
| -1338394820
 
| 2002-12-04
 
|
 
| W /O Operator to arrive and after contacting their office I found that job had been cancelled for today .
 
|
 
|
 
|
 
|-
 
|-
 
| -1701414275
 
| 2002-12-11
 
|
 
|  On location to witness plug job . Waited on location and nobody showed up to plug the well while I was on location . Departed location and went to the New Philadelphia office . Talked with Inspector Mark Moreland and he advised that he had talked with North Coast personel and they advised that they are going to plug the well tomorrow .
 
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1039704373
 
| 1039704373
 
| 2002-11-18
 
| 2002-11-18
|
+
|  
 
| Arrive to check on site after an explosion had occorred at wellsite . Found that the 8 inch casing appears to have collapsed and landed on the heavy wall conductor pipe with enough force to bell it outward . The well is not leaking badly at this time , there is  reading of 18 TO 20 PPM H 2 S . Found that the operator is not going to arrive any time soon .
 
| Arrive to check on site after an explosion had occorred at wellsite . Found that the 8 inch casing appears to have collapsed and landed on the heavy wall conductor pipe with enough force to bell it outward . The well is not leaking badly at this time , there is  reading of 18 TO 20 PPM H 2 S . Found that the operator is not going to arrive any time soon .
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1039711345
 
| 1039711345
 
| 2002-12-03
 
| 2002-12-03
|
+
|  
 
| Rig  is over the hole and is going in with tubing and will try and circulate well . Next rig had equipment problem and will reschedule work for Weds. Or Thurs.Review well with Inspector Grimm due to H 2S readings .
 
| Rig  is over the hole and is going in with tubing and will try and circulate well . Next rig had equipment problem and will reschedule work for Weds. Or Thurs.Review well with Inspector Grimm due to H 2S readings .
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -1155455712
 +
| 2002-12-11
 +
|
 +
| On location to witness plug job . Waited on location and nobody showed up to plug the well while I was on location . Departed location and went to the New Philadelphia office . Talked with Inspector Mark Moreland and he advised that he had talked with North Coast personel and they advised that they are going to plug the well tomorrow .
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 1237972050
 
| 1237972050
 
| 2002-11-19
 
| 2002-11-19
|
+
|  
 
| W/O operator to arrive and again a no show ?
 
| W/O operator to arrive and again a no show ?
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1287640570
 
| 1287640570
 
| 2002-12-12
 
| 2002-12-12
|
+
|  
| On location to witness plug job . The plug job was cancelled again today . Departed the location and went to the New Philadelphia office . I was advised by phone that they aren't going to plug the well until next week .
+
| On location to witness plug job . The plug job was cancelled again today . Departed the location and went to the New Philadelphia office . I was advised by phone that they aren't going to plug the well until next week .
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -1338394820
 +
| 2002-12-04
 +
|
 +
| W /O Operator to arrive and after contacting their office I found that job had been cancelled for today .
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 1412318881
 
| 1412318881
 
| 2002-12-12
 
| 2002-12-12
|
+
|  
| On location to witness plug job . The plug job was cancelled again today . Departed the location and went to the New Philadelphia office . I was advised by phone that they aren't going to plug the well until next week .
+
| On location to witness plug job . The plug job was cancelled again today . Departed the location and went to the New Philadelphia office . I was advised by phone that they aren't going to plug the well until next week .
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1686216299
 
| 1686216299
 
| 2002-11-20
 
| 2002-11-20
|
+
|  
 
| Arrive and found that service rig is over the hole and pulling tubing . Collected H2S reading at the 6 to 8 ppm range . Advise operator to maintain fluid level to avoid a possible kick . At this point there is not a way to control the well is a kick occurs . Check this well with Inspector Grimm due to the H 2 S potenial .The rig kis not running fast enough to be able to set plug today .
 
| Arrive and found that service rig is over the hole and pulling tubing . Collected H2S reading at the 6 to 8 ppm range . Advise operator to maintain fluid level to avoid a possible kick . At this point there is not a way to control the well is a kick occurs . Check this well with Inspector Grimm due to the H 2 S potenial .The rig kis not running fast enough to be able to set plug today .
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -1701414275
 +
| 2002-12-11
 +
|
 +
| On location to witness plug job . Waited on location and nobody showed up to plug the well while I was on location . Departed location and went to the New Philadelphia office . Talked with Inspector Mark Moreland and he advised that he had talked with North Coast personel and they advised that they are going to plug the well tomorrow .
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 1864244869
 
| 1864244869
 
| 2013-09-16
 
| 2013-09-16
|
+
|  
 
| On the day of my inspection I witnessed that the pit had been filled, vegetation was in place. All production equipment had been removed. Site passed according to 1509.072B.
 
| On the day of my inspection I witnessed that the pit had been filled, vegetation was in place. All production equipment had been removed. Site passed according to 1509.072B.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 648503960
 
| 648503960
 
| 2002-11-15
 
| 2002-11-15
|
+
|  
 
| Arrive on site to cover possible blow out of H2S On a well to be plugged .Found H2S at low level and gas at the wellhead that set off the lower explosive limit on gas detector . Found that the surface casing has colapsed down onto the surface casing . The
 
| Arrive on site to cover possible blow out of H2S On a well to be plugged .Found H2S at low level and gas at the wellhead that set off the lower explosive limit on gas detector . Found that the surface casing has colapsed down onto the surface casing . The
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 08:17, 16 July 2015

Well Details

Well ID: 34-067-20600
Loading map...
County: Harrison
Municipality:
Operator Name: EXCO - NORTH COAST ENERGY INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1983-02-06
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 40.20288371
Longitude: -81.27982087

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1985-0 28942.0 100.0
1987-0 9558.0 116.0
1988-0 4862.0 0.0
1989-0 2085.0 81.0
1990-0 1191.0 0.0
1991-0 907.0 0.0
1992-0 0.0 0.0
1993-0 0.0 0.0
1994-0 121.0 0.0
1995-0 0.0 0.0
1996-0 0.0 0.0
1997-0 0.0 0.0
1998-0 0.0 0.0
1999-0 0.0 0.0
2000-0 273.0 0.0
2001-0 0.0 0.0
2002-0 82.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1039704373 2002-11-18 Arrive to check on site after an explosion had occorred at wellsite . Found that the 8 inch casing appears to have collapsed and landed on the heavy wall conductor pipe with enough force to bell it outward . The well is not leaking badly at this time , there is reading of 18 TO 20 PPM H 2 S . Found that the operator is not going to arrive any time soon .
1039711345 2002-12-03 Rig is over the hole and is going in with tubing and will try and circulate well . Next rig had equipment problem and will reschedule work for Weds. Or Thurs.Review well with Inspector Grimm due to H 2S readings .
-1155455712 2002-12-11 On location to witness plug job . Waited on location and nobody showed up to plug the well while I was on location . Departed location and went to the New Philadelphia office . Talked with Inspector Mark Moreland and he advised that he had talked with North Coast personel and they advised that they are going to plug the well tomorrow .
1237972050 2002-11-19 W/O operator to arrive and again a no show ?
1287640570 2002-12-12 On location to witness plug job . The plug job was cancelled again today . Departed the location and went to the New Philadelphia office . I was advised by phone that they aren't going to plug the well until next week .
-1338394820 2002-12-04 W /O Operator to arrive and after contacting their office I found that job had been cancelled for today .
1412318881 2002-12-12 On location to witness plug job . The plug job was cancelled again today . Departed the location and went to the New Philadelphia office . I was advised by phone that they aren't going to plug the well until next week .
1686216299 2002-11-20 Arrive and found that service rig is over the hole and pulling tubing . Collected H2S reading at the 6 to 8 ppm range . Advise operator to maintain fluid level to avoid a possible kick . At this point there is not a way to control the well is a kick occurs . Check this well with Inspector Grimm due to the H 2 S potenial .The rig kis not running fast enough to be able to set plug today .
-1701414275 2002-12-11 On location to witness plug job . Waited on location and nobody showed up to plug the well while I was on location . Departed location and went to the New Philadelphia office . Talked with Inspector Mark Moreland and he advised that he had talked with North Coast personel and they advised that they are going to plug the well tomorrow .
1864244869 2013-09-16 On the day of my inspection I witnessed that the pit had been filled, vegetation was in place. All production equipment had been removed. Site passed according to 1509.072B.
648503960 2002-11-15 Arrive on site to cover possible blow out of H2S On a well to be plugged .Found H2S at low level and gas at the wellhead that set off the lower explosive limit on gas detector . Found that the surface casing has colapsed down onto the surface casing . The

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.